1CAN111301, Revised Inservice Inspection Summary Report for the Twenty-Fourth Refueling Outage (1R24)

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Revised Inservice Inspection Summary Report for the Twenty-Fourth Refueling Outage (1R24)
ML13310A450
Person / Time
Site: Arkansas Nuclear Entergy icon.png
Issue date: 11/05/2013
From: Pyle S
Entergy Operations
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
1CAN111301
Download: ML13310A450 (7)


Text

Entergy Operations, Inc.

1448 S.R. 333 Russellville, AR 72802 Tel 479-858-4704 Stephenie L. Pyle Manager, Licensing Arkansas Nuclear One 1CAN111301 November 5, 2013 U.S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, DC 20555

SUBJECT:

Revised Inservice Inspection Summary Report for the Twenty-Fourth Refueling Outage (1R24)

Arkansas Nuclear One, Unit 1 Docket No. 50-313 License No. DPR-51

REFERENCE:

Entergy Letter dated October 21, 2013, Inservice Inspection Summary Report for the Twenty-Fourth Refueling Outage (1R24) (1CAN101304)

(ML13295A077)

Dear Sir or Madam:

Entergy Operations, Inc., (Entergy) submitted the Arkansas Nuclear One, Unit 1 (ANO-1)

Inservice Inspection Summary Report for the twenty-fourth refueling outage (1R24) via the reference. This report was provided in accordance with Article IWA-6000 of Section XI of the 2001 Edition with the 2003 Addenda of the American Society of Mechanical Engineers Code.

The summary report contained an Owners Activity Report Form OAR-1 in place of the code-required forms.

This report was prepared at the completion of the refueling outage and submitted within 90 calendar days of the completion of the outage. This outage was completed on August 7, 2013.

During the Authorized Nuclear Inservice Inspectors review of the submitted report it was determined that some of the information that was provided was from previous OARs and not applicable to this report. Specifically Code Cases N-661 and N-513-1 were not utilized during the reporting period. In addition, the information in Table 1 of the report related to the HBD 18 repair was performed and reported correctly in the previous cycles report.

Based on the above, attached is the completed revised Form OAR-1 for ANO-1 for your information. Included with the form are tables listing the Items with Flaws or Relevant Conditions that Required Evaluation for Continued Service and Abstract of

1CAN111301 Page 2 of 2 Repair/Replacement Activities Required for Continued Service in accordance with Code Case N-532-4. The results that are contained in the revised form are for 1R24.

This letter contains no new regulatory commitments.

By means of this submittal, the reporting requirements of IWA-6000 are fulfilled for 1R24.

If you have any questions or require additional information, please contact me.

Sincerely, Original signed by David B. Bice for Stephenie L. Pyle SLP/rwc

Attachment:

Revised Form OAR-1 Owners Activity Report cc: Mr. Marc L. Dapas Regional Administrator U. S. Nuclear Regulatory Commission Region IV 1600 East Lamar Boulevard Arlington, TX 76011-4511 NRC Senior Resident Inspector Arkansas Nuclear One P. O. Box 310 London, AR 72847 U. S. Nuclear Regulatory Commission Attn: Mr. Kaly Kalyanam MS O-8B1 One White Flint North 11555 Rockville Pike Rockville, MD 20852

Attachment to 1CAN111301 Revised Form OAR-1 Owners Activity Report

Attachment to 1CAN111301 Page 1 of 4 FORM OAR-1 OWNER'S ACTIVITY REPORT Report Number OAR-1422 Plant Arkansas Nuclear One / 1448 S.R. 333, Russellville, AR. 72802 Unit No. 1 Commercial service date December 19, 1974 Refueling outage no. 1R24 (If applicable)

Current inspection interval Fourth (4th) Inspection Interval (1st, 2nd, 3rd, 4th, other)

Current inspection period Second (2nd) Inspection Period (1st, 2nd, 3rd)

Edition and Addenda of Section XI applicable to the inspection plan 2001 Edition with 2003 Addenda Date and revision of inspection plan November 23, 2010 / Revision 0 (SEP-ISI-101);

September 12, 2012 / Revision 1 (SEP-ISI-101)

July 18, 2013 / Revision 0 (SEP-ISI-ANO1-101)

Edition and Addenda of Section XI applicable to repairs and replacements, if different than the inspection plan Same _______________

Code Cases used: N-532-4 (if applicable)

CERTIFICATE OF CONFORMANCE I certify that (a) the statements made in this report are correct; (b) the examinations, tests meet the Inspection Plan as required by the ASME Code,Section XI; and (c) the repair/replacement activities and evaluations supporting the completion of 1R24 conform to the requirements of Section XI.

(refueling outage number)

Signed Original signed by Jamie Gobell / ASME Section XI Repair / Replacement Engineer Date _10/07/2013_______

Owner or Owner's Designee, Title CERTIFICATE OF INSERVICE INSPECTION I, the undersigned, holding a valid commission issued by the National Board of Boiler and Pressure Vessel Inspectors and the State or Province of Arkansas and employed by HSBCT of Hartford, Connecticut have inspected the items described in this Owner's Activity Report, and state that to the best of my knowledge and belief, the Owner has performed all activities represented by this report in accordance with the requirements of Section XI.

By signing this certificate neither the Inspector nor his employer makes any warranty, expressed or implied, concerning the repair/replacement activities and evaluation described in this report. Furthermore, neither the inspector nor his employer shall be liable in any manner for any personal injury or property damage or a loss of any kind arising from or connected with this inspection.

Original signed by Carl Thompson Commissions ARK-1054 Inspector's Signature National Board, State, Province, and Endorsements Date 10/08/2013

Attachment to 1CAN111301 Page 2 of 4 TABLE 1 ITEMS WITH FLAWS OR RELEVANT CONDITIONS THAT REQUIRED EVALUATION FOR CONTINUED SERVICE Examination Category Item Description Evaluation Description and Item Number N/A Flow Accelerated Corrosion degradation of Pipe wall thickness was measured to be less than the EBB-1-18 Feedwater piping component acceptance criteria (Tcrit). Piping was analyzed using Finite number EBB01P020A. Measured thickness Element Analysis and accepted for continued use as was 0.666 inches versus a Tcrit value of documented under EC-45816, CR-ANO-1-2013-00489 and 0.669 inches CR-ANO-1-2013-01132.

N/A Flow Accelerated Corrosion degradation of Pipe wall thickness was measured to be less than the EBB-1-18 Feedwater piping component acceptance criteria (Tcrit). Piping was analyzed using Finite number EBB01E004. Measured thickness Element Analysis and accepted for continued use as was 0.753 inches versus a Tcrit value of documented under EC-45816, CR-ANO-1-2013-00489 and 0.776 inches. CR-ANO-1-2013-01213.

Attachment to 1CAN111301 Page 3 of 4 TABLE 2 ABSTRACT OF REPAIR / REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description of Work Date Repair / Replacement Plan Class Completed Number & Work Order Number 1 Restraint Replace rear bracket due to wear in load 29-Sep-2012 Plan # WO-00281913-10 pin hole CR-ANO-2-2012-02249 1 Stud Replaced reactor closure head stud due to 5-Oct-2012 Plan # WO-52357868-06 thread damage CR-ANO-2-2012-02023 T3 Pipe Repair weld FW-36R1 in HCD-112-6 20-Jun-2013 Plan # WO-00338362-01 Service Water piping CR-ANO-1-2012-01853 1 Steam Generator E-24A tube plugging 18-Jul-2013 Plan # 52399714-09 WO 52399714 1 Steam Generator E-24B tube plugging 18-Jul-2013 Plan # 52399668-10 WO 52399668 2 Pipe Repair of socket weld FW-12GC2 on 7-Aug-2013 WO-00358952-03 CCB-1-1 piping due to pinhole leak in new CR-ANO-1-2013-02285 weld 1 Control Rod Drive Replaced CRDM top closure (Quick Vent) 14-Aug-2013 WO-52399792-13 Mechanism (CRDM)-12 assembly due to damage that occurred to R&R Plan # 50233739-13 the seating surface as a result of CR-ANO-1-2013-01708 and maintenance CR-ANO-1-2013-02626 1 CRDM-19 Replaced CRDM due to damage that 14-Aug-2013 WO-00297993-03 occurred to the seating surface as a result R&R Plan # 00297993-03 of maintenance CR-ANO-1-2011-02905

Attachment to 1CAN111301 Page 4 of 4 TABLE 2 (continued)

ABSTRACT OF REPAIR / REPLACEMENT ACTIVITIES REQUIRED FOR CONTINUED SERVICE Code Item Description Description of Work Date Repair / Replacement Plan Class Completed Number & Work Order Number 1 CV-1228 Replaced valve bonnet due to a scratch in 28-Aug-2013 Plan # 00296958-11 the pressure seal ring seating area WO 00296958 NOTE: ANO-1, Fourth Interval, Second Period