05000461/FIN-2014003-01
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Finding | |
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Title | Foreign Material in Relay Prevents Emergency Diesel Generator Output Breaker from Closing |
Description | The inspectors documented a self-revealing non-cited violation of Clinton Power Station Technical Specification 5.4.1, Procedures, for a failure to prevent foreign material from entering a relay associated with the Division 1 Diesel Generator. Specifically, contrary to station procedure CPS 8501.05, CV-2 Relay Inspection and Calibration with Doble Test Equipment, Revision 4, the licensee failed to verify that relay 227-DGIKA, CV-2 AB phase was clean and free of all foreign material. The foreign material prevented the relay from operating and satisfying the permissive logic required to close the Division 1 Diesel Generator output breaker resulting in having to declare the Diesel Generator inoperable. The relay was replaced and successfully tested and the licensee documented this issue in the corrective action program as IR 01600935. The finding was more than minor because it was associated with the procedure quality attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the availability, reliability and capability of systems that respond to initiating events to prevent undesirable consequences and is therefore a finding. Using IMC 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, issued June 19, 2012, Exhibit 2 for the Mitigating Systems Cornerstone, the inspectors answered Yes to the screening question under the Mitigating Systems Cornerstone Does the finding represent an actual loss of function of at least a single Train for > its Tech Spec Allowed Outage Time OR two separate safety systems out-ofservice for its Tech Spec Allowed Outage Time," since the finding represented an actual loss of function of at least a single Train for > its Tech Spec Allowed Outage Time of 14 days. Therefore, a detailed risk evaluation was performed using IMC 0609, Appendix A. The Senior Reactor Analysts (SRAs) evaluated the finding using the Clinton Standardized Plant Analysis Risk (SPAR) model version 8.17, Systems Analysis Programs for Hands-on Integrated Reliability Evaluations (SAPHIRE) version 8.1.0 and concluded that the risk increase to the plant due to this finding is very low (Green). The inspectors determined this finding affected the cross-cutting area of human performance in the aspect of work management where the organization implements a process of planning, controlling and executing work activities such that nuclear safety is the overriding priority. Specifically, the licensees implementation of their foreign material exclusion process for this maintenance activity lacked sufficient planning, controls and execution to prevent foreign material from entering a risk significant piece of safety related equipment. [IMC 0310 H.5] |
Site: | Clinton |
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Report | IR 05000461/2014003 Section 1R15 |
Date counted | Jun 30, 2014 (2014Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.15 |
Inspectors (proximate) | C Lipa E Sanchez Santiago K Carrington S Mischke W Schaup |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | H.5, Work Management |
INPO aspect | WP.1 |
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Finding - Clinton - IR 05000461/2014003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Clinton) @ 2014Q2
Self-Identified List (Clinton)
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