:on 980223,potential Air/Gas Intrusion in Chemical & Volume Control Sys Was Noted.Caused by Inadequate Initial Design.No Cause for Corrective Actions Because Both Flow Paths Were Operable| ML20247P389 |
| Person / Time |
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| Site: |
Millstone  |
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| Issue date: |
05/18/1998 |
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| From: |
Danni Smith NORTHEAST NUCLEAR ENERGY CO. |
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| To: |
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| Shared Package |
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| ML20247P381 |
List: |
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| References |
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| LER-98-016, LER-98-16, NUDOCS 9805270439 |
| Download: ML20247P389 (6) |
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text
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NRC f oRM 366 U.s. NUCLEAR REGULATORY Commission APPROVED BY OMB No. 3160 0104 EXPIRES 04/30/98 (4-95)
'30'W?,0=A"o"J'.?;3s? foTMs*""Jaro^" IGM n^c."' o^"AoStPa^ Mao 'sJ20?s%7c".!s'd ^."? la t
LICENSEE EVENT REPORT (LER) iSt^u's ';'cW;,*,^,'a",^/otaio $,s",^o",^T!s"J,,=;?"fc o
o Mn??h '"?J3J"'l#1"Je"! "J.%7e"o;"?#E#1'""
(See reverse for required number of digits / characters for each block)
FAC1fTV NAME fil DOCKET NUMBER (2)
PAGE (3)
Millstone Nuclear Power Station Unit 3 05000423 1 of 6 TITLE I4)
Potential Air / Gas intrusion in Chemical and Volume Control Systam EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
~
MONTH DAY YEAR YEAR SEQUENTIAL REVISloN MONTH DAY YEAR FACIUTY NAME DOCKET NUMBER NUMBER NUMBER 01 05 18 98 02 23 98 98 016 OPERATING 5
THis REPORT is SUBMITTED PURSUANT To THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE (9) 20.2201(b) 20.2203(a)(2)(v) 50.73(a)(2)(i) 50.73(a)(2)(viii)
POWER 000 20.2203(a)(1) 20.2203(a)t3)(i) 50.73(a)(2)(ii) 50.73(a)(2)(x)
LEVEL (10) 20.2203(a)(2)(i) 20.2203(a)(3)(ii) 50.73(a)(2)(iii) 73.71 20.2203(a)(2)(ii) 20.2203(a)l4) 50.73(a)(2)(iv) oTHER 20.2203(a)(2)(iii; 50.36(c)(1) 50.73(a)(2)(v)
Specify in Abstract below
~
20.2203(a)(2)(iv) 50.36(c)(2)
X so 73(a)(2)(vii)
LICENSEE CONTACT FoR THis LER (12)
NAME TELEPHONE NUMBER tinclude Area Codel David A. Smith, Manager, Unit 3 Regulatory Compliance (860)437-5840 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPROS 9
SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR X
YEs No submission 07 15 98 (If yes, complete EXPECTED submission DATE).
DATE (15)
ABSTRACT (Limit to 1400 spaces, Le., approximately 15 single-spaced typewntten tenes) (16)
On February 23,1998, with the unit in Mode 5, it was identified that there had been several Condition Reports (CRs) written since early 1997 describing Boric Acid pump air binding, or gas / air accumulation within the Boric Acid piping system. Gas / air accumulation within the system had resulted in the Boric Acid Pumps (3CHS*P2A and B) cavitating or becoming gas / air bound. Three primary pathways have been identified for gas / air intrusion: air introduced during batching operations, inadequate venting of connecting systems after maintenance, and hydrogen stripping. This gas / air binding pMnomenon has affected both trains of the Boric Acid Transfer (BAT) System. The Boric Acid system r: mains operable with the exception of the gravity boration pathway. The Reactor Water Storage Tank is operable as tn alternate boration path. These conditions are reportable pursuant to 10 CFR 50.73 (a)(2)(vii) as "any event where a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a single system designed to: (A) Shut down the r: actor and maintain it in a safe shutdown condition; [and] (D) Mitigate the consequences of an accident." This condition is historical. The cause for air intrusion into the Boric Acid Pumps is inadequate initial design of the Boric Acid system piping configuration. There were no adverse safety consequences from this condition. The unit has not l
experienced a reactivity event where operation of the BAT System has been needed, nor an event where emergency boration has been necessary.
The evaluation of hydrogen stripping / accumulation is ongoing, and the results of our investigation and corrective actions will be provided in a supplement to this report.
9805270439 980518
+
PDR ADOCK 05000423 S
PDR
I
.-U.S. NUCLEAR RESULAToRY Commission LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAoE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 2 of 6 98 016 01 TEXT (If rnore space is required, use additional copies of NRC forrn 366A) (17) 1.
Description of Event
On February 23,1998, with the unit in Mode 5, it was identified that there had been several Condition Reports (CRs) l written since early 1997 describing Bonc Acid pump air binding, or gas / air accumulation within the Boric Acid piping system. Gas / air accumulation within the system had resulted in the Boric Acid Pumps (3CHS*P2A and B) cavitating or becoming gas / air bound. Three primary pathways have been identified for gas / air intrusion: air introduced during Boric Acid batching operations, inadequate venting of connecting systems after maintenance, and hydrogen stripping. This g:s/ air binding phenomenon has affected both trains of the Boric Acid Transfer (BAT) System. The system remains operable with the exception of the gravity boration pathway. The Refueling Water Storage Tank (RWST) is operable as cn titemate boration path.
During the Nuclear Regulatory Commission (NRC) Inspection Manual Section 40500 Inspection, a question was raised regirding the adequacy of the root cause investigation associated with Condition Report (CR) M3-97-0954, dated May 14,1997, which attempted to determine the causes of the air binding problems with the Boric Acid Pumps. The root cause did not identify all the potential sources of air that could lead to air binding. CR M3-98-0975, dated February 19, 1998, was issued to re-evaluate the root cause.
(See attached figure for the following descriptions.)
Th3 boric acid batching process has led to air intrusion because the air filled space in the vertical section of piping belowl ths Boric Acid Batch Tank is swept into either the "A" or "B" Train when the batch tank drain valve is opened for filling End the respective train's pump is running for mixing during batching operations. Air binding of the Boric Acid Pumps could prevent the flow of boric acid from the system when called upon. Also, both pumps tie into a common header to the charging pumps. Sufficient air within the system could lead to air binding of one or more charging pumps as they tika suction from a common header. These conditions are reportable pursuant to 10 CFR 50.73 (a)(2)(vii) as "any event whIre a single cause or condition caused at least one independent train or channel to become inoperable in multiple systems or two independent trains or channels to become inoperable in a single system designed to: (A) Shut down the rtactor and maintain it in a safe shutdown condition; [and] (D) Mitigate the consequences of an accident." This condition is being dispositioned in accordance with the Millstone Corrective Action Program.
Tha Boric Acid Transfer System consists of two separate trains, each containing a Boric Acid Storage Tank (BAST),
Boric Acid Pump (to transfer borated water from the storage tank to either the Volume Control Tank (VCT), the RWST, or the suction of the charging pumps), a Boric Acid Batch Tank and associated piping and valves. The Boric Acid Batch Tcnk is located on the floor level abova the two trains. There is a long vertical drop in the piping from the batch tank to a connection with each system. During a batching operation a slug of air is trapped in this line and is swept into the operating Boric Acid Pump as it circulates the boric acid solution for mixing. A vent valve was installed on this section of piping during this outage.
Th2 physical configuration of the "A" Boric Acid Transfer System Gravity Boration lines contains a high point segment of piping which is at a much higher elevation (51 feet - 6 inches) than the elevation of the line running from the "A" Boric Acid Storage Tank to the suction of the "A" Boric Acid Pump (45 feet - 0 inches). This section of piping is a dead leg (only opened if gravity boration is needed) and provides a large volume to trap gas / air once i titroduced into the system. Our investigations have identified that some of the gas collected in these high points is hydrogen, The evaluation of hydrogen stripping / accumulation is ongoing, and the results of our investigation will be provided in a supplement to this report. It is presently believed that hydrogen is stripped in the miniflow lines on the Ch;rging pump discharge at the miniflow orifices, and the Reactor Coolant Pump number 1 seal leakoff. The hydrogen is then transported to the Charging pump suction header via the seal water retum path. Due to the piping configurations, N4C FORM 306A 495)
.-U.s. NUCLEAR REoVLAToRY Commission LICENSEE EVENT REPORT (LER) l TEXT CONTINUATION FdCILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3) f YEAR SEQUENTIAL Revision Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 3 of 6 98 016 01 TEXT 01more space is required, use additionalcopies of NRC Form 366A) (17}
l cny gas accumulation would migrate to the high points. A vent valve is installed on this section of piping.
l On the *B" Boric Acid Transfer System suction piping the vertical line from the Boric Acid Batch Tank contains a short horizontal segment at an elevation of 47 feet - 10 inches, which connects a short vertical segment that leads down to the horizontal suction line between the "B" Boric Acid Storage Tank and the suction of the *B* Boric Acid Pump (elevation of j
45 feet - 0 inches). This short horizontal section of piping at elevation 47 feet - 10 inches can also trap air during j
bitching operations.
II.
Cause of Event
This condition is historical. The cause for air intrusion into the Boric Acid Pumps is inadequate initial design of the Boric Acid system piping configuration. Inadequacies in the design of the piping layouts and the lack of vents in some locations resulted in trapped air in the system. Contributing factors were inadequate batching and venting procedures.
Th3 boric acid batching process used introduced air into the BAT System. The large amount of maintenance performed during this outage on portions of the Chemical and Volume Control and the Boric Acid Transfer Systems could have introduced air pockets into the Boric Acid Transfer System which may not have been adequately vented.
l It is presently believed that hydrogon is stripped in the miniflow lines on the Charging pump discharge at the miniflow orifices, and the Reactor Coolant Pump number i sealleakoff. The hydrogen is then transported to the Charging pump suction header via the seal water return path. Due to the piping configurations, any gas accumulation would migrate to th3 high points.
Ill. Analvsis of Event Th3 operability of the boric acid transfer portion of the Chemical and Volume Control System (Boron injection System) cnsures that sufficient negative reactivity controlis available during each mode of operation. Failure to maintain the Boric Acid Transfer System lines full of borated water could result in portions of the piping containing voids and/or cntriined gas pockets which could adversely affect the ability of the boric acid or charging pumps to function properly.
Th3 Boric Acid Transfer System and the Gravity Boration lines to the charging pumps are redundant to the Refueling Witir Storage Tank, which is the primary source of boration. This condition is significant in that if these trains were inoperable when the RWST was inoperable this could have resulted in the unit operating in a condition that was outside th3 units design basis.
There were no adverse safety consequences from this condition, in that the unit has not experienced a reactivity event where operation of the Boric Acid Transfer System has failed, nor a Design Basis Event where operation of the emergency boration function has been necessary.
IV. Corrective Action
There was no immediate impact on equipmerit operability and immediate corrective actions were not required because the unit was in full compliance with Technical Specification 3.1.2.1, "Boration Systems Flow Path - Shutdown," as both flow paths from the Refueling Water Storage Tank were OPERABLE.-__
NRC FORM 336A U.s. NUCLEAR REGULATORY CoMMtssK)N (4 95)
UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL Revision Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 4 of g 98 016 01 TEXT Uf more space is required, use additionalcopies of NRC Form 366A) (17)
Tha following corrective actions have been completed:
1.
Troubleshooting of the Boric Acid Transfer System to determine the source (s) of air intrusion into the system and corrective actions have been identified.
2.
Procedures have been revised to incorporate lessons learned from the troubleshooting effort to avoid air l
entrainment during Boric Acid Transfer System operation to address deficiencies in the design of the system.
3.
Vent valves have been added to the high points in the gravity boration pathways.
l Tha following corrective actions remain to be completed:
1.
Validate effectiveness of the revised batching procedure and revise as necessary. (Prior to Mode 2) 2.
Evaluate potential system modifications to minimize hydrogen stripping and eliminate locations which promote gas accumulation. (Prior to Refueling Outage 6) 3.
Investigate potential sources of hydrogen and recommend corrective actions to reduce or eliminate the gas buildup.
(Prior to Mode 2) 4.
Develop a surveillance program to periodically monitor the affected piping, to establish a gas accumulation rate and periodicity for venting gas to ensure charging pump operability (Prior to Mode 2) 5.
Establish a maximum allowed volume of gas in the boric acid gravity boration piping, to ensure pump operability and establish an allowable venting frequency. (Prior to Mode 2)
V.
Additional Information
None
Similar Events
Listed below are other historical LERs which reported conditions resulting from inadequate design. A majority of these sv;:nts were identified as a result of the Configuration Management Review Process.
LER 96-007-00 Containment Recirculation Spray, Quench Spray, and Safety injection System Outside Design Basis l
Due to Design Errors LER 96-009-02 Inoperable Shutdown Margin Monitors from Low Count Rate, Due to inadequate Design Control LER 96-013-00 Residual Heat Removal System Design Deficiency Due to Non-conservative Original Design Assumption LER 96-026-02 Non-Conservative Primary Grade Water Flow Rates Used in Boron Dilution Safety Analysis LER 97-003-00 Potential For Recirculation Spray System (RSS) Piping Failure Due To RSS Pump Stopping And j
Restarting During Accident Conditions LER 97-015-00 Potential Vortexing of Recirculation Spray System Pumps LER 97-021-00 Defective Design of RSS Expansion Joint Tie Rod Assembly LER 97-02840 Potential Loss of Net Positive Suction Head for Recirculation Spray System Pumps LER 97-029-00 Design Basis Concem on SGTR Analysis for MSPRBV k
r-NAC FORM 366A (4-951
,.-U.S. NUCLEAR REGULATORY COMMISSION (4 9 0 LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACUTY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEOuENTIAL REVISloN Millstone Nuclear Power Station Unit 3 05000423 NUMBER NUMBER 5 of 6 98 016 01 TEXT tif more space is required, use additional copies of NRC Form 366A) (17)
LER 97-031-00 RHR Valve Low Pressure Open Permissive Bistable Setting Set Non-Conservatively LER 97-035-00 Potential Nonconservatism for Steam Generator Water Level Low-Low Trip Setpoint Due to PMA Term Uncertainties l
LER 97-041-00 Voluntary Report: Operation of Service Water System With Only One Pump Operable LER 97-046-00 Containment Recirculation Spray System Cubicle Flood Potential LER 97-048-00 Oversized PGS Impeller Could Poten+.ially Result in Non-Conservative Boron Dilution Event LER 97-051-00 Design Deficiency for 4.16kV Feeder Fault Clearing Times Manufacturer Data Ells System Code Rnctor Coolant System..
..AB Chimical and Volume Control System...
..CB Ells Comoonent Code Pump..
..P Tank..
..TK Velve..
..V e
W FORM 366A U.S. NUCLEAR REGULATORY COMMISSION 14-9 3)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMSER (6) -
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 3-05000423 NUMBER NUMBER 6 Of 6 98 016 01 TEXT fit more space is required, use additional copies of NRC form 36GA) (17)
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| 05000245/LER-1998-001, Forwards LER 98-001-00,re Event Which Occurred on 980109 at Millstone Unit 1.Commitments Made within Ltr,Encl | Forwards LER 98-001-00,re Event Which Occurred on 980109 at Millstone Unit 1.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1998-001-02, :on 980109,MRP Determined That There Have Been Periods During Power Operation When Backup Pressure Regulator Was Oos.Caused by Inadequate Understanding of Safety Analysis.Evaluation Will Be Performed |
- on 980109,MRP Determined That There Have Been Periods During Power Operation When Backup Pressure Regulator Was Oos.Caused by Inadequate Understanding of Safety Analysis.Evaluation Will Be Performed
| 10 CFR 50.73(a)(2) | | 05000423/LER-1998-001-01, :on 980106,discovered Motor Pinion Gear Keys Sheared for Valve Actuators.Caused by Improper Installation of Key Matl That Was Weaker than Required for Function. Replaced Sheared Keys W/Stronger 4140 Matl |
- on 980106,discovered Motor Pinion Gear Keys Sheared for Valve Actuators.Caused by Improper Installation of Key Matl That Was Weaker than Required for Function. Replaced Sheared Keys W/Stronger 4140 Matl
| | | 05000423/LER-1998-001, Forwards LER 98-001-00,documenting Condition Determined Reportable at Millstone,Unit 3,on 980106.Commitments Made by Util,Encl | Forwards LER 98-001-00,documenting Condition Determined Reportable at Millstone,Unit 3,on 980106.Commitments Made by Util,Encl | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000336/LER-1998-001, :on 980108,ongoing Engineering Evaluations of Fault Clearing & Fuse Coordination for Vital 120 Volt AC Sys Occurred.Caused by Incomplete Engineering Evaluation of Fault Clearing.Changes Will Be Implemented |
- on 980108,ongoing Engineering Evaluations of Fault Clearing & Fuse Coordination for Vital 120 Volt AC Sys Occurred.Caused by Incomplete Engineering Evaluation of Fault Clearing.Changes Will Be Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000245/LER-1998-002-02, :on 980211,seal Welding Activities W/O Repair/ Replacement Plan Were Noted.Caused by Inappropriate Decision Making by ISI Coordinator.Evaluation of Each of Nine Seal Welds Was Performed |
- on 980211,seal Welding Activities W/O Repair/ Replacement Plan Were Noted.Caused by Inappropriate Decision Making by ISI Coordinator.Evaluation of Each of Nine Seal Welds Was Performed
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1998-002, Forwards LER 98-002-00,documenting Condition That Was Discovered at Millstone,Unit 1 on 980211.Util Commitments Made within Ltr,Listed | Forwards LER 98-002-00,documenting Condition That Was Discovered at Millstone,Unit 1 on 980211.Util Commitments Made within Ltr,Listed | 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1998-002-01, :on 980112,verification of ECCS Piping Full of Water Per TS 4.5.2.b.1 Was Not Being Met.Caused by Personnel Not Considering ECCS cross-tie Piping as Discharge Piping. Revised ECCS Venting Sp |
- on 980112,verification of ECCS Piping Full of Water Per TS 4.5.2.b.1 Was Not Being Met.Caused by Personnel Not Considering ECCS cross-tie Piping as Discharge Piping. Revised ECCS Venting Sp
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1998-002-01, Forwards LER 98-002-01,re ECC Sys Single Failure Vulnerability on 980109.LER Suppl Provides Info on Addl Discrepancies,Identified During Investigation of Condition & During Implementation of Associated Corrective Actions | Forwards LER 98-002-01,re ECC Sys Single Failure Vulnerability on 980109.LER Suppl Provides Info on Addl Discrepancies,Identified During Investigation of Condition & During Implementation of Associated Corrective Actions | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1998-002, Informs of Revised Completion Date to Complete Commitment Contained in LER 98-002-00, Verification of ECCS Piping Full of Water Per TS 4.5.2.b.1 Not Being Met. New Commitment Made by Util,Encl | Informs of Revised Completion Date to Complete Commitment Contained in LER 98-002-00, Verification of ECCS Piping Full of Water Per TS 4.5.2.b.1 Not Being Met. New Commitment Made by Util,Encl | | | 05000336/LER-1998-003, Forwards LER 98-003-00,documenting Event That Occurred at Unit 2 on 980113.Util Commitments Made within Ltr Included in Attachment 1 | Forwards LER 98-003-00,documenting Event That Occurred at Unit 2 on 980113.Util Commitments Made within Ltr Included in Attachment 1 | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-003-02, :on 980113,inadequate Evaluation Between Reactor Internals & Rv Occurred.Caused by Inadequate Design Review.Appropriate Structural Analyses Revised |
- on 980113,inadequate Evaluation Between Reactor Internals & Rv Occurred.Caused by Inadequate Design Review.Appropriate Structural Analyses Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1998-003, :on 980114,ISI Pressure Tests for Class 2 & 3 Sys Were Missed.Caused by Historical Program Interface Deficiencies.Procedure for Sys Pressure Tests Has Been Revised to Reflect Sys within Scope of ISI Program |
- on 980114,ISI Pressure Tests for Class 2 & 3 Sys Were Missed.Caused by Historical Program Interface Deficiencies.Procedure for Sys Pressure Tests Has Been Revised to Reflect Sys within Scope of ISI Program
| | | 05000336/LER-1998-004-02, :on 980316,auxiliary Feedwater Pump Performance Was Degraded.Cause of Condition Is Unknown.Pump Will Be Returned to Operable Status Prior to Mode 3 from Current Outage |
- on 980316,auxiliary Feedwater Pump Performance Was Degraded.Cause of Condition Is Unknown.Pump Will Be Returned to Operable Status Prior to Mode 3 from Current Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) | | 05000245/LER-1998-004-01, :on 980311,failure to Recognize Rod Block Monitor Inoperable Occurred.Caused by Personnel Error. Procedures Will Be Revised to Require & Document Monitoring of Local Power Range Monitor |
- on 980311,failure to Recognize Rod Block Monitor Inoperable Occurred.Caused by Personnel Error. Procedures Will Be Revised to Require & Document Monitoring of Local Power Range Monitor
| 10 CFR 50.73(a)(2)(i) | | 05000245/LER-1998-004, Forwards LER 98-004-00,documenting Condition That Was Discovered at Unit 1 on 980311.Util Commitments Made within Rept,Encl | Forwards LER 98-004-00,documenting Condition That Was Discovered at Unit 1 on 980311.Util Commitments Made within Rept,Encl | 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1998-004, :on 980114,EDG Intercoolant Coolers Were Not Capable of Meeting Design Criteria.Caused by Inadequate Implementation of GL 89-13 Section II Testing.Diesels Operability in Modes 5 & 6 Was Documented Via CAP |
- on 980114,EDG Intercoolant Coolers Were Not Capable of Meeting Design Criteria.Caused by Inadequate Implementation of GL 89-13 Section II Testing.Diesels Operability in Modes 5 & 6 Was Documented Via CAP
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000336/LER-1998-004-01, Forwards LER 98-004-01,re Event Determined Reportable on 980316 at Millstone Unit 2.Commitments Made by Util,Encl | Forwards LER 98-004-01,re Event Determined Reportable on 980316 at Millstone Unit 2.Commitments Made by Util,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1998-005-02, :on 980330,loss of S1 & S2 Power Supply Were Noted Due to Single Failure.Caused by Inadequate Design & Indequate Mod Review.Abt & Breaker Configuration for MCC EF3 & MCC FE3 Will Be Evaluated |
- on 980330,loss of S1 & S2 Power Supply Were Noted Due to Single Failure.Caused by Inadequate Design & Indequate Mod Review.Abt & Breaker Configuration for MCC EF3 & MCC FE3 Will Be Evaluated
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1998-005, Forwards LER 98-005-00,documenting Event That Occurred at Millstone Nuclear Power Station,Unit 1 on 980330.LER Being Submitted Per 10CFR50.73(a)(2)(ii).Util Commitments Made within Ltr,Listed | Forwards LER 98-005-00,documenting Event That Occurred at Millstone Nuclear Power Station,Unit 1 on 980330.LER Being Submitted Per 10CFR50.73(a)(2)(ii).Util Commitments Made within Ltr,Listed | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-005-01, Forwards LER 98-005-01 Re HELB Deficiencies for Piping Inside Containment on 980318.Commitments,encl | Forwards LER 98-005-01 Re HELB Deficiencies for Piping Inside Containment on 980318.Commitments,encl | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-005-02, Forwards LER 98-005-02,re HELB Deficiencies for Piping Inside Containment Identified on 980318.Commitments Made by Util Also Encl | Forwards LER 98-005-02,re HELB Deficiencies for Piping Inside Containment Identified on 980318.Commitments Made by Util Also Encl | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1998-005, :on 980116,AMSE Section XI Code Requirements Not Met in Scheduling & Performing Inspections of Pipe Supports or Welds Were Noted.Caused by Misinterpretation of Info.Isi Surveillance Procedure Was Revised |
- on 980116,AMSE Section XI Code Requirements Not Met in Scheduling & Performing Inspections of Pipe Supports or Welds Were Noted.Caused by Misinterpretation of Info.Isi Surveillance Procedure Was Revised
| | | 05000336/LER-1998-005, :on 980318,HELB Deficiencies for Piping Inside Containment Was Noted.Caused by Inadequate Consideration of HELB Requirements.Rept Was Submitted to NRC Discussing Applicability of leak-before-break Methodology |
- on 980318,HELB Deficiencies for Piping Inside Containment Was Noted.Caused by Inadequate Consideration of HELB Requirements.Rept Was Submitted to NRC Discussing Applicability of leak-before-break Methodology
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-006-01, :on 980327,reactor Bldg Closed Cooling Water Sys Outside Design Upon Loss of Svc Water Occurred.Caused by Inadequate Consideration of All Postulated Single Failure Events.Procedures Will Be Implemented |
- on 980327,reactor Bldg Closed Cooling Water Sys Outside Design Upon Loss of Svc Water Occurred.Caused by Inadequate Consideration of All Postulated Single Failure Events.Procedures Will Be Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-006, Forwards LER 98-006-00,documenting Event That Occurred at Millstone Nuclear Power Station,Unit 2 on 980327.LER Being Submitted Per 10CFR50.73(a)(2)(ii).NNECOs Commitments Made within Ltr Listed | Forwards LER 98-006-00,documenting Event That Occurred at Millstone Nuclear Power Station,Unit 2 on 980327.LER Being Submitted Per 10CFR50.73(a)(2)(ii).NNECOs Commitments Made within Ltr Listed | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1998-006, Forwards LER 98-006-00,documenting Condition Determined Reportable at Unit 3 on 980115.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | Forwards LER 98-006-00,documenting Condition Determined Reportable at Unit 3 on 980115.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-007-02, :on 980408,reanalysis of Ms Line Break Indicated Possible Fuel Failures.Cause Is Under Investigation.Siemens Analysis Will Be Completed Prior to Entering Mode 4 from Current Outage |
- on 980408,reanalysis of Ms Line Break Indicated Possible Fuel Failures.Cause Is Under Investigation.Siemens Analysis Will Be Completed Prior to Entering Mode 4 from Current Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1998-007, :on 980129,containment Bypass Leakage Was in Excess of TS Limits.Caused by non-conservative Decision Making (W/Respect to NRC Branch Technical Position). Calculation Review & Approval Has Been Improved |
- on 980129,containment Bypass Leakage Was in Excess of TS Limits.Caused by non-conservative Decision Making (W/Respect to NRC Branch Technical Position). Calculation Review & Approval Has Been Improved
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1998-007-01, Forwards LER 98-007-01,documenting Condition That Was Orginally Determined at Millstone,Unit 3 on 980129.LER Being Submitted Pursuant to 10CFR50.73(a)(2)(i)(B).NNECO Commitments Contained within Attachment 1 to Ltr | Forwards LER 98-007-01,documenting Condition That Was Orginally Determined at Millstone,Unit 3 on 980129.LER Being Submitted Pursuant to 10CFR50.73(a)(2)(i)(B).NNECO Commitments Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1998-007-01, :on 980408,noted That non-conservative Assumptions May Result in Violation of Fuel Centerline Temp Fuel Design Limit.Caused Indeterminate.Will Complete Siemens Analysis Prior to Entering Mode 4 from Current Outage |
- on 980408,noted That non-conservative Assumptions May Result in Violation of Fuel Centerline Temp Fuel Design Limit.Caused Indeterminate.Will Complete Siemens Analysis Prior to Entering Mode 4 from Current Outage
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-007, Forwards Corrected LER 98-007-00,documenting Event Which Occurred at Millstone Unit 2 on 980408.LER Is Being Resubmitted Due to Omission of Rept Date on Original Submittal.Commitments Made within Ltr,Encl | Forwards Corrected LER 98-007-00,documenting Event Which Occurred at Millstone Unit 2 on 980408.LER Is Being Resubmitted Due to Omission of Rept Date on Original Submittal.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-008-01, :on 980423,TS Violations Were Noted.Caused by Failure to Achieve Compliance to TS Requirements.Revised Appropriate Surveillance Procedures |
- on 980423,TS Violations Were Noted.Caused by Failure to Achieve Compliance to TS Requirements.Revised Appropriate Surveillance Procedures
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-008, Forwards LER 98-008-00,re Event Which Occurred at Millstone Unit 2,on 980423,per 10CFR50.73(a)(2)(i).Commitments Made within Ltr,Encl | Forwards LER 98-008-00,re Event Which Occurred at Millstone Unit 2,on 980423,per 10CFR50.73(a)(2)(i).Commitments Made within Ltr,Encl | 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1998-008, :on 980210,RS Sys Historically Outside of Design Basis as Result of Design Change.Caused by Inadequate Historical SE Program Design When Compared W/Current Standards.Lar Was Prepared & Submitted on 980303 |
- on 980210,RS Sys Historically Outside of Design Basis as Result of Design Change.Caused by Inadequate Historical SE Program Design When Compared W/Current Standards.Lar Was Prepared & Submitted on 980303
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1998-009, Forwards Revised Commitments Contained in LER 98-009-00 for Mnps,Unit 3, Containment Radiation Monitor CMS*22 Setpoints Non-Conservative W/Respect to Conforming W/Commitments Made to Reg Guide 1.45 within Fsar | Forwards Revised Commitments Contained in LER 98-009-00 for Mnps,Unit 3, Containment Radiation Monitor CMS*22 Setpoints Non-Conservative W/Respect to Conforming W/Commitments Made to Reg Guide 1.45 within Fsar | | | 05000336/LER-1998-009-01, :on 980501,LBLOCA Analysis Indicates Peak Clad Temp Could Exceed 2200 Degrees F.Caused by Failure to Identify Excessive Variability.Reanalyzed LBLOCA Using Current & Corrected Evaluation Models |
- on 980501,LBLOCA Analysis Indicates Peak Clad Temp Could Exceed 2200 Degrees F.Caused by Failure to Identify Excessive Variability.Reanalyzed LBLOCA Using Current & Corrected Evaluation Models
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 21.21(a)(2), Interim Report for Comply or Defect in Component 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-009, Forwards LER 98-009-00,documenting Event Which Occurred at Millstone Unit 3 on 980501.Commitments Made within Ltr,Encl | Forwards LER 98-009-00,documenting Event Which Occurred at Millstone Unit 3 on 980501.Commitments Made within Ltr,Encl | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-010, Forwards LER 98-010-00,documenting Event That Occurred at Unit 2 on 980508.Util Commitments Made within Ltr Included in Attachment 1 | Forwards LER 98-010-00,documenting Event That Occurred at Unit 2 on 980508.Util Commitments Made within Ltr Included in Attachment 1 | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-010-01, :on 980508,discovered That Encl Bldg Surveillance Procedure Did Not Adequately Verify Leak Integrity of Encl B.Caused by Inadequate Evaluation of Phenomenon Described in NRC Info Notice.Amend Implemented |
- on 980508,discovered That Encl Bldg Surveillance Procedure Did Not Adequately Verify Leak Integrity of Encl B.Caused by Inadequate Evaluation of Phenomenon Described in NRC Info Notice.Amend Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1998-010, :on 980211,failed to Meet TS Definition of Analog Channel Operational Test of Unit 1 Main Stack Noble Gas Activity Monitor.Caused by Inadequate Verification of Compliance W/Unit 3 Ts.Procedures Will Be Revised |
- on 980211,failed to Meet TS Definition of Analog Channel Operational Test of Unit 1 Main Stack Noble Gas Activity Monitor.Caused by Inadequate Verification of Compliance W/Unit 3 Ts.Procedures Will Be Revised
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-011-01, :on 980519,determined That Valves Had Been Closing Completely Under No Flow Conditions.Caused by Improper Valve Setup & Failure to Verify Adequate Valve Closure.Valves Disassembled |
- on 980519,determined That Valves Had Been Closing Completely Under No Flow Conditions.Caused by Improper Valve Setup & Failure to Verify Adequate Valve Closure.Valves Disassembled
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-011, Forwards LER 98-011-00,documenting Event That Occurred at Unit 2 on 980502.Util Commitments Made within Ltr Included in Attachment 1 | Forwards LER 98-011-00,documenting Event That Occurred at Unit 2 on 980502.Util Commitments Made within Ltr Included in Attachment 1 | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1998-011, :on 980218,failed to Adequately Test Turbine Driven Auxiliary Feedwater Pump.Caused by Inadequate Interface Among Organization.Tdafw Pump Will Be Tested |
- on 980218,failed to Adequately Test Turbine Driven Auxiliary Feedwater Pump.Caused by Inadequate Interface Among Organization.Tdafw Pump Will Be Tested
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1998-012-01, Forwards LER 98-012-01,documenting Addl Info Pertaining to Condition That Was Determined Reportable on 980218. Attachment 1 Contains Commitments in Response to Event | Forwards LER 98-012-01,documenting Addl Info Pertaining to Condition That Was Determined Reportable on 980218. Attachment 1 Contains Commitments in Response to Event | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1998-012, Forwards LER 98-012-00,re Event Which Occurred at Millstone Unit 2 on 980521.Commitments Made within Ltr,Encl | Forwards LER 98-012-00,re Event Which Occurred at Millstone Unit 2 on 980521.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1998-012, :on 980218,potential Failure of Rhrps Due to Loss of Mim Flow Protection,Was Reported.Caused by Lack of Documented Review & Analysis of Historical Design Deficiency.Performed DCR M3-98013 |
- on 980218,potential Failure of Rhrps Due to Loss of Mim Flow Protection,Was Reported.Caused by Lack of Documented Review & Analysis of Historical Design Deficiency.Performed DCR M3-98013
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1998-012-01, :on 980521,nonconservative Assumptions in Facility Loss of Normal FW Analysis Was Noted.Caused by Incorrect Calculation of SG Inventory During Lonf Event. Reanalysis of FSAR Loss of Normal FW Analysis Was Completed |
- on 980521,nonconservative Assumptions in Facility Loss of Normal FW Analysis Was Noted.Caused by Incorrect Calculation of SG Inventory During Lonf Event. Reanalysis of FSAR Loss of Normal FW Analysis Was Completed
| 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-013, Forwards LER 98-013-00,re Event Which Occurred at Millstone Unit 2 on 980526.Commitments Made within Ltr,Encl | Forwards LER 98-013-00,re Event Which Occurred at Millstone Unit 2 on 980526.Commitments Made within Ltr,Encl | 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000336/LER-1998-013-01, :on 980526,shutdown Cooling Sys Was Over Pressurized by Inadvertent Hpsip Start.Caused by Inadequate Evaluation in Original Plant Design.Appropriate Actions Were Taken to Ensure Sys Complies W/Design & Licensing Basis |
- on 980526,shutdown Cooling Sys Was Over Pressurized by Inadvertent Hpsip Start.Caused by Inadequate Evaluation in Original Plant Design.Appropriate Actions Were Taken to Ensure Sys Complies W/Design & Licensing Basis
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) |
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