text
.
QVg
'Af M
teiepnone (4:n 393-6000 "8%%"*
Shippingwt PA 15onW November 19, 1990 4
ND3MNO:3061 i
Beaver Valley Power Station, Unit No. 2 Docket No. 50-412, License No. NPF-73 LER 90-022-00 United States Nuclear Regulatory Commission Document Control Deck Washington, DC 20555 Gentlemen:
In accordance with Appendix A,
Beaver Valley Technical Specifications, the following. Licensee Event Report is submitted:
LER 90-022-00, 10 CFR 50.73.a.2.ii.B, " Inadequate Electrical Isolation between Control and Protection Circuits".
Very_truly yours, T.
P. Noonan General Manager Nuclear Operations s1 Attachment 901127I:)b76 901119 f
Ff0R ADOCK 05000412
/
5 PDC
_/
l t
s Novemb3r.19, 1990-ND3MNO:3061 Page two cc: Mr. T. T. Martin, Regional Administrator United States Nuclear Regulatory Commission Region 1 475 Allendale Road i
King of Prussia, PA 19406 c. A. Roteck, Ohio Edison i
76 S. Main Street i
Akron, OH 44308 Mr. A. DeAgazio, BVPS Licensing Project Manager 4
United States Nuclear Regulatory Commission Washington, DC 20555 J.
Beall, Nuclear Regulatory Commission, BVPS Senior Resident Inspector Larry Beck Cleveland Electric 6200 Oak Tree Blvd.
Independence, Ohio 44101 INPO Records Center Suite 1500 1100 Circle 75 Parkway Atlanta, GA 30339 G.
E. Muckle, Factory Mutual Engineering 680 Anderson Drive #BLD10 Pittsburgh, PA 15220-2773 Mr. J. N. Steinmetz, Operating Plant Projects Manager Mid Atlantic Area Westinghouse Electric Corporation-Energy-Systems Service Division Box 355 Pittsburgh, PA 15230 Mr. Richard Janati Department of Environmental Resources-P. O.
Box 2063 16th Floor, Fulton Building Harrisburg, PA 17120-Director, Safety Evaluation & Control Virginia Electric & Power Co.
P.O.
Box.26666 One James River Plaza Richmond, VA 23261
Novcmbar if, 1990 ND3MNO:306'.
l W. Hartley l
Management Analysis Company 112671 High Bluff Drive l
San Diego, CA 92130-2025 l
{
t J. M. Riddle NUS Operating Service Corporation Park West II Cliff Mine Road Pittsburgh, PA 15275 l
l'
I RC Pg 300 U.S. NUCLE AR f.51 ult TLAY COMMIS5lON APPROvtD oms NO 3160 0104 l
IKPl7 El 4/30/92 ESTIMATED BURDEN PER KtSPONSt TO COMPLY YtTH THIS LICENSEE EVENT REPORT (LER)
CO.?MtNis'?UOEDi'3 e'U' ' " "' ET'ii)#8 Y"?HE RICES DEN
^MURo"# "'M"'M"A"W'Es*N R'd"i'#^"
THE PAPERWORK REOUCTION PROJECT 0 16041041 OF F ICE OF MANAGEMENT AND BUDOti, W ASHINOTON. DC 20603.
FACILITY NAME til
' DOCK S T NUMSE R (21 PAGE (3i Beaver Valley Power Station Unit 2 oi5l0loIol411l2 1 lOFl 013 flTLE 141 l
Inadequate Electrical isolation between Control and Protection Circuits tytNT Daf t (El LIR NUMetR tel REPORT DAf t 17)
OTHER 7 ACILITIES INVOLvtD tel MONT H DAY YEAR YEAR
'n
[*j, MONTH DAY VGAR F ACILit v hAMES DOCEtt NUM9tRl51 N/A o 15 ] o'l o l o i i j 1l0 1l 9 90 9l0 0l 2l 2 0l 0 1l1 1l9 9 l0 oisio,o,o,, i Opt R ATING THIS REPORT IS SUeMITTIO PURSUANT TO THE RhOUIREMENTS OF to CFR i- (Chece ew or more of f** 'ono**si Ull 6400I m 5
to 40 i.i 20 40.iei
.0.73ieH2io.i 73.7 i.i no, Oi0i0 20 406teHt Hil 60.=leH1) 90.73teH2ilil 73.71(al n.0.i.ninal
.0.=ieim
.0 nielun..I
=;sg,g,-,
20 405(eH1Hali 60.73teH2101 60 73(eH2HvtHHA)
J66Al 20 406(eH1Hivl
[
60.736eH2Hal 80.73teH2Hviklit) 20 400(alt
- Hvi 50.73teH2Hdel 60.73 eH2Hal LICENSEE CONTACT FOR THil EER (til NAME TELEPHONE NUMetR AHE A COOS T.P. Noonan, General Manager Nuclear Operations 4 1 1l2 6l 4 1 3l-t 1l2l5l8 COMPLEf t ONE LINE FOR E ACH COMPONENT F ALLURE DESCRittD IN TH18 REPORT (131 m
M'y % ^ C~
"'y'o g",Ig'I 0
MA%AC-RtPORi A E CAust SYSTEM COMPONENT n
CAU$t SvtTEM COMPONENT y
pp I
I I I i 1 2,0 Y
I I I I I I I I
I I I I I i SUPPLEMENTAL REPORT EXPECTED it41 MONTH DAY YEAR 3
5V4MisslON Yis Ilf vos tometere EXPECTEO SutMo$$10h DA Yli NO l
l l
A T R ACT u,-,..,m e.. e. e.,,...,, e.,,,,Me., e.,*.,*,*,v r,mo,.eo n el During an engineering review for a
design change between the control and protection circuits associated with the Containment High Pressure bistables, - no documentation could be located for the electrical isolation qualification of the existing interface device (Westinghouse 7300 NCT card part #2837A91)
Westinghouse was contacted on-10/39/90 and verified that the listed card had never been qualified as an isolation device.
Qualified isolation devices have been installed in the circuits.
If a fault had occurred in the control (annunciator) portion of the circuit, it potentially would have affected - the operability of the Containment High Pressure protection circuite D
i NRC Form 3541640 l
1 wn,c *oaM sesA u.s. wuctaAn is vu tony coMMierios.
- exnzi, oa LlcENSEE EVENT REPORT (LER)
Wa"My o*,yM,M?of,5,5;o".,'t,i. c M.',"o'n" 'n'!
o TEXT CONTINUATION i#'"4,'/11*MMjuUt%R'c'"','!df v"'"MfA P PE RWO Ri JT N RJ h 6.
II IC OF MANAGEMENT AND SUDGtY.W ASHINGTON,DC 2060J.
f ACitiTV hAMt (H DOCK t Y NUMDER (21 LE A NUMetR ($)
PAOS (3)
TI""
am v
a 1
Beaver Va' ley Power Station Unit 2 0161010 l o l 411 l 2 9l0 0!2l2 0l0 0 12 0F Ol3 text <n
=,
r.
m.wime r, asam on Description of Fvent During Beaver Valley Unit 2's second refueling outage, a design change was installed ta provide control room indication when the Refueling Water Storage Tank The RWST is(RWST) Low-Low Level bistables are placed in bypass.
used as the initial water source for the Coatainment Depressurization and Quench Spray system.
In the
- coursc, of the engineering review associated with this design L
- change, the isolation qualification of four cards used in the containment Pressure Hi-3 bistables' circuitry was questioned.
These bistables are used to actuate the quench spray system in the event of high containment pressure.
The involved cards are Westinghouse 7300 NCT cards part #2837A91, the comparator trip switch cards for containment pressure protection (channels 2LMS*PTD950, 2LMS*PTD951, 2LMS*PTD952 and'2LMS*PTD953).
Outputs from these cards also cJo to control circuitry (annunciators) associated with high containment pressure.
\\
\\
After documentation on site could not be located concerning the electrical isolation capabilities of these cards, Westinghouse was questioned about this matter on 10/10/90.
On 10/19/90, Westinghouse verified that the NCT cards had never been qualified z
as isolation devices.
Based on
- this, a qualified isolation device (Westinghouse ANI6 card) was installed in each circuit between the output of the NCT cards and the annunciators.
Cause of Event
This event was due to a design error in directly' connecting the control and protection circuits for the containment high pressure bistables.
Corrective Actions
1)
As stated above, qualified isolation devices have been installed in the circuits.
These devices will prevent a
fault in the annunciator part of the circuit from affecting the protection functions.
I wac e- =A m.,
N,,,g,,g o u oCti m.sutATo.,co
.N GXT1%ES 4/30/97 LICENSEE EVENT REP 3RT (LER)
,, 6"^'A?o',$8'*d%l',7a"ldT'.#7',Y l'oTW "'!
TEXT CONTINUATION 2Nt"n't,&%"u'21"oME"f'.M!'c'n,'!d l,".'"'CNf!
1 P A,E RWO m t puCTION 6
Of MANAGEMENT AND BUDGET. WASHINGTON. DC 20603.
P AC.Lif Y NAM 4 Of DOCKit NVM.tR (23 LtR NUMetR let PA06 (3) d'"
No vva n Beaver Valley Power Station Unit 2 01510 l 0 l 0 l 4 l1 l 2 9l0 0l2l2 0l0 013 0F 0l3 TEXT wni an N w
.me==wwe r ms4wim
Previous Similar Events
Review of station documents identified no previous similar events.
Event Reportability Due to a design error, a fault in the annunciator control circuit could have resulted in a failure of the containment high pressure l
protection circuit. -Based on this potential this event is being reported under 10CFR50.73.a.2.ii.B
(" Condition that was outside the design basis of the plant").
Additionally, the station is reviewing this event to determine
reportability
per 10CFR21.21
(" Notification of failure to comply").
I
Safety Analysis
A failure of the control / annunciator portion of the circuit may have induced a fault in the Containment High Pressure protection circuit.
This fault could.potentially have affected all four channels of containment high pressure protection, defeating the automatic initiation of the. Containment Depressurization System.
NRC Perin 306A (649s
|
|---|
|
|
| | | Reporting criterion |
|---|
| 05000412/LER-1990-001, :on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to Svc |
- on 900107,high Radiation Alarm Received on Steam Generator Blowdown (SGBD) Sample Radiation Monitor, Causing SGBD Sys Isolation.Caused by Crud Particles Swept Into Monitor.Monitor Purged & Returned to Svc
| | | 05000412/LER-1990-002-02, :on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure Revised |
- on 900217,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.Caused by Failure to Complete Tech Spec Required post-maint Test. Post-maint Test Procedure Revised
| | | 05000412/LER-1990-002-01, :on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on Transmitter |
- on 900117,steam Generator B Channel 3 Pressure Transmitter Failed Low & Declared Inoperable.On 900119, Discovered That Channel Returned to Svc W/O Completing Required Time Response Testing on Transmitter
| | | 05000334/LER-1990-002, :on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance Issued |
- on 900114,120-volt Ac Inverter for Vital Bus 3 Experienced Blown Dc Input Fuse When Inverter Bypassed & Aligned to 480-volt Ac Emergency Power.Caused by Mgt Action. Administrative Guidance Issued
| | | 05000412/LER-1990-003-01, :on 900403,determined That Surveillance Test for Battery 3 Not Performed on Scheduled Date of 900329. Caused by Personnel Error.Inpo Human Performance Evaluation Sys Analysis Performed & Procedures Revised |
- on 900403,determined That Surveillance Test for Battery 3 Not Performed on Scheduled Date of 900329. Caused by Personnel Error.Inpo Human Performance Evaluation Sys Analysis Performed & Procedures Revised
| | | 05000334/LER-1990-003, :on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 Initiated |
- on 900110,determined That Recirculation Spray HX River Water Radiation Monitor Sample Lines Lacked Automatic,Remote Manual or Locked Shut Isolation Valve. Exemption Request from GDC 57 Initiated
| | | 05000412/LER-1990-004, :on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Incorrect Assessment of Plant Configuration Prior to Breaker Closure. Safety Injection Sys Reset |
- on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Incorrect Assessment of Plant Configuration Prior to Breaker Closure. Safety Injection Sys Reset
| | | 05000412/LER-1990-004-01, :on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal Reset |
- on 900423,inadvertent ESF Actuation Occurred During Safeguards Protection Sys Testing.Caused by Personnel Closing Breaker Before Resetting Safety Injection Sys Signal.Signal Reset
| | | 05000334/LER-1990-004, :on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel Counseled |
- on 900124:discovered That Control Rod Positions Not Recorded on Operator Logs on 890425 When Control Rod Insertion Limit Monitor & Deviation Alarm Out of Svc.Cause Not Stated.Personnel Counseled
| | | 05000412/LER-1990-005-01, :on 900424,discovered That Three Valves in Quench Spray Chemical Addition Sys Had Spuriously Closed & Review Found That Two Had Closed on 900423.Caused by Error in Switch Calibr Procedures.Procedures Revised |
- on 900424,discovered That Three Valves in Quench Spray Chemical Addition Sys Had Spuriously Closed & Review Found That Two Had Closed on 900423.Caused by Error in Switch Calibr Procedures.Procedures Revised
| | | 05000412/LER-1990-005, :on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21 |
- on 900209,defect Found in Casing of Limitorque Model HBC-1 Gear Operators,Causing Valve Motion to Cease Prematurely in Open Direction.Caused by Excess Matl on Housings.Also Reported Per Part 21
| | | 05000412/LER-1990-006, :on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time Requirements |
- on 900605,containment Isolation Valves Exceeded Stroke Time Limit,Per Tech Spec 3.6.3.1.Caused by Deficient Surveillance Program.Surveillance Procedures Revised to Include Stroke Time Requirements
| | | 05000334/LER-1990-006, :on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer |
- on 900227,plant Operation in Excess of Licensing Basis.Caused by Failure of Computer to Synchronize File Addresses in Task 3D.Heat Balance Calculations Reverified Using Data from Plant Variable Computer
| | | 05000412/LER-1990-007-01, :on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal Drained |
- on 900622,refueling Cavity Drain Flanges Found to Be Installed During Operation.Caused by Deficiency in Transfer Canal Draining Procedure.Procedure Revised to Verify Removal of Flanges After Canal Drained
| | | 05000412/LER-1990-007, Responds to NRC Re Deviation 50-412/90-12-01 Noted in Insp Rept 50-412/90-12.Corrective Actions:Procedure OM 2.20-4.I Revised to Require Removal of Flanges Following Drain Operations & LER 90-007-00 Issued | Responds to NRC Re Deviation 50-412/90-12-01 Noted in Insp Rept 50-412/90-12.Corrective Actions:Procedure OM 2.20-4.I Revised to Require Removal of Flanges Following Drain Operations & LER 90-007-00 Issued | | | 05000334/LER-1990-008, :on 900401,RCS Letdown Isolation/Esf Actuation Occurred.Erratic Automatic Response of Condenser Steam Valve PCV-MS-106A Caused RCS Temp to Decrease Below Tech Spec Min. Operators Took Manual Control & Shut Valve |
- on 900401,RCS Letdown Isolation/Esf Actuation Occurred.Erratic Automatic Response of Condenser Steam Valve PCV-MS-106A Caused RCS Temp to Decrease Below Tech Spec Min. Operators Took Manual Control & Shut Valve
| | | 05000412/LER-1990-008-01, :on 900702,reactor Trip Occurred,Resulting from Turbine/Generator Trip.Caused by Personnel Error Which Resulted in Protection Relay Actuation.Event Reviewed W/Personnel & Design Mod Being Reviewed |
- on 900702,reactor Trip Occurred,Resulting from Turbine/Generator Trip.Caused by Personnel Error Which Resulted in Protection Relay Actuation.Event Reviewed W/Personnel & Design Mod Being Reviewed
| | | 05000412/LER-1990-009-01, :on 900902,letdown Isolation on Loss of Containment Instrument Air Pressure Occurred.Caused by Deviation from Surveillance Procedure to Protect Plant Equipment from Unnecessary Stress |
- on 900902,letdown Isolation on Loss of Containment Instrument Air Pressure Occurred.Caused by Deviation from Surveillance Procedure to Protect Plant Equipment from Unnecessary Stress
| | | 05000412/LER-1990-010-01, :on 900904:letdown Isolation Occurred Due to Low Pressurizer Water Level.Caused by Interaction of Control Sys Dump Operation Combined W/Effects of Hydraulic Coupling of Rcs.Pressurizer Level Restored |
- on 900904:letdown Isolation Occurred Due to Low Pressurizer Water Level.Caused by Interaction of Control Sys Dump Operation Combined W/Effects of Hydraulic Coupling of Rcs.Pressurizer Level Restored
| | | 05000334/LER-1990-010, :on 900714,automatic Isolation of Reactor Coolant Letdown Sys Initiated When Transient/Cooldown Caused Pressurizer Level to Decrease Below Setpoint.Msiv Stroke Time Surveillance Tests Revised |
- on 900714,automatic Isolation of Reactor Coolant Letdown Sys Initiated When Transient/Cooldown Caused Pressurizer Level to Decrease Below Setpoint.Msiv Stroke Time Surveillance Tests Revised
| | | 05000334/LER-1990-011, :on 900719,ESF Actuation - Inadvertent Trip of Reactor Coolant Pump a Occurred During Maint Surveillance Procedure.Caused by Personnel Error.Procedures Revised |
- on 900719,ESF Actuation - Inadvertent Trip of Reactor Coolant Pump a Occurred During Maint Surveillance Procedure.Caused by Personnel Error.Procedures Revised
| | | 05000412/LER-1990-011, :on 900906,ESF Actuation & Containment Purge Occurred Due to High Radiation Signal.Caused by Electrical Disturbances Due to Lightning Strike.Damaged Instruments Replaced |
- on 900906,ESF Actuation & Containment Purge Occurred Due to High Radiation Signal.Caused by Electrical Disturbances Due to Lightning Strike.Damaged Instruments Replaced
| | | 05000412/LER-1990-012-01, :on 900913,ESF Actuation Involving Containment Purge Isolation Occurred.Caused by Communication Error by Personnel.Maint Surveillance Procedures for Control Room Radiation Monitors to Be Revised |
- on 900913,ESF Actuation Involving Containment Purge Isolation Occurred.Caused by Communication Error by Personnel.Maint Surveillance Procedures for Control Room Radiation Monitors to Be Revised
| | | 05000334/LER-1990-012, :on 900801,control Room Received 2 Battery Charger Failure Alarm.Caused by Failure of Battery Input Breaker a Phase Lug.Failed Input Breaker Replaced W/ Qualified,Equivalent Spare Breaker |
- on 900801,control Room Received 2 Battery Charger Failure Alarm.Caused by Failure of Battery Input Breaker a Phase Lug.Failed Input Breaker Replaced W/ Qualified,Equivalent Spare Breaker
| | | 05000334/LER-1990-013, :on 900815,control Room Emergency Breathing Air Pressurization Sys Actuated,Pressurizing Common Control Room Envelope.Caused by Erroneous Signal Spike.Monitor Output Signals Disabled |
- on 900815,control Room Emergency Breathing Air Pressurization Sys Actuated,Pressurizing Common Control Room Envelope.Caused by Erroneous Signal Spike.Monitor Output Signals Disabled
| | | 05000412/LER-1990-013-01, :on 900915,ESF Actuation Containment Purge Isolation Occurred During Reactor Cavity Fill.Caused by Water Turbulence.Operators Verified Containment Purge Isolation Dampers Closed in Response to Alarm |
- on 900915,ESF Actuation Containment Purge Isolation Occurred During Reactor Cavity Fill.Caused by Water Turbulence.Operators Verified Containment Purge Isolation Dampers Closed in Response to Alarm
| | | 05000412/LER-1990-014-01, :on 900916,ESF Actuation - Containment Purge Isolation Occurred During Upper Internals Lift |
- on 900916,ESF Actuation - Containment Purge Isolation Occurred During Upper Internals Lift
| | | 05000334/LER-1990-014, :on 900831,ESF Actuation Steam Generator Blowdown Isolation Occurred.Caused by Failure of Steam Driven Auxiliary Feedwater Pump Discharge Pressure Switch. Pressure Switch Replaced |
- on 900831,ESF Actuation Steam Generator Blowdown Isolation Occurred.Caused by Failure of Steam Driven Auxiliary Feedwater Pump Discharge Pressure Switch. Pressure Switch Replaced
| | | 05000412/LER-1990-015, :on 900913,insp Discovered 25 Containment Liner Weld Test Channel Vent Plugs Missing |
- on 900913,insp Discovered 25 Containment Liner Weld Test Channel Vent Plugs Missing
| | | 05000334/LER-1990-015-01, :on 901006,ESF Actuation Resulted in Closure of Main Steam Trip Valve During Partial Stroke Testing of MSIVs |
- on 901006,ESF Actuation Resulted in Closure of Main Steam Trip Valve During Partial Stroke Testing of MSIVs
| | | 05000412/LER-1990-016, :on 900921,svc Water Sys Flow Found to Be Blocked Due to Buildup Corrosion Products |
- on 900921,svc Water Sys Flow Found to Be Blocked Due to Buildup Corrosion Products
| | | 05000334/LER-1990-016-01, :on 901024,ESF Actuation - Low Head Safety Injection Recirculation Valve Closed During Testing |
- on 901024,ESF Actuation - Low Head Safety Injection Recirculation Valve Closed During Testing
| | | 05000334/LER-1990-017-01, :on 901027,auxiliary Bldg Ventilation Relignment Occurred Due to Radiation Monitor Alarm |
- on 901027,auxiliary Bldg Ventilation Relignment Occurred Due to Radiation Monitor Alarm
| | | 05000412/LER-1990-017, :on 900927,during Recirculation Spray Pump Test,Pumps B,C & D Did Not Start After Containment Isolation Phase B Signal.Caused by Delay Timer Setpoint Drift.Timers Replaced |
- on 900927,during Recirculation Spray Pump Test,Pumps B,C & D Did Not Start After Containment Isolation Phase B Signal.Caused by Delay Timer Setpoint Drift.Timers Replaced
| | | 05000334/LER-1990-017, :on 901027,ESF Actuation - Radiation Monitor Alarm Caused Auxiliary Bldg Ventilation Realignment |
- on 901027,ESF Actuation - Radiation Monitor Alarm Caused Auxiliary Bldg Ventilation Realignment
| | | 05000412/LER-1990-018, :on 901026,ESF Actuation - Inadvertent Diesel Start Occurred & Deficiency Discovered in D/G Ventilation Fan Circuit |
- on 901026,ESF Actuation - Inadvertent Diesel Start Occurred & Deficiency Discovered in D/G Ventilation Fan Circuit
| | | 05000334/LER-1990-018-01, :on 901211,ESF Actuation - Automatic Start of Standby River Water Pump Occurred During Performance of Surveillance Test.Caused by Operator Error.Pump Shut Down & Operator Counseled |
- on 901211,ESF Actuation - Automatic Start of Standby River Water Pump Occurred During Performance of Surveillance Test.Caused by Operator Error.Pump Shut Down & Operator Counseled
| | | 05000334/LER-1990-019-01, :on 901226,MSIV Closed During Partial Stroke Testing,Isolating Steam from SG B.Caused by tar-like Matl Accumulation on Valve Test Limit Switch.Switch Replaced & Design Changed to Modify MSIV Test Circuit |
- on 901226,MSIV Closed During Partial Stroke Testing,Isolating Steam from SG B.Caused by tar-like Matl Accumulation on Valve Test Limit Switch.Switch Replaced & Design Changed to Modify MSIV Test Circuit
| | | 05000412/LER-1990-019, :on 901105,fault Occurred on 138-kV Bus,Causing Loss of Power to Train a Normal & Emergency 4 Kv Buses. Caused by Adverse Weather Conditions.Air Bottles Isolated & Signal Reset |
- on 901105,fault Occurred on 138-kV Bus,Causing Loss of Power to Train a Normal & Emergency 4 Kv Buses. Caused by Adverse Weather Conditions.Air Bottles Isolated & Signal Reset
| | | 05000412/LER-1990-020, :on 901112,inadvertent Reactor Trip Occurred During RTD Verification Test |
- on 901112,inadvertent Reactor Trip Occurred During RTD Verification Test
| | | 05000334/LER-1990-020-01, :on 901217,review of Plant Logs Determined That Memory Allocation Error Occurred in Computer Operation. Caused by Dynamic Memory Allocation Problem.Plant Parameters Remained within Required Thermal Limits |
- on 901217,review of Plant Logs Determined That Memory Allocation Error Occurred in Computer Operation. Caused by Dynamic Memory Allocation Problem.Plant Parameters Remained within Required Thermal Limits
| | | 05000412/LER-1990-021, :on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves Reopened |
- on 901113,ESF Actuation & Feedwater Isolation Occurred During MSIV Stroke Testing.Caused by Operator Error.Feedwater Isolation Signal Reset & Isolation Valves Reopened
| | | 05000412/LER-1990-022, :on 901019,discovered Inadequate Electrical Isolation Between Control & Protection Circuits |
- on 901019,discovered Inadequate Electrical Isolation Between Control & Protection Circuits
| | | 05000412/LER-1990-023, :on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal Reset |
- on 901114,ESF Actuation & Feedwater Isolation Occurred in Response to Opening Condenser Steam Dump Valve. Caused by Operation of Steam Dump Sys in Steam Pressure Control Mode.Signal Reset
| | | 05000412/LER-1990-024, :on 901112,discovered That Boric Acid Storage Tank Sample Exceeded 7-day Surveillance Required by Ts. Caused by Abnormal Evolution.Personnel Counseled |
- on 901112,discovered That Boric Acid Storage Tank Sample Exceeded 7-day Surveillance Required by Ts. Caused by Abnormal Evolution.Personnel Counseled
| | | 05000412/LER-1990-025, :on 901201,intake Structure Instrument Air Compressor Failed to Automatically Start on Low Air Pressure During Power Operation.Caused by Failed Pressure Switch.New Pressure Switch Calibr & Installed |
- on 901201,intake Structure Instrument Air Compressor Failed to Automatically Start on Low Air Pressure During Power Operation.Caused by Failed Pressure Switch.New Pressure Switch Calibr & Installed
| | | 05000412/LER-1990-026, :on 901202,loss of Flow Alarm Received on Containment Airborne Radiation Monitor Skid.Monitor Inlet Isolation Valve Found Shut Due to Isolation Valve Limit Switch Being Out of Adjustment |
- on 901202,loss of Flow Alarm Received on Containment Airborne Radiation Monitor Skid.Monitor Inlet Isolation Valve Found Shut Due to Isolation Valve Limit Switch Being Out of Adjustment
| |
|