05000374/FIN-2018003-07
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Finding | |
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Title | Potential Failure to Promptly Correct the Unit 2 Primary Containment Wall Cavity Leakage Condition and to Follow Corrective Action Program Process |
Description | Condition description in AR 2420888 indicated that leakage through the Unit 2 primary containment wall has been a longstanding open issue. The leak was initially identified in 1998 when water leakage was noticed on the external side of the primary containment wall. The leakage was approximately 2025 drops per minute at the primary location and multiple areas near the 180 degree azimuth at construction joints on elevations 813 and 795. Another minor leak was noticed at a similar location near the 0 degrees azimuth. The condition was documented in AR 2269. The source of water leakage was determined to be a weld on a 2 fuel pool cooling drain line and work order 98109950 was initiated to repair the weld. The work was not scheduled and the work order was eventually cancelled. In 2010, the leakage was documented again in AR 1086083. A technical evaluation documented as ATI14709531847 in 2014 concluded that there was no adverse impact on structural adequacy of the containment. The technical evaluation stated that the leakage was to be repaired in the upcoming outage through work order 855785. Action request 2420888 was written in December 2014 to re-enter the condition in the CAP. It recommended corrective actions for liner ultrasound testing every other refueling outage, completion of weld repair, and performance of a technical evaluation for structural impact on the concrete, reinforcing steel, tendons, and liner. The technical evaluation assignment was closed to the evaluation documented under ATI14709531847 discussed above. The corrective action assignment for the weld repair was closed to a work order which has not been completed to-date. Based on the inspectors review, the licensee has deferred the actions to correct this condition identified in 1998. The inspectors question whether the continuous leakage could lead to deterioration of the concrete, corrosion of the reinforcement, or degradation of post tensioned tendons if it enters the tendon sheath or trumpet area; and therefore a condition adverse to quality. This unresolved item remains open pending additional inspector review of the issue with respect to regulatory requirements. Planned Closure Action: Inspectors will seek additional information from the licensee and the NRC will perform internal reviews to evaluate compliance with NRC regulations |
Site: | LaSalle |
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Report | IR 05000374/2018003 Section 4OA2 |
Date counted | Sep 30, 2018 (2018Q3) |
Type: | URI: |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | W Schuap J Havertape R Ng J Cassidy G Edwards V Petrella L Rodriguez B Dickson |
INPO aspect | |
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Finding - LaSalle - IR 05000374/2018003 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (LaSalle) @ 2018Q3
Self-Identified List (LaSalle)
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