08-11-2010 | Event Description: On June'10, 2010, Unit 1 Shutdown Bank "B" Rod N7 dropped fully into the core. 2010,On June 12, Unit 1 Shutdown Bank "B" Rod J13 dropped fully into the core while Rod N7 was still dropped. As directed by procedures, Operators initiated a Unit 1 Reactor trip by manually actuating the Reactor Protection System. Subsequent to tripping Unit 1, the lA and 1B Motor Driven Auxiliary Feedwater Pumps were manually actuated to maintain Steam Generator levels.
Event Cause: A regulation card in a Rod Control System Power Cabinet experienced an intermittent connection due to a degraded solder joint.
This intermittent connection caused a drop in the current supply to the Control Rod Drive Mechanisms for Unit 1 Shutdown Bank "B" Rod N7 (CDRMs) and Unit 1 Shutdown Bank "B" Rod J13. Current dropped to levels which allowed the CRDM grippers to drop Rods N7 and J13 into the core.
Corrective Actions: The degraded Rod Control System Power Cabinet regulation card'was replaced. Additional preventative maintenance strategies will be evaluated for identifying degraded solder joints on cards in the Rod Control System Power Cabinets. Replacement of selected cards in the Rod Control System Power Cabinets with. an upgraded card will be evaluated. . |
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LER-2010-003, Dropped Control Rods Resulting in Completion of a Technical Specification Required Shutdown and Actuation of the Reactor Protection System and Auxiliary Feedwater System.Docket Number |
Event date: |
06-12-2010 |
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Report date: |
08-11-2010 |
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3692010003R00 - NRC Website |
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BACKGROUND
The following information is provided to assist.. readers in understanding the event described in this LER. Applicable Energy Industry Identification [EIIS] system and component codes are enclosed within brackets. McGuire Nuclear Station unique system and component identifiers are contained within parentheses.
Rod Control System [JD](IRE):
The IRE System provides for Reactor power modulation by manual or automatic control of full length control rod banks in a pre-selected sequence and for manual operation of individual banks. Each Unit has four Control Banks and five Shutdown Banks and each of these Banks are divided into Groups. For each Group, Group Step Counters indicate the demand position of a Group in "steps". The system provides a means to trip the Reactor and place it in a shutdown MODE by inserting a large amount of negative reactivity.
The IRE System takes input from the Reactor Control System (while in automatic) or the Reactor Operator (while in manual) to position the full length control rods to the desired position in the core. The major components necessary to convert an input signal to actual rod motion are: the Logic Cabinet, the Power Cabinets, and the CRDMs. The Logic Cabinet generates signals for speed and direction based on input information from the Reactor Control System or the Reactor Operator.
The five Power Cabinets receive signals from the Logic Cabinet and utilize regulation cards [JC], phase control cards [JC], and firing cards [JC] to generate the appropriate currents to the CRDMs for holding or moving the rods served by their respective Power Cabinet. Opening the Reactor Trip Breakers will disrupt power to the Power Cabinets and the CRDMs, allowing the rods to fall into the core.
Technical Specification (TS) 3.1.4 - "Rod Group Alignment Limits" specifies that all Shutdown Bank rods and Control Bank rods shall be operable in MODES 1 and 2, with all individual indicated rod positions within 12 steps of their Group Step Counter demand position. TS 3.1.4 Condition B provides the Required Actions and associated Completion Times when one rod is not within the above alignment. None of the Required Actions of Condition B require the affected Unit be shutdown.
With more than one rod not within the above alignment limit, TS 3.1.4, Condition D, Required Action D.2 requires the affected Unit be in MODE 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and plant procedures direct Operators to manually trip the Reactor.
Reactor Protection System [JC](I,RE):
The IPE System automatically keeps the Reactor operating within a safe region by shutting down the Reactor whenever the limits of the region are approached. Whenever a direct process or calculated variable monitored by the IPE System exceeds a set point, the IPE System automatically actuates to initiate a Reactor trip in order to protect against either gross damage to fuel cladding or loss of system integrity which_ could lead to release of radioactive fission products into the Containment. Using either of two Control Board switches, Reactor Operators may elect to manually actuate the IPE System to open the Reactor Trip Breakers and initiate a Reactor trip.
Auxiliary Feedwater System [BA](CA):
The CA System provides an emergency feedwater supply to the Steam Generators [SG](SG) if the respective Unit's Condensate and Feedwater System [SJ](CF) is not available to maintain SG water inventory. This ensures the capability to transfer fission product decay heat and other residual heat loads from the Reactor Coolant System [AB](NC) during both normal operation and accident conditions. Each Unit's CA system contains an "A" and "B" Train Motor Driven Pump [P] (MDCAP) and a "C" Train Turbine Driven Pump [N(TDCAP). These pumps will automatically actuate upon receipt of a signal satisfying the logic for automatic start of the respective pump or each pump can be manually actuated from the Control Room.
EVENT DESCRIPTION
On June 10, 2010, Unit 1 was at 100% power with all Shutdown Bank rods and Control Bank rods operable and within the alignment limit specified in TS 3.1.4. At approximately 15:54 hours, Unit 1 Shutdown Bank "B" Rod N7 dropped fully into the Reactor core which represented a condition where this rod was not within the alignment limit of TS 3.1.4. Subsequent to the dropped Rod N7, the Required Actions of TS 3.1.4 Condition B were implemented within the Required Action times and Operations began a load reduction on Unit 1 as directed by procedure AP/1/A/5500/14 - "Rod Control Malfunction".
On June 12, 2010 at approximately 06:44 hours, Unit 1 Shutdown Bank "B" Rod J13 dropped fully into the Reactor core. At the time Rod J13 dropped, the Shutdown Bank "B" Rod N7 was in progress, with Rod N7 still dropped into the Reactor core. With two rods dropped into the Reactor core, this represented a condition where more than one rod was not within the alignment limit of TS be placed in MODE 3 within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />. As directed by procedure AP/1/A/5500/14, Operators initiated a Unit 1 Reactor trip at approximately 06:44 hours by manually actuating the IPE System. Upon trip of the Reactor, Unit 1 entered MODE 3 which represents a shutdown condition.
As expected, following the Unit 1 Reactor trip, the "1A" CF Pump went to rollback hold and SG levels dropped. At approximately 06:48 hours, the 1A and 1B MDCA Pumps were manually actuated in response to decreasing SG levels. These pumps operated as designed to maintain Unit 1 SG inventories.
Manual actuation of the IPE and CA Systems is reportable pursuant to the requirements of 10 CFR 50.73 (a)(2)(iv)(A) - "System Actuation". As per 10 CFR 50:73 (a)(2)(i)(A), The Unit 1 Reactor trip is being reported as a completion of a shutdown required by plant Technical Specifications.
CAUSAL FACTORS
Trouble shooting and testing determined that a solder joint on a regulation card in the 1BD IRE System Power Cabinet experienced an intermittent connection. On June 10, 2010 and June 12, 2010, this intermittent connection caused a drop in the current supply to the CRDMs Shutdown Bank "B" Rod N7 and Rod J13. These current drops were not of sufficient duration to initiate any rod control alarms. On June 10, 2010, current dropped to a level which allowed the CRDM gripper for Shutdown Bank "B" Rod N7 to drop this rod into the core. Similarly, on June 12, 2010, current dropped to a level which allowed the CRDM gripper for Shutdown Bank "B" Rod J13 to drop this rod into the core. On both June 10, 2010 and June 12, 2010, the currents to the CRDMs for all other rods served by the 1BD IRE System Power Cabinet were maintained at values sufficient to hold these rods.
The intermittent connection on the regulation card in the 1BD IRE System Power Cabinet is attributed to a degraded solder joint. The most probable cause of the degraded solder joint is cracking due to vibration experienced during normal plant operation. Further cause investigation associated with this event is in progress. If the results of this ensuing evaluation identify any information that might materially affect the understanding of this event, the cause, or the corrective actions, Duke Energy will submit a supplement to this LER.
Note, periodic preventative maintenance (PM) is performed on the cards in the IRE System Power Cabinets to identify and repair as needed any degraded solder joints. In 2008, during the last performance of this PM on the 1BD Power Cabinet, no' solder joint degradation was identified on the regulation card that experienced the degraded solder joint. Also, McGuire Nuclear Station has not experienced any previous occurrences of similar rod events caused by degraded solder joints on cards in the IRE System Power Cabinets.
CORRECTIVE ACTIONS
Immediate:
1. Initial investigation identified that the dropped N7 and J13 rods could possibly be attributed to a degraded 1BD IRE System Power Cabinet regulation card, phase control card, or firing card associated with the rods. All three cards were replaced and quarantined.
2. The quarantined 1BD IRE System Power Cabinet regulation card, phase control card, and firing card were tested onsite. No issues were identified.
Subsequent:
1. The quarantined 1BD IRE System Power Cabinet regulation card, phase control card, and firing card were sent to the vendor for failure analysis and testing, which identified the items discussed in the Causal Factors section of this LER.
Planned:
1. Additional PM strategies will be evaluated for identifying degraded solder joints on cards in the IRE System Power Cabinets.
2. Evaluate replacement of selected cards in the IRE System Power Cabinets with an upgraded card.
SAFETY ANALYSIS
Duke Energy used 'a risk-informed approach to determine the risk significance associated with the Unit 1 Reactor trip experienced on June 12, 2010.
The Conditional Core Damage Probability (CCDP) and the Conditional Large Early Release Probability (CLERP) of this event were evaluated by considering the following:
- Actual plant configuration, equipment unavailability, and maintenance activities at the time of the Unit 1 Reactor trip.
The CCDP associated with this event was determined to be less than 1.0E 06. The CLERP associated with this event was determined to be less than 1.0E-7.
This event is considered to be of no significance to the health and safety of the public.
ADDITIONAL INFORMATION
To determine if ,a recurring or similar event exists, a search of the McGuire Problem Investigation Process (PIP) database was conducted for a time period covering 5 years prior to the date of this event. Based on Duke's definition of a recurring event, similar significant event with the same cause code, no recurring events were identified.
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05000220/LER-2010-001 | Reactor Scram Due to Inadequate Post Maintenance Testing | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000410/LER-2010-001 | Reactor Scram Due to Inadvertent Actuation of the Redundant Reactivity Control System During Maintenance | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000395/LER-2010-001 | Reactor Building Cooling Units Reduced Air Flow Rate Below Technical Specification Limits | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000382/LER-2010-001 | Spent Fuel Pool Cooling Single Failure | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000374/LER-2010-001 | High Pressure Core Spray System Declared Inoperable Due to Failed Room Ventilation Control Relay | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000373/LER-2010-001 | Unauthorized Individual Gained Access to the Protected Area. | | 05000370/LER-2010-001 | Loose connection in a panel board serving a Solid State Protection System Train concurrent with redundant train maintenance could have prevented fulfillment of a safety function. | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000261/LER-2010-001 | Emergency Diesel Generator Inoperable in Excess of Technical Specifications Allowed Completion Time | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000263/LER-2010-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000255/LER-2010-001 | Potential Loss of Safety Function Due to a Service Water Pump Shaft Coupling Failure | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2010-001 | Engineered Safety Features Steam Line Pressure Dynamics Modules Discovered Outside of Technical Specification Values | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2010-001 | Unit 2 Turbine Trip during Reactor Shutdown Resulting in a Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000305/LER-2010-001 | Safety Injection Pump Recirculation Line Isolation Results in Violation of Technical Specifications | | 05000298/LER-2010-001 | Cooper Nuclear Station 05000298 1 of 4 | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2010-001 | Standby Shutdown Facility Letdown Line Orifice Strainer Blocked by Valve Gasket Material | 10 CFR 50.73(a)(2)(i)(b) | 05000282/LER-2010-001 | Unanalyzed Condition Due to Postulated High Energy Line Break On Cooling Water System | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000277/LER-2010-001 | Multiple Slow Control Rods Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i) | 05000361/LER-2010-001 | Broken Manual Valve Prevents Timely Condensate Storage Tank Isolation | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000483/LER-2010-001 | Emergency Core Cooling System MODE 4 Operating Practices Prohibited by current Technical Specification 3.5.3 | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000498/LER-2010-001 | Unit Shutdown Required by Technical Specifications | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000316/LER-2010-001 | Valid Actuation of Auxiliary Feedwater System in Response to Valid Steam Generator Low-Low Levels | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000321/LER-2010-001 | Corrosion Induced Bonding Results in Safety Relief Valve Lift Setpoint Drift | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000336/LER-2010-001 | Millstone Power Station Unit 2 Reactor Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000413/LER-2010-001 | Technical Specification Violation Associated with Failure to Perform Offsite Circuit Verification | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000440/LER-2010-001 | Invalid Isolation Signal Results in Shutdown Cooling Interruption | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | 05000424/LER-2010-001 | Breaker Failure Results in I B Train Containment Cooling System Being Declared Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000416/LER-2010-001 | Automatic Reactor Scram On Decreasing Reactor Water Level Due To Inadvertent Reactor Feed Pump Trip | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000249/LER-2010-001 | OPRM Power Supply Failure during Maintenance Results in Unit 3 Automatic Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000251/LER-2010-001 | Two Shutdown Bank Rods Were Dropped from Fully Withdrawn Position | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(iv), System Actuation | 05000261/LER-2010-002 | Plant Trip due to Electrical Fault | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000255/LER-2010-002 | Condition that Could Have Prevented the Fulfillment of a Safety Function | 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000335/LER-2010-002 | Opened ECCS Boundary Door in Violation of Identified Compensatory Measures | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000334/LER-2010-002 | 270 Degree Circumferential Flaw Found on Residual Heat Removal System Drain Valve Socket Weld | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000316/LER-2010-002 | Containment Divider Barrier Seal Mounting Bolts Not Properly Installed | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000250/LER-2010-002 | Fuel Transfer Pump Failure Renders 3B Emergency Diesel Generator Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000269/LER-2010-002 | Manual Reactor Trip due to 1A1 and 1A2 Reactor Coolant PumDHigh Vibration Indication | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000315/LER-2010-002 | Manual Auxiliary Feedwater Actuation in Response to Main Feedpump Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000271/LER-2010-002 | Inoperability of Main Steam Safety Relief Valves due to Degraded Thread Seals | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000277/LER-2010-002 | Improperly Fastened Rod Hanger Results in Inoperable Subsystem of Emergency Service Water | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000413/LER-2010-002 | Discovery of Reactor Coolant System Pressure Boundary Leak at Thermowell 1NCTW5850 Seal Weld. | | 05000282/LER-2010-002 | Postulated Flooding of Unit 1 Fuel Oil Transfer Pump Motor Starters Could Have Resulted In Reduced Fuel Oil Inventory | | 05000414/LER-2010-002 | Duke Energy Corporation Catawba Nuclear Station 4800 Concord Road York, SC 29745 803-701-4251 803-701-3221 fax December 15, 2010 U.S. Nuclear Regulatory Commission
Attention: Document Control Desk
Washington, D.C. 20555
Subject:�Duke Energy Carolinas, LLC (Duke Energy)
Catawba Nuclear Station, Unit 2
Docket No. 50-414
Licensee Event Report 414/2010-002
Pursuant to 10 CFR 50.73(a)(1) and (d), attached is Licensee Event Report 414/2010-002, Revision 0 entitled, "Technical Specification Violation Involving Mode Change with Inoperable Auxiliary Feedwater System Train Due to Closed Pump Discharge Valves". This report is being submitted in accordance with 10 CFR 50.73(a)(2)(i)(B). There are no regulatory commitments contained in this letter or its attachment. This event is considered to be of no significance with respect to the health and safety of the public. If there are any questions on this report, please contact L.J. Rudy at (803) 701-3084. Sincerely, faius4- A James R. Morris LJR/s Attachment www.duke-energy.corn (14 Document Control Desk Page 2 December 15, 2010 xc (with attachment): L.A. Reyes Regional Administrator U.S. Nuclear Regulatory Commission - Region II Marquis One Tower 245 Peachtree Center Ave., NE Suite 1200 Atlanta, GA 30303-1257 J.H. Thompson (addressee only) NRC Project Manager U.S. Nuclear Regulatory Commission Mail Stop 8-G9A 11555 Rockville Pike Rockville, MD 20852-2738 G.A. Hutto, Ill NRC Senior Resident Inspector Catawba Nuclear Station INPO Records Center 700 Galleria Place Atlanta, GA 30339-5957 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: 80 hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send commentsLICENSEE EVENT REPORT (LER) regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by Internet e-mail to infocollectssesource@nre.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used(See reverse for required number of to impose an information collection does not display a currently valid OMB control number, the NRCdigits/characters for each block) may not conduct or sponsor, and a person is not required to respond to, the info(mation collection. 1.. FACILITY NAME 2. DOCKET NUMBER I3. PAGE Catawba Nuclear Station, Unit 2 05000414 1 OF 7 4. TITLE Technical Specification Violation Involving Mode Change with Inoperable Auxiliary Feedwater System Train Due to Closed Pump Discharge ValvesD • | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2010-002 | Unit 2 Turbine Shutdown Due To the Loss of a Main Feed Water Pump That Resulted in a Reactor Scram | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000440/LER-2010-002 | Piping Leak Results in Condition Prohibited by Technical Specifications | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000382/LER-2010-002 | Main Feedwater Isolation Valve B exceeded allowed outage time due to tubing connection failure | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000370/LER-2010-002 | ref Energy® REGIS T. REPKO Vice President McGuire Nuclear Station Duke Energy MGO1VP / 12700 Hagers Ferry Rd. Huntersville, NC 28078 980-875-4111 980-875-4809 fax regis.repko(Codu ke-energy.corn 10 CFR 50.73 May 10, 2011 U.S. Nuclear Regulatory Commission ATTENTION: Document Control Desk Washington, D.C. 20555 Subject: D Duke Energy Carolinas, LLC McGuire Nuclear Station, Unit 2 Docket Nos. 50-370 Licensee Event Report (LER) 370/2010-02, Supplement 1 Problem Investigation Process (PIP) M-10-05982 Pursuant to 10 CFR 50.73 Sections (a) (1) and (d), attached is Supplement 1 to Licensee Event Report 370/2010-02, regarding past inoperability of the Unit 2 "A" Train Nuclear Service Water System and satisfies the commitment to supplement the LER following completion of the root cause analysis This supplement to LER 370/2010-02 supersedes the LER previously submitted December 20, 2010. Completion of the root cause analysis has not affected the original reporting criteria which was completed in accordance with 10 CFR 50.73 (a) (2) (i) (B), an Operation Prohibited by Technical Specifications, and 10 CFR 50.73 (a) (2) (v) (B), any Event or Condition That Could Have Prevented Fulfillment of the Safety Function needed to remove residual heat. Additionally, the supplement did not affect the significance of the event which was considered to be of no significance with respect to the health and safety of the public. There are no regulatory commitments contained in this report. If questions arise regarding this LER, contact Rick Abbott at 980-875-4685. Very truly yours, Zi1:77 Regis T. Repko Attachment www. duke-energy. corn U.S. Nuclear Regulatory Commission May 10, 2011 Page 2 cc:�V. M. McCree, Regional Administrator U.S. Nuclear Regulatory Commission, Region II
Marquis One Tower
245 Peachtree Center Ave., NC, Suite 1200
Atlanta, Georgia 30303-1257
Jon H. Thompson (Addressee Only)
Senior Project Manager (McGuire)
U.S. Nuclear Regulatory Commission
11555 Rockville Pike
Rockville, MD 20852-2738
J. B. Brady
Senior Resident Inspector
U.S. Nuclear Regulatory Commission
McGuire Nuclear Station
W. L. Cox Ill, Section Chief North Carolina Department of Environment and Natural Resources Division of Environmental Health Radiation Protection Section 1645 Mail Service Center Raleigh, NC 27699-1645 NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB. NO 3150-0104 EXPIRES: 08/31/2013 (10-2010) Estimated burden per response to comply with this mandatory collection request: SO hours. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear Regulatory Commission. Washington, DC 20555-0001, or by Internet e-mail to info (See reverse for required number of collects resmirceOnrc.gov, and to the Desk Officer, Office of Information and Regulatory digits/characters for each block) Affairs, NEOB-10202, (3150-01041, Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection. LICENSEE EVENT REPORT (LER) 1. FACILITY NAME 2. DOCKET NUMBER 3. PAGE McGuire Nuclear Station,2Unit 2 05000-212
0370 OF-7 4. TITLE Unit 2 Nuclear Service Water System "A" Train Past Inoperable due to
Failed Strainer Differential Pressure Instrument. | 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2010-002 | | | 05000456/LER-2010-002 | Limiting Condition for Operation Action Not Completed Within the Required Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000249/LER-2010-003 | Steam Leak Results in HPCI Inoperability | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000251/LER-2010-003 | Damaged Speed Sensor Caused the 4A Emergency Diesel Generator to be Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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