05000368/FIN-2017002-02
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Finding | |
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| Title | Failure to Install Set Screw Leads to Breaker Failure |
| Description | Green . The inspectors documented a Green self -revealing finding and associated non- cited violation of Unit 2 Technical Specification 6.4.1.a, for failure to properly pre-plan and perform maintenance on the Unit 2 containment spray pump B breaker in accordance with written procedures. Specifically, the licensee failed to install a cam shaft set screw during the breakers last overhaul. The cam eventually became displaced on the shaft, and the breaker failed to close. To correct the issue, the licensee replaced the breaker and installed a cam shaft set screw in the failed breaker. The licensee also inspected all other similar breakers to verify the cams were properly secured. The licensee entered the issue in to their corrective action program as Condition Report CR -ANO -2-2017- 03168. The failure to install a cam shaft set screw during the overhaul of the Unit 2 containment spray pump B breaker is a performance deficiency. The performance deficiency is more than minor because it was associated with the equipment performance attribute of the mitigating systems cornerstone and adversely affected the cornerstone objective to ensure the reliability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the performance deficiency resulted in the failure of a Unit 2 containment spray pump breaker. Using Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At -Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, the issue screened as having very low safety significance (Green) because it was not a design or qualification deficiency; did not represent a loss of system; did not result in the actual loss of function of a train of technical specification equipment for greater than its allowed outage time; and did not screen as potentially risk significant due to seismic, flooding, or severe weather events. The inspectors determined this finding did not have a cross -cutting aspect because the most significant contributor did not reflect current licensee performance. Specifically, the error occurred during the breakers last overhaul, which occurred in 2011 |
| Site: | Arkansas Nuclear |
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| Report | IR 05000368/2017002 Section 1R15 |
| Date counted | Jun 30, 2017 (2017Q2) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | Self-revealing |
| Inspection Procedure: | IP 71111.15 |
| Inspectors (proximate) | B Tindell T Sullivan M Tobin J Choate J Drake N Greene M Phalen N O'Keefe |
| Violation of: | Technical Specification - Procedures |
| INPO aspect | |
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Finding - Arkansas Nuclear - IR 05000368/2017002 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2017Q2
Self-Identified List (Arkansas Nuclear)
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