05000313/FIN-2017001-03
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Finding | |
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Title | Inadvertent Reactivity Addition |
Description | Green. Inspectors documented a Green self-revealing finding and associated non-cited violation of Unit 1 Technical Specification 5.4.1.a. Specifically, the licensee failed to properly pre-plan and perform maintenance of the integrated control system equipment that can affect the performance of safety-related equipment. The licensee failed to plan and perform post-maintenance testing on newly installed integrated control system cards before returning the system to service. As a result, the licensee failed to detect a failed card. When the associated controller was placed into automatic mode, the system responded to a false demand signal that resulted in an inadvertent rod withdrawal that required prompt operator action to terminate the power increase and restore power to the original level. To correct the failed card, the licensee installed a new card that had been tested and validated prior to installation. The licensee documented this issue in Condition Report CR-ANO-1-2016-05551. Inspectors concluded that the failure to perform a post-maintenance test prior to placing a component in service is a performance deficiency. Specifically, the work order for replacing the steam generator reactor demand circuit card did not include a verification that the system was functioning properly after the replacement card was installed in the plant. The performance deficiency is more than minor because if left uncorrected, the performance deficiency has the potential to become a more significant safety concern. Specifically, if the operator had not taken prompt action to mitigate the event, it could have resulted in a more significant plant transient and could have challenged plant equipment. In accordance with Inspection Manual Chapter 0609, Attachment 4, Initial Characterization of Findings, issued October 7, 2016, and Exhibit 1 of IMC 00609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, Issued June 19, 2012, the inspectors determined the finding to be of very low safety significance (Green) because the finding is associated with the initiating events cornerstone and did not cause a reactor trip. The finding was determined to have a cross-cutting aspect in the area of human performance associated with Work Management, because the licensee did not ensure that they followed a process of planning, controlling, and executing the work activities in a formalized manner, allowing the work order to not have complete instructions for a post-maintenance test. [H.5] |
Site: | Arkansas Nuclear |
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Report | IR 05000313/2017001 Section 4OA2 |
Date counted | Mar 31, 2017 (2017Q1) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71152 |
Inspectors (proximate) | B Correll B Tindell E Uribe J Choate M Kirk M Tobin N O'Keefe |
Violation of: | Technical Specification |
CCA | H.5, Work Management |
INPO aspect | WP.1 |
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Finding - Arkansas Nuclear - IR 05000313/2017001 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2017Q1
Self-Identified List (Arkansas Nuclear)
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