05000354/FIN-2018003-04
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Finding | |
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Title | Enforcement Action (EA)-18-044: EGM on Dispositioning BWR Licensee Noncompliance With TS Containment Requirements During Operations With A Potential For Draining The Reactor Vessel (EGM-11-003) |
Description | From April 19 through April 29, 2018, HCGS performed OPDRVs without establishing secondary containment integrity. An OPDRV is an activity that could result in the draining or siphoning of the reactor pressure vessel water level below the top of fuel, without crediting the use of mitigating measures to terminate the uncovering of fuel. TS 3.6.5.1, Secondary Containment Integrity, requires that secondary containment integrity be maintained, and is applicable during OPDRVs. The required action for this specification without secondary containment integrity in this condition of applicability is to suspend OPDRVs. As reported in LER 05000354/2018-001, HCGS conducted the following OPDRVs during the period of secondary containment inoperability: Control rod drive mechanism replacements; Local power range monitor replacements; and Cavity let down via Reactor Water Clean Up system. Additionally, an unplanned OPDRV occurred due to RHR system relief valves seat leakage. NRC EGM 11-03, EGM on Dispositioning BWR Licensee Noncompliance With TS Containment Requirements During Operations With A Potential For Draining The Reactor Vessel, Revision 3, provides, in part, for the exercise of enforcement discretion only if the licensee demonstrates that it has met specific criteria during an OPDRV activity. The inspectors assessed that HCGS adequately implemented these criteria. In accordance with EGM 11-003, in order to continue to receive enforcement discretion, a license amendment request (LAR) must be submitted and accepted for review within 12 months of the NRC staffs publication of the generic change that occurred on December 20, 2016. The inspectors verified that PSEG submitted the required LAR on September 20, 2017 (ADAMS Accession No. ML17265A847), and that it was subsequently accepted by the NRC for review by a letter dated October 25, 2017 (ADAMS Accession No. ML17299A009). Corrective Action: PSEG submitted an LAR to adopt TS Task Force Traveler 542, Reactor Pressure Vessel Water Inventory Control, on September 20, 2017, that was subsequently accepted by the NRC for review on October 25, 2017. (After the end of the inspection period, on October 30, 2018, the NRC staff responded (ML18260A203) to PSEGs LAR dated September 20, 2017, and issued License Amendment No. 213 that revised the technical specifications to adopt TSTF-542, Revision 2. Corrective Action Reference: 20792923
15 Enforcement: Violation: TS 3.6.5.1, Secondary Containment Integrity, requires that secondary containment integrity be maintained, and is applicable during OPDRVs. The required action for this specification without secondary containment integrity in this condition of applicability is to suspend OPDRVs. Contrary to the above, from April 19 through April 29, 2018, HCGS performed OPDRVs without secondary containment integrity. Therefore, set and maintain secondary containment integrity during OPDRVs without suspending the operation was considered a condition prohibited by TSs as defined by 10 CFR 50.73(a)(2)(i)(B). Basis for Discretion: The NRC is exercising enforcement discretion in accordance with Section 3.5, Violations Involving Special Circumstances, of the NRC Enforcement Policy because all criteria described in EGM 11-003 were met and enforcement discretion was previously authorized by EA-2017-071; therefore, no enforcement action will be issued for this violation. The disposition of this violation closes LER 05000354/2018-001-00. |
Site: | Hope Creek |
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Report | IR 05000354/2018003 Section 4OA3 |
Date counted | Sep 30, 2018 (2018Q3) |
Type: | Violation: Severity level Enforcement Discretion |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71153 |
Inspectors (proximate) | J Hawkins S Haney J Furia F Bower |
Violation of: | 10 CFR 50.73 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications Technical Specification |
INPO aspect | |
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Finding - Hope Creek - IR 05000354/2018003 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Hope Creek) @ 2018Q3
Self-Identified List (Hope Creek)
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