05000336/LER-1982-002, Forwards LER 82-002/03L.Detailed Event Analysis Encl

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Forwards LER 82-002/03L.Detailed Event Analysis Encl
ML17054D372
Person / Time
Site: Millstone Dominion icon.png
Issue date: 02/01/1982
From: Mroczka E
NORTHEAST UTILITIES
To: Haynes R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17054D373 List:
References
CON-IIT07-773-91, CON-IIT7-773-91 MP-2-5044, NUREG-1455, NUDOCS 8202090080
Download: ML17054D372 (6)


LER-1982-002, Forwards LER 82-002/03L.Detailed Event Analysis Encl
Event date:
Report date:
3361982002R00 - NRC Website

text

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. BOX 270 4)FORD, CONNECTICUT 06101

) 666-6011 p.o IIA (203 1982

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,V>>,1 on, D.C. (30)

ontrol, ment Branch,

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~F",'~'~"'"~~'.)I,"8":.!"'~<"5'-':"""AFebruary 1, Mr. Rona 1 d C. Haynes

',". ",yi.~l::.p';<'j';:-.',."..'".y<~."-',<<;:.-Sf~-'-~,~g-2>> 5044 Regional Administratorl'egio+nipgjjj!~>><>>a>j~p<%j'~<~psi,.";;:i Office of Inspection" and:Enforcement-.",4z<<'~+-',~~.,+YP+>'<<

D.S. Nuclear Regulatory C'omn$s'sioiig:j'j~ihpz'j4",,;:"

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Reference:

facility Operating~kPiceqs'eNoeIDp>>R';65 Docket No 50.,",336.j<$j<

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Director, Office of Inspection.landt,,Enforicement, Washingt Director, Office of Management)information>and Program C

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> ",I OTHER STATUS h~ l~L4OISCOVEAY:kggv'~ ('>> '>> >'T OF ACTIVITY~ 4< +ih<>>'-;Tom&;-0~ <<fj< hyI Y<< "<3 orscovcnv DEScnrptroN Q32 ra tor observa tion LOCAI<UN Or RF.LEASE Q3G NA ~.. 82020'3100'll 'S2020 i -",",:, PDR ADOGK'I05OQ0336'8 '%'t Q PjtF lgttvryf '~i~' f CPDR NRC uSE ONLY 8 9 10 Nah'lE QF PREPARER 34'p v 3<'tr< <4<<r Steve Stadnic 4~M""".vkT'~4"~L~~2~-'~Fhtf, '; ptroNE ~ <<hh 3 ~ ~ rr Ih,>>h'4. 80 80 80 80 80 I 80 ~ S 0 Vh0 I 4< JJ was being performed ected to the printed card to fail and a gated. The load CR 82 was on con-Due to frequency causing the input 'in panel 8 VA20 ircuit for shutdown Maintenance was om the reactor od of time, i.ess from 84 to 114'F, in performing a issued to test to connecting to Event Descri tion and Pi obab1es'Conse uencesg~"@j~'E~.'p'll","', During refueling operations,~a~preventatgve maintenance, test on static switch VS2.

'A,.i'S'h'orstgc rcu(tved test~leadjwas leone circuit card of the swit'chj;-'This,causedfa compoyejtgon the silicon controlled rectifier,(SCR.N2)gfooObecomegcontinuously on Inverter 62 was transferi ed~togijve~itegrp6~ejbutjbecause S

tinuously the inverter, orutlevts~were~~conn'ectedgfjPaparal 1 el. differences a large current>flowjresujted'pion"'eaclj~'inverted fuses to blow. This resulted<igloss~v'ofmvs(t'alp/nstrument AC which in turn caused contactgcl'osure~P'jpthefoyerprotection c cooling. This caused yal v'gi2-Sl -652'Sstioaclose'~vi~i~vq~p~,",', Health physics was notified:;to':evacuateathe>steavm.',gen'craters. notified to assist in opening<2;Sl 652~>Its:P,-.@~Rip'@,)j;".,, The loss of shutdown cooling pi eventsgdecayjheat;.,jremoval, fr vessel. since shutdown cooling',was(restoredilinaafshort peri SeVen (7) minutea and reaCtar; COOlannt'<tern'peraturmev';inCreaSed there was no significant effectwsonYthgepla'nt.':,,",, ...'fi;,". Cause Descri tion and Corrective" Actions~4@>;A; ~~ ~~'.."4'"< " The cause of this event was,a,eshortI~circuited;test~lead.used preventative maintenance test.'>'@'A>'depmartmental 'memo"'has been technicians to check all 'test."leadslfor."",short~scircui ts prior equipment. sn /vs> + 'fIsh+& iI'i >"-'5,~eh ppcp+~; 5~4' Nj V c 0 )