05000324/FIN-2014005-01
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Finding | |
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Title | Failure to Protect Emergency Diesel Generator 4-Day Fuel Oil Tank Ventilation Piping from Tornado Missi |
Description | The NRC-identified a Green non-cited violation (NCV) of Title 10 of the Code of Federal Regulations (10 CFR) Part 50, Appendix B, Criterion III, Design Control, for the failure to ensure adequate tornado missile protection for the emergency diesel generator (EDG) 4-day fuel oil tank ventilation piping. Specifically, it was determined that the ventilation piping could be sheared with a design basis tornado missile at the 4-day fuel oil tank building roof level and water intrusion into the EDG fuel oil system would occur during a design basis rain event that would prevent the diesel from performing its required safety function. The licensee documented this issue in their corrective action program (CAP) and performed corrective actions to install concrete blocks around the piping. The inspectors determined that the finding was more than minor in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue Screening, dated September 7, 2012, because it is associated with the Mitigating Systems Cornerstone attributes of Protection Against External Factors and Equipment Performance, and adversely affected the cornerstone objective to ensure the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, it was determined that the ventilation piping could be sheared with a design basis tornado missile at the 4-day fuel oil tank building roof level and water intrusion into the EDG fuel oil system would occur during a design basis rain event that would prevent the EDG from performing its required safety function. Using IMC 0609, Appendix A, issued June 19, 2012, The Significance Determination Process (SDP) for Findings At-Power, the inspectors determined the finding screened to a detailed risk evaluation since the EDG1 fuel oil system was assumed to be completely failed due to a tornado, and it would degrade one or more trains of a system that supports a risk significant system or function. The regional Senior Reactor Analyst performed a detailed risk evaluation by using a qualitative screening analysis to determine the significance of the finding. Tornado initiating event frequency was derived from Nation Weather Service data. Because of the low likelihood of a tornado powerful enough to throw an object of sufficient size to damage the piping, the remote chance the thrown object would strike the vent pipe, and because the remaining EDGs would not be impacted in the same way by the tornado, the finding was determined to be Green. The inspectors did not identify a cross-cutting aspect associated with this finding because the finding is an old design issue that has been in place since original plant construction. |
Site: | Brunswick |
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Report | IR 05000324/2014005 Section 1R15 |
Date counted | Dec 31, 2014 (2014Q4) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.15 |
Inspectors (proximate) | A Scarbeary G Hopper G Kolcum M Bates M Catts M Schwieg |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Brunswick - IR 05000324/2014005 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Brunswick) @ 2014Q4
Self-Identified List (Brunswick)
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