05000313/FIN-2017007-01
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Finding | |
|---|---|
| Title | Failure to Promptly Identify and Correct an Inadequate Design Bases Calculation |
| Description | The inspectors identified a Green, non-cited violation of 10 CFR Part 50, Appendix B, Criterion XVI, Corrective Actions, requires, in part, that measures shall be established to assure that conditions adverse to quality, such as failures, malfunctions, deficiencies, deviations, defective material and equipment, and nonconformance are promptly identified and corrected. Specifically, from 1996 until August 10, 2017, the licensee failed to properly resolve the environmental conditions in room 38 following a high-energy line break, even when challenged during a self-assessment by members of the quality assurance group in June 29, 2015. In response to this issue, the licensee determined that in the event of a break in the letdown line, an engineered safety feature signal automatic closure of both the inside and outside reactor building isolation valves occurs in approximately 40 seconds, preventing room 38 from going harsh. This finding was entered into the licensees corrective action program as Condition Report CR-ANO-1-2017-02441. The inspectors determined that the licensees failure to adequately evaluate and take prompt corrective actions to resolve an identified condition adverse to quality related to the high energy line break analysis for room 38 was a performance deficiency. The performance deficiency was more than minor because it was associated with the design control attribute of the Mitigating Systems Cornerstone and affected the associated objective to ensure availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, when the licensee identified that the environmental conditions in room 38 of the auxiliary building were harsh, as determined by Design Bases Calculation CALC-01-EQ-1002-02, they failed to properly resolve the condition adverse to quality. In accordance with Inspection Manual Chapter 0609, Appendix A, The Significance Determination Process (SDP) for Findings At-Power, dated June 19, 2012, Exhibit 2, Mitigating Systems Screening Questions, dated July 1, 2012, the inspectors determined that the finding was of very low safety significance (Green) because the finding (1) was not a deficiency affecting the design and qualification of a mitigating structure, system, or component, and did not result in a loss of operability or functionality; (2) did not represent a loss of system and/or function; (3) did not represent an actual loss of function of at least a single train for longer than its allowed outage time, or two separate safety systems out-of-service for longer than their technical specification allowed outage time; and (4) does not represent an actual loss of function of one or more non-technical specification trains of equipment designated as high safety-significant for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in accordance with the licensees maintenance rule program. The finding has a cross-cutting aspect in the area of human resources, training, because the organization failed to provide training and ensure knowledge transfer to maintain a knowledgeable, technically competent workforce and instill nuclear safety values. Specifically, there was a lack of understanding of the current licensing bases for the plant displayed by engineering, operations, and management [H.9]. |
| Site: | Arkansas Nuclear |
|---|---|
| Report | IR 05000313/2017007 Section 1R21 |
| Date counted | Sep 30, 2017 (2017Q3) |
| Type: | NCV: Green |
| cornerstone | Mitigating Systems |
| Identified by: | NRC identified |
| Inspection Procedure: | IP 71111.21N |
| Inspectors (proximate) | J Drake S Alferink J Braisted T Farnholtz |
| Violation of: | 10 CFR 50 Appendix B 10 CFR 50 Appendix B Criterion XVI Technical Specification |
| CCA | H.9, Training |
| INPO aspect | CL.4 |
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Finding - Arkansas Nuclear - IR 05000313/2017007 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Arkansas Nuclear) @ 2017Q3
Self-Identified List (Arkansas Nuclear)
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