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LER-1981-119, Forwards LER 81-119/03L-0.Detailed Event Analysis Encl |
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Pubhc Service Electric ana Gas Company P.O. Box #168 Hancocks Bridge. New Jersey 08038 i
December 10, 1981 i
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l Mr.
R.
C.
Haynes Director of USNRC cf Office of Inspecticn and Enforcement G
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Region 1
'N/'
631 Park Avenue 8
King of Prussia, Pennsylvan!.d 19406 MEUD
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DEC 2 21981> [
Dear Mr. Haynes:
n 8m.,....,...,
""Tf"".;,'9 LICENSE NO. DPR-75 offx DOCKET NO. 50-311
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7 REPORTABLE OCCURRENCE 81-119/03L
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, T tp Pursuant to the requirements of Salem Generating Station Unit No. 2, Technical Specifications, Section 6.9.1.9.b, we are submitting Licensee Event Report for Reportable Occurrence 81-119/03L.
This report is required within thirty (30) days of the occurrence.
Sincerely yours,
,/l(,N Y&'d H.
J. Midura General Manager -
Salem Operations CC:
Distribution l
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8112230314 811210' PDR ADOCK 05000311 s i S
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The Energy Peop!c
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Report Number:
81-119/03L i
Report Date:
12-10-81 Occurrence Date:
11-11-81, 11-17-81, 11-18~81, and 11-22-81 Facility:
Salem Generating Station, Unit 2 Public Service Electric & Gas Company 3ancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:
Nuclear Instrumentation - Power Range Channel N Inoperable.
This report was initiated by Incident Reports81-457,81-463,81-464, 81-465, and 81-475.
CONDITIONS PRIOR TO OCCURRENCE:
11-11-81 Mode 1 - Rx Power 100% - Unit Load 1150 MWe 11-17-81 Mode 1 - Rx Power 50% - Unit Load 540 MWe 13-17-81 Mode 1 - Rx Power 94% - Unit Load 1100 MWe 11-18-81 Mode 1 - Rx Power 86% - UI.it Load 1000 MWe 11-22-81 Mode 1 - Rx Power 50% - Unit Load 580 MWe l
DESCRIPTION OF OCCURRENCE, APPARENT CAUSE, AND CORRECTIVE ACTION:
l Fro u November 11, 1981 through November 28, 1981 malfunctions in Power Range Channel N-4^ Nuclear Instrumentation caused a series of related incidents.
On November 11, 1SCl, after a Quadrant Power Tilt Ratio (QPTR) calculation, it was determined that the QPTR was 1.03.
Channel N-43 was low by 3%.
At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> Action Statement 3.2.4.a was entered, and, accordingly, reactor power was reduced to 90%.
In order'to correct Channel N-43, the summing amplifier was recalibrated and tested satisfactorily.
The QPTR was recalcu-lated satisfactorily, and at 0825 hours0.00955 days <br />0.229 hours <br />0.00136 weeks <br />3.139125e-4 months <br />, November 12, 1981 Action Statenznt 3.2.4.a was terminated.
On Novenber 17, 1981, after reaching 50% reactor power, following a startup from a tri.p the previous day, the QPTR was again calculated.
Again it was datermined to be 1.03.
At 0230 hours0.00266 days <br />0.0639 hours <br />3.80291e-4 weeks <br />8.7515e-5 months <br /> j
Action Statement 3.2.4.a was entered, and reactor power was held at 50%.
After holding the reactor power constant for one hour, the QPTR was recalculated and found to be within specification at 1.02.
At 0338 hours0.00391 days <br />0.0939 hours <br />5.588624e-4 weeks <br />1.28609e-4 months <br /> Action Statement 3.2.4.a was terminated.
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LER 81-119/03L Later in the day a QPTR Surveillance calculation determined QPTR was cut of specification at 1.03.
At 1250 hours0.0145 days <br />0.347 hours <br />0.00207 weeks <br />4.75625e-4 months <br />,
' November 17, 1981 Action Statement 3.2.4.a was entered.
Flux mapping was performed, and established the QPTR as satisfactory.
Since N-43 was the channel whi.ch caused the QPTR to be out of specificauion, due to full power current drift it was declared inoperable at 1030 hours0.0119 days <br />0.286 hours <br />0.0017 weeks <br />3.91915e-4 months <br />, November 18, 1981,'and Action Statement 3.3.1 Action 2 was entered.
All associated bistables were placed in the tripped condition within one hour.
A QPTR calculation was then performed utilizing the three remaining operable channels.
The results were satisfactory and at 1115 hours0.0129 days <br />0.31 hours <br />0.00184 weeks <br />4.242575e-4 months <br />, November 18, 1981 Action Statement 3.2.4.a was terminated.
A plateau calibration was performed on Channel N-43.
The channel was then recalibrated utilizing new full power currents.
QPTR cali' orations were performed at least once every 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />, as required by Technical Specifications.
At 2230 hours0.0258 days <br />0.619 hours <br />0.00369 weeks <br />8.48515e-4 months <br />, November 18, 1981, Channel N-43 was tested satisfactorily and declared operable, and Action Statement 3.3.1 Action 2 was terminated.
The instrument manufacturer was contacted con 7erning the problems being experienced.
They indicated that another plant with similar instrumentation was experiencing similar problems which had been diagnosed as premature detector aging.
Their recommendation was to change the detector if problems continued to occur.
At 2320 hours0.0269 days <br />0.644 hours <br />0.00384 weeks <br />8.8276e-4 months <br />, November 22, 1981, Power Range Channel N-43 was declared inoperable due to current drift, indicating detector degradation, and Action Statement 3.3.1 Action 2 was entered.
The associated bistables were placed in the tripped condition as required by Technical Specifications.
All requirements of Technical Specification 3.3.1 Action 2 were met.
On November 24, 1981 the reactor tripped.
While the unit was shutdown, according to the manufacturerb recommendation, the upper and lower detectors of Channel N-43 were replaced and recalibrated.
The channel was tested satisfactorily and declared operable.
At 0327 hours0.00378 days <br />0.0908 hours <br />5.406746e-4 weeks <br />1.244235e-4 months <br />, November 28, 1981 Acticn Statement 3.3.1 Action 2 was terminated.
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LER 81-119/03L -
ANALYSIS OF OCCURRENCE:
Technical Specification 3.2.4.a requires:
With the Quadrant-Power Tilt Ratio (QPTR) determined to exceed 1.02 but-less than or equal to 1.09, calculate the QPTR'at least once per hour until either the QPTR is re-duced to within its limit, or thermal power is reduced to less than 50% of rated thermal power.
Within 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> either reduce the QPTR to within its limit, or reduce thermal power at least 3% from rated thermal power for each 1% of indicated QPTR in-excess of 1.0.
Technical Specification 3.3.1 Acon 2 requires:
With the number of operable channels one less than the total number of channels, atartup and/or power operation may proceed provided the following conditions are satisfied:
a) the operable channel is placed in the tripped condition within one hour; d) the Quadrant Power Tilt Ratio is verified at least once per 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> when thermal power is greater than 75% of rated thermal power.
FAILURC DATA:
Westinghouse Electric Corporation Power Range Detector i
Prepared By F.
Dickey
, kl[' c wd Gen (ral Manager -
Salem Operations SORC Meeting No.81-125 4
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| 05000311/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001, Forwards LER 81-001/03L-0 | Forwards LER 81-001/03L-0 | | | 05000272/LER-1981-001-03, /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | /03L-0:on 810105,axial Flux Difference in Two Channels Drifted Out of Required Band.Caused by Operator Error.Reactor Power Level Reduced & Axial Flux Differences Returned to Values within Required Range | | | 05000311/LER-1981-001-03, /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | /03L-0:on 810104,during Cold Shutdown,Diesel Unit Trip Relay on Diesel Generator 2A Tripped.Cause Undetermined.Relay Reset.Diesel Generator Determined Operable After Satisfactory Completion of Tests | | | 05000311/LER-1981-002, Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | Forwards LER 81-002/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-002-03, /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | /03L-0:on 810117,during Routine Surveillance Test, 2A Diesel Generator Failed to Accelerate to 875 Rpm within 10-s.Caused by Failure of Solenoid Pilot Valves 21DA23A & 22DA23B.Valves Replaced | | | 05000272/LER-1981-002-03, /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | /03L-0:on 810108,during Normal Operations, Indication in Control Room of Svc Water Flow to Fan Coil Unit 14 Was Lost.Caused by Portable Propane Heaters Running Out of Fuel Resulting in Instrument Lines Freezing | | | 05000272/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000311/LER-1981-003, Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | Forwards LER 81-003/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-003-03, Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | Liquid Waste from Waste Monitor Tank 22 Was Released W/O Authorization.Caused by Operator Neglecting to Take Release Form to Lab for Approval.Supervisor & Operator Counseled | | | 05000272/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000272/LER-1981-003-03, /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | /03L-0:on 810109,component Cooling Water Heat Exchanger 12 Removed from Svc.Caused by Repair of Leaking Pipe Nipple at Weld Connecting Svc Water Drain Valve 12SW124 W/Heat Exchanger Tube Sheet.Nipple Replaced & Weld Reworked | | | 05000311/LER-1981-004-04, /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | /04T-0:on 810407,containment Fan Cooling Unit 24 Found Leaking Svc Water.Caused by Vent Valve 24SW63 Not Fully Closed.Valve Closed | | | 05000311/LER-1981-004, Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | Forwards LER 81-004/04T-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000272/LER-1981-004-03, /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | /03L-0:on 810119,during Daily Surveillance Test on Control Room Emergency Air Conditioning Sys Isolation Dampers,Damper 1CAA3 Failed to Close.Caused by Ice Formation on Louvers.Ice Melted & Damper Returned to Svc | | | 05000311/LER-1981-005-03, /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | /03L-0:on 810413,all Reactor Coolant & Residual Heat Removal Pumps Were de-energized Longer than Time Allowed by Tech Specs.Caused by Replacement of Relief Valve 2RH3 in Residual Heat Removal Sys | | | 05000311/LER-1981-005, Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | Forwards LER 81-005/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-005-03, /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. Defective Module Replaced | /03L-0:on 810128,during Routine Functional Test on Reactor Protection Sys,Safety Injection Signal Failed.Caused by Comparator Unit (Hagan Model 4111082-001) Failure. Defective Module Replaced | | | 05000272/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000311/LER-1981-006, Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | Forwards LER 81-006/03L-0.Detailed Event Analysis Encl | | | 05000311/LER-1981-006-03, /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | /03L-0:on 810419,valve 2PR1 Found Leaking.Caused by Seizing & Galling of Valve Stem & Gauge.Stem & Gauge Replaced.Channel Tested Satisfactorily & Returned to Svc 810504 | | | 05000272/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000272/LER-1981-006-03, /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | /03L-0:on 810115,no Audible Fire Alarm Would Sound.Caused by Current Impedance Mismatch Between Tone Generator of Fire Alarm Sys & Remainder of Sys Due to Overload.Generator Amplifier Adjusted | | | 05000272/LER-1981-007-03, /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | /03X-2:on 800128,during Review of Sys Diagrams, Demineralized Water Supply Check Valve to Auxiliary Feedwater Storage Tank 1DR7 Found to Be Not Seismically Qualified.Caused by Design Deficiency.Valve Qualified | | | 05000311/LER-1981-007, Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | Forwards LER 81-007/03L-0.Detailed Event Analysis Encl | | | 05000272/LER-1981-007, Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | Forwards LER 81-007/01X-1.Detailed Event Analysis Encl | | | 05000272/LER-1981-007-01, /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | /01X-1:on 810119,throttling Valves 14SJ16,11SJ138, 12SJ138 & 13SJ138 Found Out of Position.Caused by Procedure Inadequacy & Personnel Error.Valves Moved to Correct Positions & Procedures Changed | | | 05000311/LER-1981-007-03, /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | /03L-0:on 810423,while Attempting to Start Auxiliary Feedwater Pump 22,relay Flags for Phases a & C on Breaker 2B1D Found Dropped.Caused by Drifting of Wipe on Trip Latch.Wipe of Trip Latch Reset | | | 05000272/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000272/LER-1981-008-03, /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | /03L-0:on 810124,carriage Guide Wire of Auxiliary Annunciator Typewriter Broke,Resulting in Loss of Containment Sump Level Monitoring Sys.Caused by Equipment Failure.Broken Wire Replaced by Ibm Technician | | | 05000311/LER-1981-009-03, /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | /03L-0:on 810423,during Plant Cooldown,Inadvertent Safety Injection Occurred.Caused by Valve 24MS10 Opening, Causing Dilution of Boron Injection Tank to Below Min Limits.Situation Corrected within Allowed Limits | | | 05000272/LER-1981-009-01, /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | /01X-2:on 810129,during Normal Operation, Containment Sump Pump Operation Indicated 4.3 Gpm of Unidentified Leakage.Caused by Magnetrol Level Indicator Operating Erratically | | | 05000272/LER-1981-009, Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | Forwards LER 81-009/01X-2.Detailed Event Analysis Encl | | | 05000311/LER-1981-009, Forwards LER 81-009/03L-0 | Forwards LER 81-009/03L-0 | | | 05000311/LER-1981-010-03, /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. Caused by Worn Main Shaft Packing.Packing Replaced | /03L-0:on 810426,during Mode 3 Operations,Svc Water Pump 23 Declared Inoperable Due to Packing Leaks. Caused by Worn Main Shaft Packing.Packing Replaced | | | 05000311/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000272/LER-1981-010-03, /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | /03L-0:on 810126,containment Fan Coil Unit 11 Declared Inoperable in Order to Replace Leaking Spool Piece in Svc Water Line.Due to Reactor Trip,Fan Coil Unit Had to Be Tested & Declared Operational | | | 05000272/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000311/LER-1981-011-03, /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | /03L-0:on 810427,during Routine Entry Into Containment,Containment Airlock Outer Door Would Not Close. Caused by Out of Alignment Linkage & Subsequent Roller Bearing Damage.Linkage Realigned & Roller Bearings Replaced | | | 05000311/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-011-03, /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | /03L-0:on 810127,svc Water Line to Containment Fan Coil Unit 11 Found Leaking.Caused by Leaking Weld Connecting Spool Piece to Valve 11SW57.Weld Reworked & Spool Piece Replaced | | | 05000272/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000272/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000272/LER-1981-012-03, /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | /03L-0:on 810204,fire Pump 2 in Fire Suppression Water Sys Declared Inoperable for Maint on Leaking Inlet Cooling Water Line.Caused by Leaking Corrugated Stainless Steel Hose Connecting Common Cooling Water Piping | | | 05000311/LER-1981-012-03, /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | /03L-0:on 810427,during Surveillance Procedure Sp(O) 4.6.1.3 on Containment Air Lock,Leak Rate Exceeded Tech Specs.Caused by Inability of Inner Door Seals to Maintain Test Pressure.Seals Replaced | | | 05000311/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000311/LER-1981-013, Forwards LER 81-013/03L-0 | Forwards LER 81-013/03L-0 | | | 05000311/LER-1981-013-03, /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | /03L-0:on 810501,during Scheduled Type B & C Leakage Tests,Leak Rate Was Greater than Max Range of Volumetric Test Equipment.Caused by Use of Limited Range Equipment.Valves Adjusted & Airlock Door Seals Reworked | | | 05000272/LER-1981-013-03, /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | /03L-0:on 810201,centrifugal Charging Pump 12 Declared Inoperable Due to Leak in Pump Oil Cooler.Oil Cooler Replaced | |
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