05000311/LER-1981-047, Forwards LER 81-047/03L-0.Detailed Event Analysis Encl

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Forwards LER 81-047/03L-0.Detailed Event Analysis Encl
ML20030A809
Person / Time
Site: Salem PSEG icon.png
Issue date: 07/22/1981
From: Uderitz R
Public Service Enterprise Group
To: Grier B
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20030A810 List:
References
NUDOCS 8107290060
Download: ML20030A809 (3)


LER-1981-047, Forwards LER 81-047/03L-0.Detailed Event Analysis Encl
Event date:
Report date:
3111981047R00 - NRC Website

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O PSEG Public Service Electric and Gas Company 80 Park Plaza Newark, N.J. 07101 Phone 201/430-7000 July 22, 1981 to A

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i Mr. Boyce H. Grier I

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631 Park Avenue sj w ot King of Prussia, Pennsylvania 19406 4

Dear Mr. Grier:

LICENSE NO. DPR-75 DOCKET NO. 50-311 REPORTABLE OCCURRENCE 81-47/03L Pursuant to the requirements of Salem Generating Station Unit No. 2 Technical Specifications, Section 6.9.1.9.b, we are submitting Licenseo Event Report for Reportable Occurrence 81-47/03L.

This report is required within thirty (30) days of the occurrence.

Sincerely yours,

/Adda'/p p R. A.

Uderitz General Manager -

i Nuclear Production i

CC:

Director, Office of Inspection and Enforcement (30 copies) r Director, Office of Management Information and Program Control (3 copies)

? I 8107290060 810722 PDR ADOCK 05000311 S

PDR The Energy People w>zwn am m ten q

I Report Number:

81-47/03L Report Date:

July 22, 1981 Occurrence Date:

6-23-81 Facility:

Salem Generating Station, Unit 2 Public Service Electric & Gas Company Hancocks Bridge, New Jersey 08038 IDENTIFICATION OF OCCURRENCE:

Individual Rod Position Indication - ISB2 - Inoperable.

This report was initiated by Incident Report 81-205.

CONDITIONS PRIOR TO OCCURRENCE:

Mode 3 - Rx Power 0% - Unit Load 0 MWe DESCRIPTION OF OCCURRENCE:

During startup on June 23, 1981, the control operator noticed that the individual rod position indicator for rod ISB2 was in disagree-ment with the shutdown rod bank demand indicator by greater than

+ 12 steps.

The individual rod position indicator was declared Inoperable at 0624 hours0.00722 days <br />0.173 hours <br />0.00103 weeks <br />2.37432e-4 months <br /> and action statement 3.1.3.2.2 was entered.

This occurrence constituted operation in a degraded mode in accord-ance with technical specification 6.9.1.9.b.

DESIGNATION OF APPARENT CAUSE OF OCCURRENCE:

Equipment failure.

The individual rod position indicator for shutdown rod ISB2 was not in agreement with the shutdown rod bank demand indi-cator due to failure of the amplifier board in the indicator.

ANALYSIS OF OCCURRENCE:

Technical specification 3.1.3.2.2 requires:

When one rod position indicator is not within + 12 steps of the rod bank demand irdicator, the reactor trip system breakers be opened immediately.

CORRECTIVE ACTION

The reactor trip breakers were opened immediately.

The amplifier board in the individual rod position indicator for shutdown rod ISB2 was replaced in kind.

The indicator was recalibrated satisfactorily and returned to service.

Action statement 3.1.3.2.2 was terminated at 1011 hours0.0117 days <br />0.281 hours <br />0.00167 weeks <br />3.846855e-4 months <br />, June 23, 1981.

a LER 81-47/03L July 22, 1981 FAILURE DATA:

Bailey Instrument Co.,

Inc.

Bailey Edgewise Indicator Model RY2 Amplifier Board # 6627353-2 N', '/ -

4 *%~

Prepared By F.

Dickey Manafer - Salem Gederating Station SORC Meeting No.

81-65