05000281/FIN-2015004-01
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Finding | |
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Title | |
Description | A self-revealing, Green non-cited violation (NCV) of Surry Technical Specification (TS) 6.4.A.7 was identified because 2-RC-PCV-2455A, the Unit 2 A pressurizer (PZR) spray valve, developed a body to bonnet mechanical joint leak as a result of the failure of the joint upper gasket to adequately seal the joint. The gasket inadequately sealed the body to bonnet joint due to a misalignment of the cage and the cage spacer assembly with the valve body. This misalignment caused the reactor coolant system (RCS) allowable unidentified leak rate to approach the TS limit on July 13, 2015, and subsequently required an unplanned Unit 2 shutdown. This issue was documented in the licensees corrective action program (CAP) as condition report (CR) 1002302. The inspectors concluded that the failure of the licensee to have the instructions necessary to successfully accomplish the purpose of 0-MCM-0414-13, Copes-Vulcan 4 inch, 1500 pound Control Valve, Model D-1000 with Bellows Overhaul, Revision 3, as required by Dominion procedure SPAP-0504, Technical Procedure Writers Guide, Revision 9, and to correctly measure and resolve the upper gasket crush on A PZR spray valve, was a performance deficiency (PD). Using IMC 0612, Appendix B, Issue Screening, dated September 7, 2012, the inspectors determined that the PD was more than minor because it was associated with the procedural quality attribute of the Initiating Events Cornerstone and adversely affected the cornerstone objective to limit the likelihood of events that upset stability and challenge critical safety functions during shutdown as well as power operations. Using IMC 0609.04, Initial Characterization of Findings, Table 2, dated June 19, 2012; the finding was determined to affect the Initiating Events Cornerstone. The inspectors screened the finding using Manual Chapter 0609, Appendix A, SDP for Findings at-Power, dated June 19, 2012, and determined that it screened as Green because the deficiency did not cause a loss of mitigation equipment relied upon to transition the plant to a stable shutdown condition. This finding has a cross-cutting aspect in the consistent process aspect of the human performance area, H.13, because the licensee did not use a systematic approach to evaluate all available data in deciding to return the A PZR spray valve to service during the spring 2014 refueling outage (RFO). |
Site: | Surry |
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Report | IR 05000281/2015004 Section 1R12 |
Date counted | Dec 31, 2015 (2015Q4) |
Type: | NCV: Green |
cornerstone | Initiating Events |
Identified by: | Self-revealing |
Inspection Procedure: | IP 71111.12 |
Inspectors (proximate) | A Sengupta C Jones D Bacon P Mckenna R Kellner S Rose W Loo |
Violation of: | Technical Specification - Procedures Technical Specification |
CCA | H.13, Consistent Process |
INPO aspect | DM.1 |
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Finding - Surry - IR 05000281/2015004 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Surry) @ 2015Q4
Self-Identified List (Surry)
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