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| 05000277/LER-1981-001-04, /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. Instructions Posted at Chlorination Control Panel,Procedure Clarified & Individual Reinstructed | /04T-0:on 801019,max Daily Chlorination Time Limit Exceeded by 30 Minutes.Caused by Personnel Error. Instructions Posted at Chlorination Control Panel,Procedure Clarified & Individual Reinstructed | |
| 05000277/LER-1981-001, Forwards LER 81-001/04T-0 | Forwards LER 81-001/04T-0 | |
| 05000278/LER-1981-001-01, /01P-0:on 810101, While Operating at 100% Power, During Surveillance Testing,Core Spray Pump D Was Found Nonoperable.Caused by de-energized Condition of Springs in 4 Kv Circuit Breaker.Breaker Replaced | /01P-0:on 810101, While Operating at 100% Power, During Surveillance Testing,Core Spray Pump D Was Found Nonoperable.Caused by de-energized Condition of Springs in 4 Kv Circuit Breaker.Breaker Replaced | |
| 05000278/LER-1981-002-03, /03L-0:on 810109,HPCI Turbine Exhaust Inboard Drain Isolation Valve AO-5247 Failed to Stroke Fully.Caused by Cocked Valve Packing Follower Preventing Free Valve Stem Travel.Follower Realigned & Packing Retensioned | /03L-0:on 810109,HPCI Turbine Exhaust Inboard Drain Isolation Valve AO-5247 Failed to Stroke Fully.Caused by Cocked Valve Packing Follower Preventing Free Valve Stem Travel.Follower Realigned & Packing Retensioned | |
| 05000277/LER-1981-002, Forwards LER 81-002/01T-0 | Forwards LER 81-002/01T-0 | |
| 05000277/LER-1981-002-01, /01T-0:on 810105,reactor Core Isolation Cooling Pump Flow Indication Failed Rendering Automatic Flow Control Sys Inoperable.Caused by Electronic Failure of Square Root Extractor in Flow Control Circuitry.Extractor Replaced | /01T-0:on 810105,reactor Core Isolation Cooling Pump Flow Indication Failed Rendering Automatic Flow Control Sys Inoperable.Caused by Electronic Failure of Square Root Extractor in Flow Control Circuitry.Extractor Replaced | |
| 05000277/LER-1981-003-03, /03L-0:on 810112,DPIS 2-14-43B,core Spray Sparger to Reactor Pressure Vessel Dp Switch Found Set Below Tech Spec Limit.Caused by Barton Model 288 Dp Switch Failure Due to Setpoint Drift.Switch Recalibrated & Returned to Svc | /03L-0:on 810112,DPIS 2-14-43B,core Spray Sparger to Reactor Pressure Vessel Dp Switch Found Set Below Tech Spec Limit.Caused by Barton Model 288 Dp Switch Failure Due to Setpoint Drift.Switch Recalibrated & Returned to Svc | |
| 05000278/LER-1981-003, Forwards LER 81-003/01T-0 | Forwards LER 81-003/01T-0 | |
| 05000278/LER-1981-003-01, /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm | /01T-0:on 810113,during Surveillance Test W/Unit at Full Power,Oil Leak of Approx 3-5 Gallons Per Minute Discovered on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm | |
| 05000277/LER-1981-004, Forwards LER 81-004/01T-0 | Forwards LER 81-004/01T-0 | |
| 05000277/LER-1981-004-01, /01P-0:on 810114,while Operating at 100% Power, During Routine Surveillance Test of Diesel Generator,Breaker E-32 Failed to Close on Request.Caused by Unidentified Mechanical Deficiencies.Breaker Replaced & Tested | /01P-0:on 810114,while Operating at 100% Power, During Routine Surveillance Test of Diesel Generator,Breaker E-32 Failed to Close on Request.Caused by Unidentified Mechanical Deficiencies.Breaker Replaced & Tested | |
| 05000278/LER-1981-004-03, /03L-0:on 810126,reactor Pressure Switch PS-3-2-3-102C,which Trips Recirculation Pump a Found to Exceed Tech Spec Limit.Caused by Setpoint Drift of Static-O-Ring Pressure Switch.Instrument Recalibr | /03L-0:on 810126,reactor Pressure Switch PS-3-2-3-102C,which Trips Recirculation Pump a Found to Exceed Tech Spec Limit.Caused by Setpoint Drift of Static-O-Ring Pressure Switch.Instrument Recalibr | |
| 05000277/LER-1981-005-03, /03L-0:on 810116,torus Vent Valve AO-2514 Failed to Close Upon Receipt of Group Three Isolation Signal & W/Use of Remote Valve Control Switch.Caused by Sticking Solenoid Valve Asco 8300 D9RF.Valve Freed & Replaced 810116 | /03L-0:on 810116,torus Vent Valve AO-2514 Failed to Close Upon Receipt of Group Three Isolation Signal & W/Use of Remote Valve Control Switch.Caused by Sticking Solenoid Valve Asco 8300 D9RF.Valve Freed & Replaced 810116 | |
| 05000278/LER-1981-005-03, /03L-0:on 810127,setpoint of Temp Switch TS 5943 B (HPCI Steam Line Area High Temp Isolation) Found to Be Above Tech Spec Limit.Caused by Setpoint Drift.Instrument Recalibr to within Tech Spec Limits,Tested & Returned to Svc | /03L-0:on 810127,setpoint of Temp Switch TS 5943 B (HPCI Steam Line Area High Temp Isolation) Found to Be Above Tech Spec Limit.Caused by Setpoint Drift.Instrument Recalibr to within Tech Spec Limits,Tested & Returned to Svc | |
| 05000278/LER-1981-006-03, /03L-0:on 810227,core Spray Logic Sys B Failed. Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | /03L-0:on 810227,core Spray Logic Sys B Failed. Caused by Blown Fuse Due to Grounded Lug on Core Spray Pump Circuit Breaker D Latch Check Switch.Circuit Breaker Replaced & Lug on Grounded Circuit Breaker Repositioned | |
| 05000277/LER-1981-006-03, /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | /03L-0:on 810117,main Steam Line D Radiation Monitor Failed & During Repairs Line a Monitor Cable Was Disconnected.Caused by Technician Error.Techniques Reviewed W/Technicians | |
| 05000278/LER-1981-007-03, /03L-0:on 810206,main Steam Line Monitor a Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | /03L-0:on 810206,main Steam Line Monitor a Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | |
| 05000277/LER-1981-007-03, /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gain | /03L-0:on 810103,average Power Range Monitor Flux Scram Trip Setting Was Outside Tech Spec.Caused by Engineer Failure to Make Adjustments to Setting Gains.Gains Reset & Personnel Reinstructed in Importance of Monitoring Gains | |
| 05000278/LER-1981-008-01, /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | /01T-0:on 810211,main Isolation Valve on Loop B Mistakenly Isolated Instead of Loop a Valve During Installation of Test Connection to 1-inch Containment Atmospheric Dilution Line.Caused by Wrong Valve Designation | |
| 05000278/LER-1981-008, Forwards LER 81-008/01T-0 | Forwards LER 81-008/01T-0 | |
| 05000277/LER-1981-008-03, /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | /03L-0:on 810127,containment Isolation Valves SV-2978C & SV-2671A in Sample Lines to Oxygen Analyzer Failed to Close Fully.Caused by Sticking Plunger Assemblies. Valves Cleaned,Reassembled & Leak Tested on 810204 | |
| 05000278/LER-1981-009-03, /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | /03L-0:on 810216,during Surveillance Test,Oil Leak of 3-5 Gpm Found on Oil Supply Line to HPCI Turbine Manual/ Overspeed Trip Mechanism.Caused by Ruptured Diaphragm in Oil Line Pressure Control Valve VC-210 | |
| 05000277/LER-1981-009-03, /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | /03L-0:on 810126,diesel Cardox Fire Protection Sys E-3 Failed to Initiate Automatically During Testing. Caused by Microswitch in Electromanual Pilot Control Valve Solenoid Circuitry Being Stuck Open,Preventing Initiation | |
| 05000277/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | |
| 05000277/LER-1981-010-03, /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | /03L-0:on 810127,drywell Radiation Monitor Found Out of Svc During Full Operation.Caused by No Sample Flow Through Sys Due to Manual Sample/Purge Valve Dislodged from Normal Sample Position.Valve Returned to Position | |
| 05000278/LER-1981-011-03, /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | /03L-0:on 810307,seven MSIVs Failed Individual Tech Spec Leakage Limits.Single Valves Failed on HPCI 2-inch Turbine Exhaust Line.Test Taps Failed on Reactor Core Isolation Cooling 10 & 2-inch Exhaust Lines.Cause Unknown | |
| 05000278/LER-1981-012-03, /03L-0:on 810428,snubber from a Recirculation Pump Discharge Header Found to Have Locking Velocity Under Compression Less than Acceptable Value.Cause Not Determined. Snubber to Be Recalibr | /03L-0:on 810428,snubber from a Recirculation Pump Discharge Header Found to Have Locking Velocity Under Compression Less than Acceptable Value.Cause Not Determined. Snubber to Be Recalibr | |
| 05000277/LER-1981-012-03, /03L-0:on 810202,main Steam Line Monitor D Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | /03L-0:on 810202,main Steam Line Monitor D Indicated Low Level Radiation Resulting in Trip Setpoint Above Tech Spec Limit.Caused by Instrument Zero Drift. Monitor Calibr & Returned to Svc | |
| 05000277/LER-1981-013, Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | Forwards LER 81-013/01T-0.Provides Narrative Description of 810203 Occurrence Re Failure of Valves to Meet Seismic Qualification Requirements | |
| 05000278/LER-1981-013-01, /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | /01T-0:on 810830,personnel Discovered Water Backed Up Out of Floor Drain Sys Flowing Under Railroad Doors. Caused by Blockage in Drain Sys.Blockage Cleared,Water Pumped Out & Processed Through Radwaste | |
| 05000278/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | |
| 05000277/LER-1981-014-03, /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | /03L-0:on 810131,Leeds & Northrup Model W multi-point Temp Recorder TR-2-10-131 Found Not Recording Suppression Chamber Water Temp Per Tech Spec.Caused by Bound Drive Motor.Instrument Repaired & Returned to Svc on 810202 | |
| 05000278/LER-1981-014, Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-014/01T-0.Detailed Event Analysis Submitted | |
| 05000278/LER-1981-014-01, /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | /01T-0:on 810928,while in Cold Shutdown Condition W/Crd Sys Off to Support Plant Testing,Problems Were Encountered in Maintaining Vessel Level.Caused by Personnel Error & Incomplete Closure of Feedwater Stop Valve | |
| 05000278/LER-1981-015-01, /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | /01X-1:on 811023,offgas Sampling Sys Found Not Receiving Sufficient Flow.Caused by Sample Line Root Valve That Had Been Closed During Welding.Valve Opened & Added to Sys Checkoff List | |
| 05000278/LER-1981-015, Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | Forwards LER 81-015/01T-1.Detailed Event Analysis Submitted | |
| 05000278/LER-1981-016-03, /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | /03L-0:on 811027,during Surveillance Testing,Speed Control Problems W/Reactor Core Isolation Cooling Sys Were Observed.Caused by Electronic & Hydraulic Speed Controls Being Out of Tolerance.Adjustments Made to Components | |
| 05000277/LER-1981-016-03, /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | /03L-0:on 810225,reactor Core Isolation Cooling Trip Throttle Valve Would Not Reset to Normally Open Position Using Limitorque Operator,Following Manual Trip. Caused by Worn Worm Gear in Trip Throttle Valve Operator | |
| 05000277/LER-1981-017-03, /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | /03L-0:on 810318,all Inboard Sample Isolation valves,SV-2671A-SV2671G,closed.Caused by Short in Coil of dymo-type Solenoid Valve SV-2671A,which Blew Common Fuse in Control Circuit for All Seven Valves | |
| 05000278/LER-1981-017-03, /03L-0:on 811109,reactor Core Isolation Cooling High Steam Flow Isolation Switch Exceeded Tech Spec Limit. Caused by Setpoint Drift of Barton Model 288 Dpis.Instrument Recalibr | /03L-0:on 811109,reactor Core Isolation Cooling High Steam Flow Isolation Switch Exceeded Tech Spec Limit. Caused by Setpoint Drift of Barton Model 288 Dpis.Instrument Recalibr | |
| 05000277/LER-1981-018-03, /03L-0:on 810306,local Leak Rate Test Determined Excessive Leakage from Manual Isolation Valve SV-2671A. Caused by Dirt Buildup on Seating Surface,Preventing Proper Valve Disc Seating.Valve Cleaned & Returned to Svc | /03L-0:on 810306,local Leak Rate Test Determined Excessive Leakage from Manual Isolation Valve SV-2671A. Caused by Dirt Buildup on Seating Surface,Preventing Proper Valve Disc Seating.Valve Cleaned & Returned to Svc | |
| 05000278/LER-1981-018-03, /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | /03L-0:on 811124,HPCI Turbine Steam Supply Valve MO-3-123-14 Failed Shut & Sys Declared Inoperable.Caused by Blown Fuse in Valve Motor Circuit.Fuse Replaced | |
| 05000277/LER-1981-019, Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | Forwards LER 81-019/01T-0.Vent Monitors Could Become Inoperable If Walls Collapsed During Seismic Event | |
| 05000277/LER-1981-019-01, /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | /01T-0:on 810320,two Walls on Refueling Floor of Each Unit Found Unstable Under Effects of Dbe.Caused by Const or Design Error.Mods Completed to Walls.Mods Scheduled for Unit 3 Prior to Completion of Refueling Outage | |
| 05000278/LER-1981-019-03, /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | /03X-1:on 811121,drywell Wide Range Pressure Recorder PR-3508 Did Not Receive Signal & Was Declared Inoperable.Caused by Intentional Internal Ground in Printed Circuit Assembly.Floating Dc Sys Substituted | |
| 05000277/LER-1981-020-03, /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | /03L-0:on 810325,inboard Containment Radioactive Gas Sampler Isolation Valve SV-2671A Found Leaking.Caused by Plunger Assembly Sticking Due to Dirt Accumulation.Valve Cleaned | |
| 05000278/LER-1981-020-03, /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | /03L-0:on 811207,reactor Coolant Isolation Cooling Torus Suction Valve MO-3-13-41 Failed to Stroke.Caused by Broken Indicating Rod Jammed within Guide Cap.Broken Rod Removed & Valve Successfully Stroked Electrically | |
| 05000277/LER-1981-021-03, /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | /03L-0:on 810329,while at Full Power,Drywell Pressure Channel D Found Malfunctioning.Caused by Electronic Failure in Rosemount Model 1151 GP Pressure Transmitter. Circuit Boards on Transmitter Replaced | |
| 05000278/LER-1981-021-03, /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | /03L-0:on 811211,D Core Spray Pump Failed to Start During Surveillance Test Due to Failure of Pump Breaker to Close.Cause Not Determined.Failed Breaker Replaced & Checked Daily for 2 Wks to Verify Core Spray Sys Operability | |
| 05000277/LER-1981-022-01, /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | /01T-0:on 810331,drywell Chilled Water Sys Found Draining Via Normal Waste & Storm Drains to Discharge Canal. Caused by Operator Error.Release Terminated.Addl Corrective Actions Forthcoming | |