05000272/FIN-2017007-02
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Finding | |
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Title | |
Description | The team identified a Green non-cited violation of Technical Specification (TS) 6.8.1, Procedures and Programs, because since January 2007, PSEG did not establish an appropriate preventive maintenance (PM) schedule for the emergency diesel generator (EDG) ventilation dampers. Specifically, PSEG cancelled a pre-existing 36-month lubrication/clean/inspect PM in 2007 but failed to add the lubrication task to an existing 6-year damper PM as intended. As a result, since January 2007, the intended lubrication PM was cancelled for the inlet, recirculation, and exhaust ventilation dampers on all six Unit 1 and Unit 2 EDG ventilation systems. PSEGs immediate corrective actions included initiating a corrective action NOTF to address the PM inadequacy and extent-of-condition. The issue is more than minor because, if left uncorrected, it had the potential to lead to a more significant safety concern. Specifically, the removal of the EDG ventilation damper lubrication PM had the potential to adversely impact EDG reliability. In accordance with IMC 0609.04, Initial Characterization of Findings, and Exhibit 2 of IMC 0609, Appendix A, The SDP for Findings At-Power, the team determined that this finding was Green because it was not a design or qualification deficiency, did not involve an actual loss of safety function, did not represent the actual loss of a safety function of a single train for greater than its TS allowed outage time, and did not represent an actual loss of function of one or more non-TS trains of equipment designated as high safety-significant in PSEGs Maintenance Rule program for greater than 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The team determined there was no cross-cutting aspect associated with this finding since it was not representative of current PSEG performance. |
Site: | Salem |
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Report | IR 05000272/2017007 Section 1R21 |
Date counted | Sep 30, 2017 (2017Q3) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.21 |
Inspectors (proximate) | J Schoppy J Brand J Kulp A Patel S Kobylarz M Yeminy M Gray |
Violation of: | Technical Specification |
INPO aspect | |
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Finding - Salem - IR 05000272/2017007 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Salem) @ 2017Q3
Self-Identified List (Salem)
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