LER-1981-062, Forwards LER 81-062/03L-0.Detailed Event Analysis Encl |
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public Service Company *f Coblade VW 16805 Road 19 1/2, Platteville, Colorado 80651-9298 November 13, 1981 Fort St. Vrain Unit No. 1 P-81286
- M@MO\\V/F ls f"!i Mr. Karl V. Seyfrit, Director l (
D l 6 l981 lD*
Nuclear Regulatory Commission
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I' Region IV Office of Inspection and Enforcement 611 Ryan Plaza Drive
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Suite 1000 Arlington, Texas 76012
Reference:
Facility Operating License No. DPR-34 Docket No. 50-267
Dear Mr. Seyfrit:
Enclosed please find a copy of Reportable Occurrence Report No. 50-267/81-062, Final, submitted per the requirements of Technical Specification AC 7.5.2(b)2.
- Also, please find enclosed one copy of the Licensee Event Report for Reportable Occurrence Report No. 50-267/81-062.
Very truly yours, A'.
WLttn&
Don Warembourg
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Manage'r, Nuclear Production DW/cis Enclosure 4
1 cc: Director, MIPC 2
110V2 019816
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OCCURRENCE REPORT DISTRIBUTION Number of Copies t
l Department of Energy - - - - - - - - - - - - - - - - - - - - * - - - - - - - - -
1 (P Letter)
San Francisco Operations Office Attn California Patent Group
'1333 Broadway Oakland, California '94612 Department of Energy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Letter)'
Mr. Glen A. Newby, Chief HTR Branch Division of Nuclear Power Developannt Mail Station B-107 Washington. D.C.
20545 De pa r tme nt o f Ene r gy - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Letter)
Attnt Project Manager 110 Vest A Street. Suite 460 San Diego, California 92*^1 Mr. Karl V. Seyfrit Director 1
(Original of P Letter Region IV Office of Inspection and Enforcement and Copy of LER)
Nuclear Regulatory Commission 611 Ryan Plaza Drive Suite 1000 Arlington, Texas 76012 Dfrector - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - - -
1 (P Letter, LER)
Office of Management Information and Program Control U. S. Nuclear Regulatory Commission Washington, D.C.
20555-Mr. Ri cha rd ihe lps -
T- - - -. - ~- - - - - - - - - - - - - - - - - - - - - - 10 (0riginal of PFLC IAtter
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FSV, CA, Site plus Two Copies, One Representative Copy of P Letter. One General Atomic Cogany Copy of LER)
P. O. Box 425 Platteville, Colorado 80651 M r. B i ll Imva lee - - - - - - - - - - -.. - - - - - - - - - - - - - - - - - -
1 (P Letter, LER)
Nuclear Safety Analysis Center 3412 Hillview Avenue P. O. Box 10412 Palo Alto, California 94303 NRC Resident Site Inspector 1
(P Letter, LER)
' b1 REPORT DATE:
November 13, 1981 REPORTABLE'0CCURRENCE 81-062 ISSUE 0 OCCURRENCE DATE:
October 14, 1981 Page 1 of 3 FORT ST. VRAIN NUCLEAR GENERATING STATION PUBLIC SERVICE COMPANY OF COLORADO 16805 WELD COUNTY ROAD 19 1/2 PLATTEVILLE, COLORADO 80651-9298 REPORT N0. 50-267/81-062/03-L-0 Final IDENTIFICATION OF OCCURRENCE:
On three separate occasions, during the period from October 14, 1981, to October 19, 1981, the prestressed concrete reactor vessel cooling water system temperatures exceeded the allowable limits. This is a degraded mode of the LCD 4.2.15 and is reportable per Fort St.
Vrain Technical Specification AC 7.5.2(b)2.
EVENT
- - DESCRIPTION:
On October 14, 1981, during a planned power reduction for maintenance, the prestressed concrete reactor vessel (PCRV) cooling l
water Loop 2 temperature controller failed.
The Operations personnel j
discovered the problem and returned system operation and temperature to normal by means of an auxiliary bypass controller. Tne Loop 2 cooling water outlet temperature exceeded the 120 degrees fahrenheit limit of LC0 4.2.15 during this event.
The instrument department examined the controller, adjusted the input bridge amplifier, tested the controller, and returned it to service.
The same problem occurred again on October 16, 1981, and Operations personnel again utilized a bypass controller to return the system to l
normal temperature and operation.
The Loop 2 cooling water outlet temperature again exceeded the LCO limit of 120 degrees fahrenheit.
The instrument department inspected the controller, replaced the input bridge amplifier, calibrated the controller, and returned it to service.
On October 19, 1981, the temperature controller failed again with the cooling water temperature decreasing in Loop 2 until the average of the inlet and outlet was less than the 100 degrees fahrenheit required by-LC0 4.2.15.
The operations personnel restored system operations and temperature to' normal with a bypass controller.
The instrument department inspected the controller and found a bad solder
- - foint under the auto-manual relay.
The connection was resoldered, and the controller tested and returned to service.
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r REPORTABLE OCCURRENCE 81-062 ISSUE O Page 2 of 3
CAUSE
DESCRIPTION:
- - The_ temperature controller failure in all three cases was caused by a bad solder joint uride'r' the auto-manual relay.
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CORRECTIVE ACTION:
Th! cooling water temperature was returned to acceptable values, and the bad solder joint was resoldered.
No further corrective action is anticipated or required.
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- - l REPORTABLE OCCURRENCE 81-062 ISSUE 0 Page 3 of 3 M
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Prepared By:
Asa B. Reed Technical-Services Technician Reviewed By: bal da Charles Fuller Technical Services Engineering Supervisor Reviewed By:
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Edwim Df Hill Station Manager Approved By:
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[Auwb Don Warembourg
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Manager, Nuclear Production
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| 05000267/LER-1981-001, Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | Forwards LER 81-001/03L-0.Includes Narrative Description of Event Re High Outlet Temp in Pcrv Cooling Water Sys | | | 05000267/LER-1981-001-03, /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | /03L-0:on 801230,outlet Temp of Loop 2 Pcrv Cooling Water Sys Exceeded Tech Spec Level.Caused by High Setpoint of Cooling Water Temp Controller Following Calibr. Controller Reset & Operators Will Be Reinstructed on Sys | | | 05000267/LER-1981-002-03, /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | /03L-0:on 810107,during Normal Operation,Sampling Requirements of SR NR1.1 Found Not Met for Day shift,801225. Caused by Personnel Error.Sampling Resumed on Next Shift & Personnel Reinstructed Re Importance of Requirements | | | 05000267/LER-1981-002, Forwards LER 81-002/03L-0 | Forwards LER 81-002/03L-0 | | | 05000267/LER-1981-003-03, /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | /03L-0:on 810106,during Test,One Channel of 1D Helium Circulator Drain Malfunction Found Inoperable.Caused by Blown Switch Module Fuse.Fuse Replaced & Switch Returned to Svc | | | 05000267/LER-1981-003, Forwards LER 81-003/03L-0 | Forwards LER 81-003/03L-0 | | | 05000267/LER-1981-004-03, /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | /03L-0:on 810115,high Residual Chlorine Levels Found in Circulating Water Sys Liquid Effluent Sample.Cause Unknown.Subsequent Samples Normal | | | 05000267/LER-1981-004, Forwards LER 81-004/03L-0 | Forwards LER 81-004/03L-0 | | | 05000267/LER-1981-005, Forwards LER 81-005/03L-0 | Forwards LER 81-005/03L-0 | | | 05000267/LER-1981-005-03, /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | /03L-0:on 810107,during Surveillance Testing,Trip Setting on PDIS-21177 Bearing Water Differential Pressure Switch Found Below Tech Spec Limit.Caused by Instrument Drift.Switch Adjusted & Returned to Svc | | | 05000267/LER-1981-006-03, During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Annual Testing & Calibr,Six of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-006, Forwards LER 81-006/03L-0 | Forwards LER 81-006/03L-0 | | | 05000267/LER-1981-007, Forwards LER 81-007/03T-0 | Forwards LER 81-007/03T-0 | | | 05000267/LER-1981-007-03, /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | /03T-0:on 810108,during Pcrv Cooling Water Sys Data Evaluation,Violation of Limiting Conditions of Operation Found Re Loop 2 Inlet & Outlet Average Temp Below Tech Spec Limit.Caused by Insufficient Heat Input | | | 05000267/LER-1981-008, Forwards LER 81-008/03L-0 | Forwards LER 81-008/03L-0 | | | 05000267/LER-1981-008-03, /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | /03X-2:on 810120,during Primary Coolant Pressure Scram,Calibr Found Voltage Outputs of Three Pressure Transmitters High.Caused by Instrument Drift.Pressure Transmitters Calibr | | | 05000267/LER-1981-009, Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | Forwards LER 81-009/03L-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-009-03, /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | /03L-0:on 810116-0131,plant Operated in Degraded Mode on Five Occasions.Caused by Moisture Outgassing from Core Graphite Due to Increased Power Level.Average Core Outlet Temp Reduced & Purification Sys Removed | | | 05000267/LER-1981-010-03, /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | /03L-0:on 810120,five Sample Flow Circuits Found Out of Calibr.Caused by Change of Instrument Characteristics.Calibr Values Revised & Flow Transmitters Recalibr.Alarm Setpoint Functional Test Values Also Changed | | | 05000267/LER-1981-010, Forwards LER 81-010/03L-0 | Forwards LER 81-010/03L-0 | | | 05000267/LER-1981-011, Forwards LER 81-011/03L-0 | Forwards LER 81-011/03L-0 | | | 05000267/LER-1981-011-03, /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | /03L-0:on 810121,liquid Nitrogen Storage Tank Level Noted Below Min Required.Caused by Sys Usage & Late Delivery of Liquid Nitrogen.Delivery Restored Tank Levels to Acceptable Values.Second Load Delivered to Top Off Tank | | | 05000267/LER-1981-012-03, /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | /03L-0:on 810127,six of Twelve Steam Pipe Rupture (Pipe Cavity)Ultrasonic Noise Channels Had Unacceptably Low Response to Known Noise Source During Test.Caused by Microphone &/Or Transmitter Gain Reduced to Stop Tripping | | | 05000267/LER-1981-012, Forwards LER 81-012/03L-0 | Forwards LER 81-012/03L-0 | | | 05000267/LER-1981-013-01, /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | /01T-0:on 810203,following Liquid Waste Release 429,tritium Concentration Exceeded Tech Spec.Caused by Sys Design Inadequacy W/Oil Separator on Liquid Waste Discharge Line.Bypass Installed Around Oil Separator | | | 05000267/LER-1981-013, Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | Forwards LER 81-013/01T-0.Detailed Event Analysis Submitted | | | 05000267/LER-1981-014, Forwards LER 81-014/03L-0.Detailed Summary Also Encl | Forwards LER 81-014/03L-0.Detailed Summary Also Encl | | | 05000267/LER-1981-014-03, /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | /03L-0:on 810104,instrument Air Compressors 1C & 1A Out of Svc,Leaving Only Compressor 1B in Svc.Caused by Compressor 1C Tripping on High Discharge Air Temp & Compressor 1A Being Cleared Out for Insp & Repairs | | | 05000267/LER-1981-015, Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | Forwards LER 81-015/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-015-03, /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | /03L-0:on 810204-0220,plant Operated in Degraded Mode on Nine Occasions.Causes Include Increased Oxidant Outgassing After Power Increase & Moisture Introduced Into Primary Coolant as Part of Approved Test | | | 05000267/LER-1981-016-03, During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | During Testing,Three of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Dirt Accumulation in Electrical Switches.Switches Replaced | | | 05000267/LER-1981-016, Forwards LER 81-016/03L-0 | Forwards LER 81-016/03L-0 | | | 05000267/LER-1981-017-03, /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | /03L-0:on 810217,standby Diesel Engine 1B Tripped on High Cooling Water Temp.Caused by Sticking Temp Control Valve.Valve Disassembled,Cleaned & Returned to Svc | | | 05000267/LER-1981-017, Forwards LER 81-017/03L-0 | Forwards LER 81-017/03L-0 | | | 05000267/LER-1981-018-03, /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | /03L-0:on 810214,sample Flow Alarm Setpoints of Three Dewpoint Moisture Monitors Found Outside Tech Spec. Probably Caused by Previous Misadjustment.Trip Points Readjusted | | | 05000267/LER-1981-018, Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | Forwards LER 81-018/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019, Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | Forwards LER 81-019/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-019-03, /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | /03L-0:on 810220,plant Operated in Degraded Mode to Repair Pressure Control Valve PV-21243-1.Caused by Excessive Leakage Through 1/2-inch Masoneilan Pressure Control Valve.Valve Stroke Lengthened.Seat & Stem Replaced | | | 05000267/LER-1981-020, Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | Forwards LER 81-020/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-020-03, /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | /03L-0:on 810226,primary Coolant Moisture & Oxidants Exceeded Limits.Caused by Circulator Buffer Sys Upset & Helium Circulator Trip Due to 810223 Reactor Scram. Reactor Power Reduced Until Moisture Level Decreased | | | 05000267/LER-1981-021, Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | Forwards LER 81-021/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-021-03, /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | /03L-0:on 810302,liquid Nitrogen Storage Tank Level Lower than Tech Spec Requires.Caused by Sys Usage & Unavailable Recondensers.Level Restored W/Two Loads | | | 05000267/LER-1981-022, Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | Forwards LER 81-022/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-022-03, /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | /03L-0:on 810310,found That Total Dissolved Solids in Plant Nonradioactive Liquid Waste Effluent Exceeded Tech Specs on 810224.Caused by Restoration of Water Sys Blowdown at High Rate.Blowdown Reduced | | | 05000267/LER-1981-023, Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | Forwards LER 81-023/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-023-03, /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | /03L-0:on 810310,during Release of Reactor Bldg Sump,Sump Pump Effluent Discharge Proportional Sampler Found Inoperable.Caused by Error in Instructions.New Instructions Issued to Assure Sampler Operability | | | 05000267/LER-1981-024-03, During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | During Testing,Five of 12 Helium Circulator Seal Malfunction Pressure Differential Switch Units Tripped Outside Limits.Caused by Accumulation of Dirt on Switches.Switches Replaced | | | 05000267/LER-1981-024, Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | Forwards LER 81-024/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025, Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | Forwards LER 81-025/03L-0.Detailed Event Analysis Encl | | | 05000267/LER-1981-025-03, /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | /03X-1:on 810317,liquid Nitrogen Storage Tank Level Decreased to Below 650 Gallons.Caused by Loss of Power to Fill Line Isolation Valve.Circuit Breaker Reclosed.Level Reestablished.Bypass Valve Installed Around Converter | |
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