06-13-2016 | At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> EST on 4'13'2016 with H. B. Robinson Steam Electric Plant, Unit No. 2 in Mode 1 at 100 percent power, it was determined that the source document for the mass and energy release parameters used to determine the containment pressure and temperature response to a main steam line break inside containment does not adequately account for all possible single active failure scenarios in the steam or feedwater line isolation provisions. The source document addresses the active failure of the main feedwater regulating valves to close in the faulted steam generator feedline, but not the failure of a feedwater regulating bypass valve to close in that feedline. An active failure of a feedwater regulating bypass valve whereby the valve fails to close will increase the secondary mass available for release to the containment structure. This can result in higher peak containment pressure that could challenge the containment design pressure. This condition is only a concern when the feedwater regulating bypass valves are in the open position in Modes 1, 2, or 3, and they fail to close on an engineered safeguards actuation signal. Administrative controls and corrective actions have been implemented to maintain design control of the feedwater regulating bypass in these modes of operation. |
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Category:Letter
MONTHYEARIR 05000261/20244022024-10-16016 October 2024 – Security Target Set Baseline Inspection Report 05000261/2024402 IR 05000261/20244012024-09-11011 September 2024 Security Baseline Inspection Report 05000261/2024401 ML24242A2612024-08-29029 August 2024 Operator Licensing Examination Approval 05000261/2024301 IR 05000261/20240052024-08-22022 August 2024 Updated Inspection Plan for H.B. Robinson Steam Electric Plant - Report 05000261/2024005 ML24169A2712024-08-14014 August 2024 – Issuance of Amendment No. 280 to Adopt TSTF-258-A, Revision 4, Regarding Changes to Technical Specification 5.7, High Radiation Area IR 05000261/20240022024-08-0101 August 2024 Integrated Inspection Report 05000261/2024002 ML24183A0972024-07-12012 July 2024 ISFSI; Catawba 1, 2 & ISFSI; McGuire 1, 2 & ISFSI; Oconee 1, 2, 3 & ISFSI; Shearon Harris 1; H. B. Robinson 2 & ISFSI; and Radioactive Package Shipping Under 10 CFR 71 (71-266 & 71-345) – Review of QA Program Changes EPID L-2024-LLQ-0002 IR 05000261/20240112024-06-0303 June 2024 Focused Engineering Inspection- Commercial Grade Dedication Report 05000261/2024011 ML24114A0152024-06-0303 June 2024 Unit 2 – Issuance of Amendment No. 279 Regarding Application of Leak-Before-Break Methodology for Auxiliary Reactor Coolant System Piping IR 05000261/20240012024-05-0909 May 2024 Integrated Inspection Report 05000261/2024001 IR 05000261/20240102024-04-30030 April 2024 Biennial Problem Identification and Resolution Inspection Report 05000261/2024010 IR 05000261/20230062024-02-28028 February 2024 Annual Assessment Letter for H.B. Robinson Steam Electric Plant Unit 2 - Report 05000261-2023006 IR 05000261/20243012024-02-0606 February 2024 – Notification of Licensed Operator Initial Examination 05000261/2024301 ML24033A0592024-02-0202 February 2024 Response to Request for Additional Information License Amendment Request to Exclude the Dynamic Effects of Specific Postulated Pipe Ruptures from the Design and Licensing Basis Based on Leak-Before-Break Methodology IR 05000261/20230042024-01-31031 January 2024 Integrated Inspection Report 05000261/2023004 ML24009A2432024-01-25025 January 2024 Unit, No. 2 - Exemption from Select Requirements of 10 CFR Part 73 (EPID L-2023-LLE-0047 (Security Notifications, Reports, and Recordkeeping and Suspicious Activity Reporting)) ML24009A2712024-01-24024 January 2024 Revision to Reactor Vessel Material Surveillance Capsule Withdrawal Schedule ML23354A0052024-01-0808 January 2024 Request for Withholding Information from Public Disclosure, H. B. Robinson Steam Electric Plant, Unit No. 2 ML23342A0902023-12-0808 December 2023 Notification of Inspection and Request for Information for NRC Problem Identification and Resolution Inspection IR 05000261/20234202023-11-30030 November 2023 Security Baseline Inspection Report 05000261/2023420 (Cover Letter with Report) IR 05000261/20230102023-11-28028 November 2023 Fire Protection Team Inspection Report 05000261/2023010 ML23317A3462023-11-14014 November 2023 Duke Fleet - Correction Letter to License Amendment Nos. 312 & 340 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 IR 05000261/20230032023-11-0707 November 2023 Integrated Inspection Report 05000261 2023003 and 07200060 2023001 ML23226A0862023-10-12012 October 2023 Issuance of Amendment No. 277 Regarding Revision of TSs to Add High-High Steam Generator Level Function to Table 3.3.2-1 and Remove Obsolete Content from TSs 2.1.1.1 and 5.6.5.b ML23346A1322023-10-0606 October 2023 Communication from C-10 Research & Education Foundation Regarding NextEra Common Emergency Fleet Plan License Amendment Request and Related Documents Subsequently Published ML23256A0882023-09-25025 September 2023 Issuance of Alternative to Steam Generator Welds ML23195A0782023-08-29029 August 2023 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-554, Revision 1 ML23235A0552023-08-23023 August 2023 Notification of an Fire Protection Team Inspection (FPTI) (NRC Inspection Report 05000261/2023010) and Request for Information (RFI) IR 05000261/20230052023-08-21021 August 2023 Updated Inspection Plan for H.B. Robinson Steam Electric Plant (Report 05000261/2023005) IR 05000261/20230022023-08-0707 August 2023 Integrated Inspection Report 05000261/2023002 IR 05000261/20234022023-05-30030 May 2023 Cyber Security Inspection Report 05000261/2023402 ML23145A1602023-05-25025 May 2023 Submittal of Updated Final Safety Analysis Report (Revision No. 30), Independent Spent Fuel Storage Installation Safety Analysis Report (Revision No. 28), Technical Specifications Bases Revisions, Quality IR 05000261/20230012023-05-0202 May 2023 Integrated Inspection Report 05000261/2023001 ML23118A0762023-05-0101 May 2023 Approval for Use of Specific Provision of a Later Edition of the American Society of Mechanical Engineers Boiler and Pressure Vessel Code, Section XI ML22332A4932023-03-10010 March 2023 William States Lee III 1 and 2 - Issuance of Amendments Regarding the Relocation of the Emergency Operations Facility IR 05000261/20220062023-03-0101 March 2023 Annual Assessment Letter for H.B. Robinson Steam Electric Plant, Unit 2 (Report 05000261/2022006) ML23047A4512023-02-21021 February 2023 Information Request for the Cyber-Security Baseline Inspection, Notification to Perform Inspection 05000261/2023402 ML23041A2272023-02-13013 February 2023 2022 Q4 Robinson_Workflow Final ML22329A2982023-01-19019 January 2023 Issuance of Amendment No. 274 Regarding Revision of Technical Specification 3.8.1 Surveillance Requirement 3.8.1.16 ML22294A0922022-12-15015 December 2022 Issuance of Amendment No. 273 Regarding Adoption of TSTF-577, Revised Frequencies for Steam Generator Tube Inspections, Revision 1 ML22339A1362022-12-0101 December 2022 2023 Requalification Program Inspection - H.B. Robinson Nuclear Plant ML22322A1322022-11-18018 November 2022 301, NRC Operator License Examination Report & Cover Letter Merged ML22096A0032022-11-18018 November 2022 McGuire Nuclear Station and Shearon Harris Nuclear Power Plant Authorization of RA-19-0352 Regarding Use of Alternative for RPV Head Closure Stud Examinations ML22256A2532022-11-14014 November 2022 Issuance of Amendments Regarding the Adoption of Technical Specifications Task Force Traveler TSTF-541, Rev. 2 IR 05000261/20220032022-11-0303 November 2022 Integrated Inspection Report 05000261 2022003 IR 05000261/20224022022-10-19019 October 2022 Security Baseline Inspection Report 05000261/2022402 IR 05000261/20220102022-09-26026 September 2022 Design Basis Assurance Inspection (Teams) Inspection Report 05000261/2022010 IR 05000261/20223012022-09-23023 September 2022 301 Operator License Exam Approval Letter (05000261/2022301) ML22258A0302022-09-15015 September 2022 Evacuation Time Estimate Reports IR 05000261/20220052022-08-26026 August 2022 Updated Inspection Plan for the H.B Robinson Steam Electric Plant - Report 05000261/2022005-Final 2024-09-11
[Table view] Category:License Fee Requirements Letter
MONTHYEAR05000261/LER-2016-0022016-06-13013 June 2016 Unanalyzed Condition Related to Main Steam Line Break Inside Containment, LER 16-002-00 for H.B. Robinson Steam Electric Plant, unit No. 2, Regarding Unanalyzed Condition Related to Main Steam Line Break Inside Containment 2016-06-13
[Table view] Category:Licensee Event Report (LER)
MONTHYEARRA-19-0384, LER 20190-001-00 for H.B. Robinson Steam Electric Plant, Unit 2, Turbine Trip/Reactor Trip Due to Main Generator Lockout2019-10-0909 October 2019 LER 20190-001-00 for H.B. Robinson Steam Electric Plant, Unit 2, Turbine Trip/Reactor Trip Due to Main Generator Lockout 05000261/LER-2017-0022017-12-14014 December 2017 Plant Vital Area Security Vulnerability Discovered Without Compensatory Security Measures, LER 17-002-00 for H.B. Robinson, Unit 2, Regarding Plant Vital Area Security Vulnerability Discovered Without Compensatory Security Measures 05000261/LER-2017-0012017-06-0101 June 2017 Auxiliary Feedwater System Actuation During Surveillance Testing, LER 17-001-00 for H.B. Robinson, Unit 2, Regarding Auxiliary Feedwater System Actuation During Surveillance Testing 05000261/LER-2016-0052017-02-22022 February 2017 Reactor Trip and Automatic System Actuation Due to Weather-Related Grid Disturbance, LER 16-005-01 for H. B. Robinson Steam Electric Plant, Unit 2 Regarding Reactor Trip and Automatic System Actuation Due to Weather-Related Grid Disturbance 05000261/LER-2016-0022016-06-13013 June 2016 Unanalyzed Condition Related to Main Steam Line Break Inside Containment, LER 16-002-00 for H.B. Robinson Steam Electric Plant, unit No. 2, Regarding Unanalyzed Condition Related to Main Steam Line Break Inside Containment 05000261/LER-2016-0012016-03-21021 March 2016 Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling, LER 16-001-00 for H.B. Robinson, Unit 2, Regarding Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling RNP-RA/11-0057, LER 011-001-00 for H. B. Robinson, Unit 2, Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Pl2011-06-30030 June 2011 LER 011-001-00 for H. B. Robinson, Unit 2, Regarding Condition Prohibited by Technical Specifications When Non-Seismic System Was Aligned to Refueling Water Storage Tank Due to Regulatory Requirements Not Adequately Incorporated in Plant Do 2019-10-09
[Table view] |
Reported lessons learned are incorporated into the licensing process and fed back to industry Send comments regarding burden estimate to the FOIA, Privacy and Information Collections Branch (T-5 F53), U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001, or by intemet e-mail to Infocollects.Resource@nrc.gov, and to the Desk Officer Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget.
Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.
BACKGROUND
Regulatory Technical Specification (TS) Limiting Condition For Operation (LCO) 3.7.3 requires three Main Feedwater Isolation Valves (MFIVs) [ISV], three Main Feedwater Regulating Valves (MFRVs)[FCV], and three bypass valves[V] to be operable, except when valves are closed or isolated by a closed manual valve[V]. The capability for these valves to close following a steam line break is relied upon to terminate core response to excess feedwater flow induced Reactor Coolant System (RCS)[RCS] cooling, and to terminate mass energy release inside containment[VSL]. Continued feedwater flow to a faulted Steam Generator (SG)[SG] will provide additional secondary mass available for release to Containment resulting in a calculated exceedance of the structure's design pressure and its operability. Per T.S. 3.6.1, Containment shall be operable in Modes 1, 2, 3, and 4. This scenario was not considered in the plant safety analysis, and is therefore an unanalyzed condition.
The regulatory impact to the station as a consequence of this condition necessitates a 60-day licensee event report (LER) to the Nuclear Regulatory Commission (NRC) under 10 CFR 50.73(a)(2)(ii)(B), "Degraded or Unanalyzed Condition," and required an 8- hour non-emergency notification per 10 CFR 50.72(b)(3)(ii)(B), "Degraded or Unanalyzed Condition.
Technical H. B. Robinson Steam Electric Plant, Unit No. 2, (HBRSEP2) is equipped with three steam generators (SGs). Feedwater (FW) is independently supplied to each SG through a main feedwater isolation valve (MFIV) followed in series by a main feedwater regulating valve (MFRV). Both valves are designed to close on a Feedwater Isolation signal for the purpose of isolating FW. Each main feedwater line includes a bypass line with a smaller regulating valve known as the feedwater regulating bypass valve (FRBV). This line bypasses both the MFIVs and MFRVs and is connected upstream of the MFIVs. The FRBVs are normally closed during full power operation, will automatically close on Feedwater Isolation signal, and are used primarily during startup and shutdown when reduced feedwater flow is required to maintain SG water inventory. These valves may also be used during full power operation when automatic control of the MFRVs is not available. Because the bypass line is connected upstream of the MFIVs, there is no redundancy to automatic flow isolation through this bypass line. With the FRBV open during a faulted SG event, there could be continued FW if the FRBV failed to close as designed.
EVENT DESCRIPTION
At 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> EST on 4/13/2016, with the plant in Mode 1 at 100 percent power and no involvement of out-of-service structures, systems or components, a condition was identified with the Main Feedwater system [Si] whereby the current MSLB accident analysis does not consider a single active failure of the FRBVs (FCV-479, FCV-489 and FCV-499) to close coincident with a MSLB inside containment. This resulted in an unanalyzed condition that is contrary to the plant's design basis.
Westinghouse report, WCAP-15305, "Carolina Power & Light Company H.B. Robinson Steam Electric Plant Unit No. 2, Steam Line Break Containment Integrity Analysis," is the source document for the mass and energy release parameters to determine the containment pressure and temperature response to a MSLB. Nuclear Regulatory Commission (NRC) guidance provides that for steam and feedwater line break analyses the analysis should assume a single active failure in the steam or feedwater line isolation provisions or feedwater pumps[P] to maximize the containment peak pressure and temperature. The active failures in the feedwater line isolation provisions included in the WCAP only include failure of the main feedwater control valves (FCV-478, FCV-488 and FCV-498) to close in the faulted SG feedline. The WCAP does not address failure of the FRBVs (FCV-479, FCV-489 and FCV-499) to close in the faulted SG feedline. Operating Procedure (OP)-106, "NORMAL PLANT OPERATIONS," contains provisions for operation of the FRBVs in Mode 1. These valves are also open during plant startup. Upon a MSLB or a loss of coolant accident (LOCA) in containment the engineered safety features actuation system (ESFAS)[JE] is designed to actuate Feedwater Isolation which isolates feedwater (including tripping the main feed pumps[P]), by closing the MFRVs, the FWRVs, and the MSIVs.
EVENT DESCRIPTION (Continued) An active failure of a FRBV whereby the valve fails to close will increase the secondary mass available for release to the containment as well as increase the heat transferred to the secondary fluid. During an ESFAS initiation or Feedwater Isolation signal, the condensate pumps[P] and the heater drain pumps[P] (until low level trip) would continue to provide feedwater to the failed open FRBV. Increased secondary mass available for release to the containment will result in a higher peak containment pressure that would exceed the containment design pressure of 42 pounds per square inch gauge (PSIG), and can alter the offsite and control room total effective dose equivalent (TEDE) doses.
The relevant analyses that appear to be unanalyzed for this scenario are Updated Final Safety Analysis Report (UFSAR) Chapter 6.2.1.4, "Containment Analysis for Postulated Secondary System Pipe Ruptures," (WCAP-15305) related to containment design, and UFSAR Chapter 15.1.5, "Main Steamline Break Event," (ANP-2560) related to radiological consequences for both 102°0 power and Hot Zero Power conditions.
WCAP-15305 and ANP-2560 do not address a single failure of a feedwater bypass valve, and based on the estimated flow rates through the feedwater bypass valves following a feedwater pump trip. The resulting increase in secondary mass available for release to the containment under this postulated single failure is considered an unanalyzed condition.
A Prompt Determination of Operability (PDO) was prepared that recommended the Containment be considered operable but in a non- conforming condition while the plant was in Modes 1, 2, and 3, and that the FRBVs should remain closed and/or isolated while operating in these Modes. Administrative controls and corrective actions have been established to ensure this configuration.
CAUSAL FACTORS
The cause analysis resulting from this event has determined that during the establishment of the plant's current licensing basis for MSLB inside containment, the postulated single failure of the feedwater regulating bypass valve to close was not considered. This is a combination of original design issues and plant engineering decisions and activities that took place during the 1980s.
CORRECTIVE ACTIONS
Corrective actions in response to the condition and to restore compliance with regulations are listed below.
Immediate:
1. CR 2012658 generated to capture conditions in Corrective Action Program.
2. CR 2020495 generated to capture extent of condition in Corrective Action Program.
3. CR 2018710 generated to capture incorrect response to NRC IE Bulletin 80-04.
4. Standing Instruction 16-0003 implemented and Caution Tags placed on the FRBVs.
Planned:
1. Revise plant containment analysis input documents to complete a single failure analysis to address all the secondary side assumptions and make provisions for implementing further corrective actions as necessary.
2. Complete engineering change to update single failures to containment analysis inputs and licensing basis for MSLB to incorporate the feedwater isolation single failures as defined in related calculation into the current licensing basis.
SAFETY ANALYSIS
Failure of the feedwater bypass valves to automatically close following a main steamline break inside containment was found to be an issue as a single failure may lead to containment overpressure. This scenario was assessed utilizing probabilistic risk assessment methodology to determine the likelihood of this scenario occurring. Using conservative modeling techniques and conservative failure frequencies for the postulated events, this scenario was assessed and determined to have a very low safety significance. Two different failure modes were postulated for the valves: failure to close on demand and spuriously open during operation (and relevant common cause failures). These failure modes were evaluated for time frames determined from plant operation data and limited operator action was credited. The assessment determined that the scenario has a low safety significance for the periods with the valve(s) open. In addition this analysis did not credit any other potentially mitigating system to avert core damage in order to bound the analysis.
ADDITIONAL INFORMATION
A review of the industry Operating Experience (OE) was performed for a five (5) year span from 2011 to 2016. The search produced 433 reports. Several reports were reviewed for applicability based on subject titles, however no OE reviewed had the same circumstances as the subject condition, where an inadequate single failure analysis of the system was utilized in containment structure design pressure determination.
Energy Industry Identification System (EIIS) codes for systems and components relevant to this event are identified in the text of this document within brackets [ ].
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05000261/LER-2016-001 | Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling LER 16-001-00 for H.B. Robinson, Unit 2, Regarding Inoperability of Motor-Driven Auxiliary Feedwater Pumps Due to Insufficient Lube Oil Cooling | 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) | 05000261/LER-2016-002 | Unanalyzed Condition Related to Main Steam Line Break Inside Containment LER 16-002-00 for H.B. Robinson Steam Electric Plant, unit No. 2, Regarding Unanalyzed Condition Related to Main Steam Line Break Inside Containment | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000261/LER-2016-003 | Failure of Lake Robinson Tainter Gates to Fully Open During Performance of Functionality Testing | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | 05000261/LER-2016-004 | Reactor Trip During The Performance of a Visual Inspection of The Main Turbine Trip Block | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000261/LER-2016-005 | Reactor Trip and Automatic System Actuation Due to Weather-Related Grid Disturbance LER 16-005-01 for H. B. Robinson Steam Electric Plant, Unit 2 Regarding Reactor Trip and Automatic System Actuation Due to Weather-Related Grid Disturbance | 10 CFR 50.73(a)(2)(iv)(A), System Actuation |
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