05000261/FIN-2010009-10
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Finding | |
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Title | Failure of Charging Pump Suction Valves to Automatically Transfer Due to Errors in Implementing a Instrumentation Component Upgrade |
Description | Following the cable fault and resultant reactor trip, VCT level decreased and reached a low level set point that should have automatically transferred the suction source for the running charging pump to the RWST. The transfer did not take place as designed. The control circuitry which implements this transfer utilizes two VCT level transmitters. When each transmitter senses a low level, it energizes a relay via a comparator. When both relays are energized, and their contacts are closed, the circuit for opening the charging pump suction from RWST valve (LCV-115B) should be made up and the valve should open. Then, when LCV-115B opens, a signal is generated to close the VCT suction valve (LCV-115C.) One of the relays in the LCV-115B circuit was driven by an older style Hagan level comparator, and the other relay was driven by a newer style NUS comparator. Different NUS comparator configuration options, such as electromechanical relay or solid state output, can be made by placing plug-type jumpers at different locations on the circuit board. The licensees post-event troubleshooting revealed that the NUS comparator was not properly configured when it was installed in 2008. The NUS comparator should have been configured to have its output function operate in the solid state mode and energize the control relay when a low level was sensed. When the comparator was configured in 2008, the placement of jumpers resulted in an electromechanical relay output, which was only capable of de-energizing the control relay upon low level. As a result, the control relay driven by the NUS comparator was in the energized state when level in the VCT was normal. When level in the VCT decreased below the level at which the suction to the charging pumps should have transferred, the associated valves did not reposition because the relay driven by the NUS comparator was de-energized and the valve open circuit was not made up. The licensee did not detect the incorrect configuration of the NUS comparator after installation because of the limited scope of the post-installation testing. When the new comparator module was calibrated the bistable trip light responded as intended, satisfying the test acceptance criterion. The output contacts were not checked during the calibration and the licensee did not perform an integrated test, such as simulating a low VCT level, to confirm the two valves repositioned. The licensee replaced the VCT level Hagan comparator with an NUS comparator as part of a larger project to provide a replacement for obsolete Hagan comparators. Licensee engineers stated that about 80 percent of the Hagan comparators had been replaced with NUS comparators at the time of the AIT inspection. The team questioned the extent of condition for potential similar errors in replacement comparators, i.e. incorrect placement of jumpers and inadequate testing for detecting errors. The licensee noted that comparators used to perform reactor protection system functions, safety injection functions and certain other functions were subject to Technical Specification surveillance testing, which provided a check of the comparator output contacts. The licensee also pointed out that the circuit in question may have been unique in that only one of the comparators used in the two-out-of-two logic had been changed to the new NUS module. If two NUS modules had been installed, both containing the incorrect configuration for the jumpers, the transfer from VCT to RWST suction would have taken place with a normal VCT level and the problem would have been self revealing. The licensee stated that many control functions using the new NUS modules would alarm when the bistable actuates, making a similar problem self revealing. The licensee controlled the substitution of NUS comparators for Hagan comparators under the plant modification process using Engineering Evaluation EE-92-144. The licensee controlled component removal and installation within the maintenance process. The installation of the comparator for the charging pump suction transfer control circuit was accomplished under Work Order 011162348 in September 2008. Work order instructions directed an I&C technician to refer to the calibration procedure to determine the desired comparator configuration and refer to NUS instruction book EIP-M-DAM800 to determine the placement of jumpers necessary to implement that configuration. The placement and removal of jumpers was translated to work instructions which were reviewed and verified by an I&C system engineer. The licensee stated their planned corrective actions would include a review of all control circuits incorporating NUS comparators to confirm these circuits will operate properly. In cases where a review indicates proper operation cannot be assured, the licensee stated that appropriate testing will be performed. In addition, the process for implementing any future NUS comparator installations will be strengthened to preclude the problems described above. The team determined the failure of the suction for the charging pumps to automatically transfer from the VCT to the RWST upon low level in the VCT was caused by an error in the work instructions describing the placement of jumpers when a VCT level comparator was replaced. Additionally, the licensees post-maintenance testing was not adequate to detect the problem. Additional review by the NRC will be needed to determine whether these problems represent a performance deficiency. An Unresolved Item will be opened pending completion of this review. The issue is identified as URI 05000261/2010009-10, Failure of Charging Pump Suction Valves to Automatically Transfer Due to Errors in Implementing an Instrumentation Component Upgrade. |
Site: | Robinson |
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Report | IR 05000261/2010009 Section 4OA5 |
Date counted | Jun 30, 2010 (2010Q2) |
Type: | URI: |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 93800 |
Inspectors (proximate) | J Hanna J Hickey L Miller L Wert P Fillion P Pieringer R Monk S Currie F Ehrhardta Nielsenc Kontz D Bollock D Mills G Laska G Skinner J Beavers J Brady J Hickey J Worosilo M Bates P Braxton R Musserr Monkf Ehrhardt J Hanna L Miller J Hickey P Fillion L Wert P Pieringer S Currie |
INPO aspect | |
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Finding - Robinson - IR 05000261/2010009 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Robinson) @ 2010Q2
Self-Identified List (Robinson)
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