On December 22, 2005, while offline for maintenance, at approximately 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, both motor driven Auxiliary Feedwater pumps (AFWPs) received an automatic actuation signal to start. Both AFWPs were in service at the time feeding the SGs with the 22 Main Boiler Feedwater Pump ( MBFP) on turning gear and the 21 MBFP isolated and in recirculation.T A 22 SG High-High Level signal resulted in tripping the 21 MBFP which by design initiates start of the AFWPs.T The Reactor Operator ( RO) assigned to feed water control failed to adequately monitor SG level and overfed the 22 SG.T The RO had decreased AFW flow instead of stopping AFW flow as intended.T The RO failed to adequately monitor SG levels, check his actions or request a peer check. Operators restored the 22 SG level to normal.T The apparent cause was personnel error due to failure to perform self checking, and failure to monitor alternate SG level indications to ensure appropriate SG levels. Corrective actions include, administrative removal of the RO from licensed duties, simulator testing and evaluation and return to duty, coaching the RO on use of human performance tools, issuing a Station Clock Reset/Red Memo for this event as well as others for the shutdown to advise personnel of the event and lessons learned and convey management's expectations on use of human performance tools.TThe event had no effect on public health and safety.
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Note: The Energy Industry Identification System Codes are identified within brackets { }
DESCRIPTION OF EVENT
On December 22, 2005, while maintaining the plant at approximately 3% power during a plant shutdown to repair a packing leak on the 24 Steam Generator (SG) Feedwater Regulating Valve (FCV), at approximately 0550 hours0.00637 days <br />0.153 hours <br />9.093915e-4 weeks <br />2.09275e-4 months <br />, a High-High water level FW isolation signal {JB) was initiated at 73% water level for the 22 Steam Generator (SG) {AB). High level (73%) on two of three level transmitters {LT) on any SG results in a main turbine trip, automatic closure of the main and low flow FW regulating valves {FCV}, and closure of the Main Boiler Feedwater Pump (MBFP) {SJ} discharge valves. Closure of the MBFP discharge valves causes a trip of both MBFPs (SJ) and closure of all eight FW stop valves although only the main FW line stop valves are credited in the accident analysis for closing. A trip actuation signal for the MBFPs initiates the start of both motor driven Auxiliary Feedwater (AFW) {BA) Pumps (21 AFWP and 23 AFWP). Each AFWP supplies two SGs.
AFWP 21 delivers FW to SG-21 and SG-22 through valves FCV-406A and B. AFWP-23 delivers FW to SG-23 and SG-24 through valves FCV-406C and D. Although the AFWPs received an actuation signal to start, the AFWPs had been started at approximately 0523 hours0.00605 days <br />0.145 hours <br />8.647487e-4 weeks <br />1.990015e-4 months <br />, and operating in support of the maintenance outage.
The 22 MBFP was shutdown, isolated and had been placed on turning gear at approximately 0255 hours0.00295 days <br />0.0708 hours <br />4.21627e-4 weeks <br />9.70275e-5 months <br />. The 21 MBFP was isolated but operating in recirculation mode. The Main Turbine-Generator had been tripped at 0513 hours0.00594 days <br />0.143 hours <br />8.482143e-4 weeks <br />1.951965e-4 months <br />, in support of the maintenance outage. On December 22, 2005, at 1208 hours0.014 days <br />0.336 hours <br />0.002 weeks <br />4.59644e-4 months <br />, an eight hour non-emergency notification was made to the NRC (Log Number 42220) for a valid actuation of the AFW system under 10CFR50.72(b)(3)(iv)(A). The event was recorded in the Indian Point Energy Center corrective action program (CAP) as CR- IP2-2005-05252.
On December 21, 2005, the valve packing for SG FCV-447 was found to be leaking.
Maintenance attempted to adjust the packing for the valve but was unsuccessful.
Management decided to commence a power reduction in order to repair the valve packing. On December 22, at approximately 0025 hours2.893519e-4 days <br />0.00694 hours <br />4.133598e-5 weeks <br />9.5125e-6 months <br />, a down power commenced to 3% power to facilitate repacking FCV-447. During the maintenance shutdown, the reactor operator (RO) assigned FW control/SG level failed to check his actions when FW flow to the 22 SG was decreased. The RO observed the 22 SC water level rising but thought he had stopped AFW flow to the 22 SG. However, AFW flow was not completely isolated as intended and continued to supply AFW to the 22 SG at approximately 40 gpm. The RO then realized that the 22 SG water was still rising after observing 22 SG level at approximately 65%. The RO rechecked. AFW flow control and discovered AFW flow to 22 SG was not completely shut off as intended and was still feeding the 22 SG. The RO closed the AFW flow control valve and informed the Control Room Supervisor (CRS) of the high level.
However, the cold AFW addition near the High-High level setpoint heated and expanded in the SG and exceeded the 73% level FW isolation setpoint initiating FW isolation and the resultant MBFP trip and AFW actuation. Operations returned the 22 SG water level to the proper level.
CAUSE OF EVENT
The cause of the AFW pump actuation was an actuation signal from the MBFP trip circuit as a result of MBFP Overspeed trip actuation caused by a FW isolation signal due to High-High 22 SG level (73%). The High-High 22 SG level was the result of overfeeding the 22 SG. The apparent cause of overfeeding the 22 SG was human error as a result of inadequate error detection practices. Self checking was not applied to ensure the expected response. The RO responsible for monitoring and controlling SG levels did not verify the expected response after closing the control valve for AFW supply to the 22 SG. The RD failed to monitor important system parameters and compare alternate indications.
Alternate indications (e.g., flow indicator, computer, level trend recorder) were not checked to ensure flow was stopped. Contributing causes were: CC-1:
error detection practices, other intended or required verification was not performed. The RO controlling SG levels did not obtain a peer check when closing the AFW supply valve for the 22 SG. This is an expectation when manipulating plant components where adverse consequences can result from improper performance. CC-2: Ineffective oversight/command and control.
Supervisors did not reinforce expectations for using human performance tools (self checking/peer checking) and monitoring of important parameters.
CORRECTIVE ACTIONS
The following corrective actions have been or will be performed under the CAP to address the causes of this event and prevent recurrence.
- The RO was administratively removed from licensed duties. The RO was simulator tested and evaluated and no issues were identified. The RO returned to licensed duty.
- The RO received documented coaching as to management's expectations on the use of human performance tools and the need to perform self checking and peer checking.
- A Station Clock Reset and Red Memo was issued to site personnel due to this event as well as others during this shutdown to advise site personnel of the event and lessons learned and convey management's expectations on use of human performance tools (i.e., self-checking, peer checking, questioning attitude).
- The INPO AFI Action Plan (CR-IP2-2005-03898) will be revised to place added focus in the areas of monitoring of important process parameters and using alternate indications to confirm system status; use of self checking and peer checking during component manipulations, effectively implementing procedures, exercising effective oversight, and command and control.
EVENT ANALYSIS
The event is reportable under 10CFR50.73(a)(2)(iv)(A). The licensee shall report any event or condition that resulted in manual or automatic actuation of any of the systems listed under 10CFR50.73(a)(2)(iv)(B). Systems to which the requirements of 10CFR50.73(a)(2)(iv)(A) apply for this event include the AFWS. This event meets the reporting criteria because a start signal was initiated for the AFWS in accordance with design as a result of the 22 SG High-High level signal.
PAST SIMILAR EVENTS
A review of the past two years of Licensee Event Reports (LERs) for events that involved an AFWS actuation as a result of high SG level identified one LER.
LER-2004-001 reported a High-High level signal due to overfeeding the 22 SG as a result of a failure of Main Feedwater Regulating valve (FCV-427) to fully close.
The AFWPs had already been started due to a low SG level signal as a result of a manual reactor trip. The event reported in LER-2004-001 did not have the same cause (stuck valve) as this event (operator error), therefore the corrective actions for the event reported in LER-2004-001 would not have prevented this event
SAFETY SIGNIFICANCE
This event had no effect on the health and safety of the public.
There were no actual safety consequences for the event because there were no transients or accidents during the time of the event. Both AFWPs were operating and providing adequate FW flow to the SGs. Operators had alarms/indications alerting them to high SG level and procedures to direct proper actions.
Operators during this event recognized the 22 SG overfeed condition and took actions in accordance with plant procedures.
There were no significant potential safety consequences of this event under reasonable and credible alternative conditions. Excess FW addition at full power would cause a greater load demand on the reactor coolant system (RCS) due to increased subcooling in the SGs. A failure of operators to recognize the AFW pump operation could result in excess FW flow. The addition of cold FW would cause a decrease in RCS temperature and a consequential positive reactivity insertion due to the effects of negative moderator coefficient of reactivity.
Continuous excessive FW addition would be terminated by an automatic FW isolation actuated upon receipt of a SG High-High level water signal. The SG high-high water level signal also results in a turbine trip and subsequent reactor trip. Excessive FW addition transients at power are attenuated by the thermal capacity of the secondary plant and of the RCS. The reactor protection system overpower and overtemperature delta temperature trips and the high neutron flux trip prevent any power increase that could lead to a departure from nucleate boiling ratio (DNBR) less than the applicable DNBR limit.
This event was bounded by the analyzed event described in FSAR Section 14.1.10, Excessive heat removal due to a FW system malfunction. The plant performed as expected and the event was bounded by the FSAR analysis. For this event the AFWS actuated as designed and operators were alerted to the high SG condition to perform corrective action in accordance with plant procedures.
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05000328/LER-2005-001 | Unit 2 Reactor Trip Following Closure of Main Feedwater Upon Inadvertent Opening of Control Breakers | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000388/LER-2005-001 | DDegradation of Primary Coolant Pressure Boundary due to Recirculation Pump Discharge Valve Bonnet Vent Connection Weld Flaw | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000423/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000455/LER-2005-001 | Unit 2 Automatic Reactor Trip Due to Low Steam Generator Level resulting from a Software Fault on the Turbine Control Power Runback Feature | | 05000370/LER-2005-001 | Automatic Actuation of Motor Driven Auxiliary Feedwater Pumps During Outage | | 05000244/LER-2005-001 | Failure of ADFCS Power Supplies Results in Plant Trip | | 05000247/LER-2005-001 | 0Technical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by an Inoperable Auxiliary Component Cooling Water Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000529/LER-2005-001 | REACTOR HEAD VENT AXIAL INDICATIONS CAUSED BY DEGRADED ALLOY 600 COMPONENT | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000336/LER-2005-001 | | | 05000266/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000269/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000289/LER-2005-001 | | | 05000293/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000298/LER-2005-001 | Reactor Scram due to Reactor Level Transient and Inadvertent Rendering of High Pressure Coolant Injection Inoperable | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000331/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000315/LER-2005-001 | Reactor Trip Following Intermediate Range High Flux Signal | | 05000316/LER-2005-001 | Reactor Trip from RCP Bus Undervoltage Signal Complicated by Diesel Generator Output Breaker Failure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000317/LER-2005-001 | Main Feedwater Isolation Valve Inoperability Due to Handswitch Wiring | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000323/LER-2005-001 | TS 3.4.10 Not Met During Pressurizer Safety Valve Surveillance Testing Due to Random Lift Spread | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000333/LER-2005-001 | Inoperable Offsite Circuit In Excess of Technical Specifications Allowed Out of Service Time | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000352/LER-2005-001 | Loss Of Licensed Material In The Form Of A Radiation Detector Calibration Source | | 05000353/LER-2005-001 | Core Alterations Performed With Source Range Monitor Alarm Horn Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-001 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-001 | | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000362/LER-2005-001 | Emergency Diesel Generator (EDG) 3G003 Declared Inoperable Due to Loose Wiring Connection on Emergency Supply Fan | | 05000263/LER-2005-001 | | | 05000456/LER-2005-001 | Potential Technical Specification (TS) 3.9.4 Violation Due to Imprecise Original TS and TS Bases Wording | | 05000454/LER-2005-001 | Failed Technical Specification Ventilation Surveillance Requirements During Surveillance Requirement 3.0.3 Delay Period | | 05000282/LER-2005-001 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function | 05000286/LER-2005-001 | Plant in a Condition Prohibited by Technical Specifications due to Error Making Control Room Ventilation System Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000400/LER-2005-001 | Reactor Auxiliary Building Emergency Exhaust System Single Failure Vulnerability | | 05000395/LER-2005-001 | Emergency Diesel Generator Start and Load Due To A Loss Of Vital Bus | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000382/LER-2005-001 | RCS Pressure Boundary Leakage Due to Primary Water Stress Corrosion Cracking of a Pressurizer Heater Sleeve | 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | 05000305/LER-2005-001 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000369/LER-2005-001 | Reactor Coolant System Leakage Detection Instrumentation Inoperable | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000266/LER-2005-002 | | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | 05000255/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000361/LER-2005-002 | Missing Taper Pins on CCW Valve Cause Technical Specification Required Shutdown | 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000370/LER-2005-002 | Ice Condenser Lower Inlet Door Failed Surveillance Testing | | 05000353/LER-2005-002 | High Pressure Coolant Injection System Inoperable due to a Degraded Control Power Fuse Clip | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | 05000263/LER-2005-002 | | | 05000454/LER-2005-002 | One of Two Trains of Hydrogen Recombiners Inoperable Longer Than Allowed by Technical Specifications Due to Inadequate Procedure | | 05000244/LER-2005-002 | Emergency Diesel Generator Start Resulting From Loss of Off-Site Power Circuit 751 | | 05000362/LER-2005-002 | Emergency Containment Cooling Inoperable for Longer than Allowed by Technical Specifications | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000247/LER-2005-002 | DTechnical Specification Prohibited Condition Due to Exceeding the Allowed Completion Time for One Inoperable Train of ECCS Caused by Gas Intrusion from a Leaking Check Valve | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | 05000306/LER-2005-002 | | 10 CFR 50.73(a)(2)(v)(C), Loss of Safety Function - Release of Radioactive Material 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000265/LER-2005-002 | Main Steam Relief Valve Actuator Degradation Due to Failure to Correct Vibration Levels Exceeding Equipment Design Capacities | 10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | 05000286/LER-2005-002 | • Entergy Nuclear Northeast Indian Point Energy Center 450 Broadway, GSB P.O. Box 249Entergy Buchanan. NY 10511-0249 Tel 914 734 6700 Fred Dacimo Site Vice President Administration July 5, 2005 Indian Point Unit No. 3 Docket Nos. 50-286 N L-05-078 Document Control Desk U.S. Nuclear Regulatory Commission Mail Stop O-P1-17 Washington, DC 20555-0001 Subject:L Licensee Event Report # 2005-002-00, "Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure." Dear Sir: The attached Licensee Event Report (LER) 2005-002-00 is the follow-up written report submitted in accordance with 10 CFR 50.73. This event is of the type defined in 10 CFR 50.73(a)(2)(iv)(A) for an event recorded in the Entergy corrective action process as Condition Report CR-IP3-2005-02478. There are no commitments contained in this letter. Should you or your staff have any questions regarding this matter, please contact Mr. Patric W. Conroy, Manager, Licensing, Indian Point Energy Center at (914) 734-6668. Sincerely, 4F-/t R. Dacimo Vice President Indian Point Energy Center Docket No. 50-286 NL-05-078 Page 2 of 2 Attachment: LER-2005-002-00 CC: Mr. Samuel J. Collins Regional Administrator — Region I U.S. Nuclear Regulatory Commission U.S. Nuclear Regulatory Commission Resident Inspector's Office Resident Inspector Indian Point Unit 3 Mr. Paul Eddy State of New York Public Service Commission INPO Record Center NRC FORM 3660 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB NO. 3150-0104 EXPIRES: 06/30/2007 (6-2004) Estimated burden per response to comply with this mandatory collection request 50 hours.RReported lessons teamed are incorporated into the licensing process and fed back to Industry. Send comments regarding burden estimate to the Records and FOIA/Privacy Service Branch (T-5 F52), U.S. Nuclear Regulatory Commission, Washington, DC 29555-0001, or by InternetLICENSEE EVENT REPORT (LER) e-mail to Infocoilectsenrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-l0202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person Is not required to respond to, the Information collection. 1. FACIUTY NAME 2. DOCKET NUMBER 3. PAGE INDIAN POINT 3 05000-286 10OF06 4. TITLE Automatic Reactor Trip Due to 32 Steam Generator Steam Flow/Feedwater Flow Mismatch Caused by Low Feedwater Flow Due to Inadvertent Condensate Polisher Post Filter Bypass Valve Closure | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000287/LER-2005-002 | Unit 3 trip with ES actuation due to CRD Modification Deficiencies | 10 CFR 50.73(a)(2)(iv)(A), System Actuation | 05000336/LER-2005-002 | | 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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