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On February 2,
1985 the reactor was manually tripped during an orderly i
shutdown commenced when a hydrogen leak / oil mist was observed at the shaft seals of the Main Generator. The cause of the hydrogen leak was a malfunction of an oil filter in the seal oil supply line to the air side hydrogen seals.
Repairs were made to the filter which corrected the hydrogen leakage.
There was no impact on plant safety.
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.,...........-..w LICENSEE EVENT REPORT (LER) TEXT CONTINUATION o..owso o.
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INDIAN POINT, UNIT 2 02 0 ( 0; 1 0 ;0 Oj 2 o is to lo io l 2 417 B~ t 5 or 9
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1 On February 2, 1985 while the plant was at full power, a main generator
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hydrogen system trouble alarm annunciated.
Visual inspection of the - -
turbine generator revealed an oil mist at the shaft seals.
Further
.j inspection of the hydrogen seal oil unit revealed that the air side backup pump was in operation and the air si'de Cuno filter could not he rotated. The hydrogen pressure was observed to decrease.
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A decision was made to vent the generator hydrogen and to proceed with an orderly shutdown.
At fifty percent of full power the reactor was manually tripped.
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l Subsequent examination of the Cuno filter indicated that internal j
supports' had most likely failed as a result of incorrect reassembly.
H This. resulted in an inability to clean the Cuno filter, which had clogged' causing the sequence of. events described.
The Cuno filter was b
repaired and,placed back ~1n service.
The hydrogen seal oil unit was then manner and the plant was [j
shown - to be functioning in a.,sa,tisfactory il returned
A new duplex filter is being order. to
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k replace the current filter.
This is intended to assure that at least one l1 filter will be available.
O There wa r-no effect upon plant safety; the Peactor Protection System operated as designed.
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John D. O'Toob V.ce President Consolidated Edison Cornpany of New York, Inc.
4 frying Place, New York, NY 10003 Telepnene (212) 460-2533 February 20, 1985 Re:
Indian Point Unit No. 2 Docket No. 50-247 LER-85-001-00 Document Control Desk U. S. Nuclear Regulatory Commission Washington, D. C.
20555
Dear Sirs:
The attached Licensee Event Report LER-85-001-00 is hereby submitted in accordance with the requirements of 10 CFR Part 50.73.
Ve truly yours, J
l }/ f, YT a
attach.
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Dr. Thomas E. Murley, Regional Administrator-Region I U.
S. Nuclear Pegulatory Commission 631 Park Avenue King of Prussia, Pa.
19406 Senior Resident Inspector U.
S. Nuclear Regulatory Commission P. O.
Box 38 Buchanan, New York 10511
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| 05000247/LER-1985-001, :on 850202 Reactor Manually Tripped.Caused by H Leak & Oil Mist from Main Generator Shaft Seals Due to Malfunction of Oil Filter in Seal Oil Supply Line.Filter Repaired Correcting H Leak |
- on 850202 Reactor Manually Tripped.Caused by H Leak & Oil Mist from Main Generator Shaft Seals Due to Malfunction of Oil Filter in Seal Oil Supply Line.Filter Repaired Correcting H Leak
| | | 05000286/LER-1985-001-01, :on 850121,unit Trip & Safety Injection Actuation Occurred.Caused by Operators Switching Bus 31 to Backup Power Due to Low Voltage on Two Buses.Solenoid Coil Replaced & Surveillance Test Peformed |
- on 850121,unit Trip & Safety Injection Actuation Occurred.Caused by Operators Switching Bus 31 to Backup Power Due to Low Voltage on Two Buses.Solenoid Coil Replaced & Surveillance Test Peformed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-002, :on 850204,during Full Power,One of Two Main Boiler Feed Pumps Tripped Upon Loss of Control Oil.Caused by High Pressurizer Pressure & Orifices Clogging Main Boiler Feed Pump Control Oil Sys.Orifices Cleaned |
- on 850204,during Full Power,One of Two Main Boiler Feed Pumps Tripped Upon Loss of Control Oil.Caused by High Pressurizer Pressure & Orifices Clogging Main Boiler Feed Pump Control Oil Sys.Orifices Cleaned
| | | 05000286/LER-1985-002-01, :on 850123,high Level Generator Triggered Turbine & Reactor Trips.Caused by Feedwater Sys Perturbation Due to Starting Second Condensate Pump & Recirculation Valve.Valve Repaired & Calibr |
- on 850123,high Level Generator Triggered Turbine & Reactor Trips.Caused by Feedwater Sys Perturbation Due to Starting Second Condensate Pump & Recirculation Valve.Valve Repaired & Calibr
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000286/LER-1985-003-01, :on 850319,reactor Trip Breaker Opened, Initiating Unit Trip.Possibly Caused by Inadvertent Actuation of Manual Trip Lever.Testing & Preventive Maint Found No Irregularities |
- on 850319,reactor Trip Breaker Opened, Initiating Unit Trip.Possibly Caused by Inadvertent Actuation of Manual Trip Lever.Testing & Preventive Maint Found No Irregularities
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-003, :on 850213,recombiners 21 & 22 Experienced Malfunctions of Oxygen Supply Flow Regulating Valve & Pressure Switch,Respectively.Caused by Filter Clogged W/Rust & Defective Pressure Switch |
- on 850213,recombiners 21 & 22 Experienced Malfunctions of Oxygen Supply Flow Regulating Valve & Pressure Switch,Respectively.Caused by Filter Clogged W/Rust & Defective Pressure Switch
| | | 05000247/LER-1985-004, :on 850306,reactor Trip Occurred.Caused by Improperly Functioning Feedwater Regulating Valve.Relays in Instrumentation Sys for Feedwater Regulating Valves Replaced |
- on 850306,reactor Trip Occurred.Caused by Improperly Functioning Feedwater Regulating Valve.Relays in Instrumentation Sys for Feedwater Regulating Valves Replaced
| | | 05000286/LER-1985-004, :on 850320,during Plant Startup,Failure of Power Fuses for Nuclear Instrumentation intermediate-range Channel 36 Resulted in Three Reactor Trips.Caused by Intermittent Current Leak Across Test Switch |
- on 850320,during Plant Startup,Failure of Power Fuses for Nuclear Instrumentation intermediate-range Channel 36 Resulted in Three Reactor Trips.Caused by Intermittent Current Leak Across Test Switch
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000286/LER-1985-004-01, :on 850320,control Power Fuses for Nuclear Instrumentation Range Channel 36 Failed,Resulting in Three Reactor Trips.Caused by Current Leakage Across Test Switch. Testing Performed.Investigation Continuing |
- on 850320,control Power Fuses for Nuclear Instrumentation Range Channel 36 Failed,Resulting in Three Reactor Trips.Caused by Current Leakage Across Test Switch. Testing Performed.Investigation Continuing
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-005, :on 850326,main Boiler Feedwater Pumps 21 & 22 Tripped During Preplanned Power Descent.Probably Caused by Pressure Transient in Feedwater Sys.Positioner on Feedwater Regulating Valve Replaced & Valve Stroke Reset |
- on 850326,main Boiler Feedwater Pumps 21 & 22 Tripped During Preplanned Power Descent.Probably Caused by Pressure Transient in Feedwater Sys.Positioner on Feedwater Regulating Valve Replaced & Valve Stroke Reset
| | | 05000286/LER-1985-005-01, :on 850607,w/reactor at 55% Power While Unit Being Shut Down for Refueling Outage,High Pressure Steam Leak Occurred on Cover Gasket for Moisture Separate Reheater Drain Tank 32A.Gasket Replaced |
- on 850607,w/reactor at 55% Power While Unit Being Shut Down for Refueling Outage,High Pressure Steam Leak Occurred on Cover Gasket for Moisture Separate Reheater Drain Tank 32A.Gasket Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000286/LER-1985-006-01, :on 851004,turbine Trip & Subsequent Reactor Trip Initiated Automatically by High Water Level in Steam Generator 33.Caused by Malfunctioning Valve Positioner Linkage Assembly |
- on 851004,turbine Trip & Subsequent Reactor Trip Initiated Automatically by High Water Level in Steam Generator 33.Caused by Malfunctioning Valve Positioner Linkage Assembly
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-006, :on 850416,loss of Main Boiler Feedwater Pump 22 Initiated Reactor Trip on lo-lo Level Signal from Steam Generator 24.Caused by Reduction in auto-stop Oil Pressure. Pump Oil Sys Overhauled |
- on 850416,loss of Main Boiler Feedwater Pump 22 Initiated Reactor Trip on lo-lo Level Signal from Steam Generator 24.Caused by Reduction in auto-stop Oil Pressure. Pump Oil Sys Overhauled
| | | 05000247/LER-1985-007, :on 850711,gap Identified Between Seismic Restraint & Collar Mounted on Vertical Pumps in Excess of Structural Drawing Specs.Caused by Relaxing of Horizontal Restraints to Correct Pump Misalignment |
- on 850711,gap Identified Between Seismic Restraint & Collar Mounted on Vertical Pumps in Excess of Structural Drawing Specs.Caused by Relaxing of Horizontal Restraints to Correct Pump Misalignment
| | | 05000286/LER-1985-007-01, :on 851015,main Turbine Generator Trip Initiated Automatically by Signal from Main Turbine High Pressure Control Oil Sys.Caused by Blockage of Control Oil Strainers & Orifices.Strainer Cleaned |
- on 851015,main Turbine Generator Trip Initiated Automatically by Signal from Main Turbine High Pressure Control Oil Sys.Caused by Blockage of Control Oil Strainers & Orifices.Strainer Cleaned
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-008, :on 850821,daily Heat Balance Not Performed. Caused by Preoccupation W/Recovery from Transient Resulting from Rod Drop During Control Rod Insertion Test.Heat Balance Performed on 850822 |
- on 850821,daily Heat Balance Not Performed. Caused by Preoccupation W/Recovery from Transient Resulting from Rod Drop During Control Rod Insertion Test.Heat Balance Performed on 850822
| | | 05000286/LER-1985-008-01, :on 851018,boric Acid Concentrations Outside Tech Spec Limits.Caused by Difficulties Encountered by Plant Operators When Performing Precipitation Checks.Boric Acid Check Added to Plant Operator Training Program |
- on 851018,boric Acid Concentrations Outside Tech Spec Limits.Caused by Difficulties Encountered by Plant Operators When Performing Precipitation Checks.Boric Acid Check Added to Plant Operator Training Program
| 10 CFR 50.73(a)(2)(1) | | 05000247/LER-1985-009, :on 850920,short Circuit Between Phases of Main Transformer Caused Turbine Generator Trip.Caused by River Water Spray from Condenser Water Box Exhaust.Changes Made to Exhaust to Eliminate Spray |
- on 850920,short Circuit Between Phases of Main Transformer Caused Turbine Generator Trip.Caused by River Water Spray from Condenser Water Box Exhaust.Changes Made to Exhaust to Eliminate Spray
| | | 05000286/LER-1985-009-01, :on 851022,two 480-volt Bus Degraded Grid Voltage Timers Did Not Actuate within 45 as Required by Tech Specs.Caused by Instrument Drift.Timers Reset |
- on 851022,two 480-volt Bus Degraded Grid Voltage Timers Did Not Actuate within 45 as Required by Tech Specs.Caused by Instrument Drift.Timers Reset
| 10 CFR 50.73(a)(2)(1) | | 05000286/LER-1985-010-01, :on 851129,unit Tripped Due to Inadvertent Main Boiler Feedpump Shutdown & Low Water Level in Steam Generator 34.Caused by Painter Inadvertently Actuating Trip Lever.Painters Reinstructed |
- on 851129,unit Tripped Due to Inadvertent Main Boiler Feedpump Shutdown & Low Water Level in Steam Generator 34.Caused by Painter Inadvertently Actuating Trip Lever.Painters Reinstructed
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-010, :on 850923,reactor Tripped During Restart. Caused by Operator Failure to Anticipate Steam Generator Swell at Time of Synchronization of Generator Output.Event & Measures Implemented Reviewed |
- on 850923,reactor Tripped During Restart. Caused by Operator Failure to Anticipate Steam Generator Swell at Time of Synchronization of Generator Output.Event & Measures Implemented Reviewed
| | | 05000286/LER-1985-011-01, :on 851130,turbine Trip & Subsequent Reactor Trip Initiated Automatically by High Water Level in Steam Generator 32.Caused by Feedwater Perturbations During Flow Transfer Maneuvers |
- on 851130,turbine Trip & Subsequent Reactor Trip Initiated Automatically by High Water Level in Steam Generator 32.Caused by Feedwater Perturbations During Flow Transfer Maneuvers
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-011, :on 850927,hot Shutdown Completed Per Tech Specs Due to Proximity of Hurricane Gloria |
- on 850927,hot Shutdown Completed Per Tech Specs Due to Proximity of Hurricane Gloria
| | | 05000286/LER-1985-012-01, :on 851130,after Trip,Source Range Nuclear Instrumentation Channel 31 Failed to Reenergize When Reactor Neutron Flux Dropped Below Permissive Setpoint.Caused by Loose Wire Connection.Connection Repaired |
- on 851130,after Trip,Source Range Nuclear Instrumentation Channel 31 Failed to Reenergize When Reactor Neutron Flux Dropped Below Permissive Setpoint.Caused by Loose Wire Connection.Connection Repaired
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000247/LER-1985-012, :on 850928,reactor Trip Occurred Due to Power Range High flux-low Level Trip Signal.Caused by Operator Failure to Block Trip Signal Although Permissive for Blocking Trip Existed.Condition Stabilized |
- on 850928,reactor Trip Occurred Due to Power Range High flux-low Level Trip Signal.Caused by Operator Failure to Block Trip Signal Although Permissive for Blocking Trip Existed.Condition Stabilized
| | | 05000247/LER-1985-013, :on 851004,leakage Into Containment from All Sources Exceeded Tech Spec Limit of 10 Gpm for Combined Leakage.Source of Leakage Traced to Tube in Fan Cooler Unit Water Box.Tubing Replaced |
- on 851004,leakage Into Containment from All Sources Exceeded Tech Spec Limit of 10 Gpm for Combined Leakage.Source of Leakage Traced to Tube in Fan Cooler Unit Water Box.Tubing Replaced
| | | 05000247/LER-1985-014, :on 851024,reactor Tripped Due to High Steam Generator Level.Caused by Operator Error,Including Inadequate Training & Operator inexperience.Long- & short-term Actions Planned |
- on 851024,reactor Tripped Due to High Steam Generator Level.Caused by Operator Error,Including Inadequate Training & Operator inexperience.Long- & short-term Actions Planned
| | | 05000247/LER-1985-015, :on 851024,two Boron Injection Tank Level Transmitters Found Out of Calibr During Surveillance Test. Caused by burn-in of Transmitters.Surveillance Test Frequency Increased |
- on 851024,two Boron Injection Tank Level Transmitters Found Out of Calibr During Surveillance Test. Caused by burn-in of Transmitters.Surveillance Test Frequency Increased
| | | 05000247/LER-1985-016, :on 851212,reactor Trip Occurred Due to Loss of Reactor Coolant Flow Signals from Reactor Coolant Loop 21. Caused by Failed Bistable in Instrument Channel Coincident W/Signal from Low Flow Instrument Channel |
- on 851212,reactor Trip Occurred Due to Loss of Reactor Coolant Flow Signals from Reactor Coolant Loop 21. Caused by Failed Bistable in Instrument Channel Coincident W/Signal from Low Flow Instrument Channel
| | | 05000247/LER-1985-017, :on 851231,reactor Tripped on Low Pressurizer Pressure Due to Rapid Decrease in Pressure.Caused by Failure of Spray Valve PCV455A to Close Completely.Valve Isolated |
- on 851231,reactor Tripped on Low Pressurizer Pressure Due to Rapid Decrease in Pressure.Caused by Failure of Spray Valve PCV455A to Close Completely.Valve Isolated
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