05000247/FIN-2014002-03
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Finding | |
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Title | Spent Fuel Pool Fuel Assembly Interference Events |
Description | The Inspectors identified an NCV of 10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings, when Entergy used a test procedure that was not appropriate to the circumstances and the operating loop of RHR was stopped during the conduct of the test. The test procedure did not assure technical specification (TS) requirements were met for an operating loop of RHR when steam generators were not available for backup decay heat removal. This issue was entered into the licensees corrective action program as CR-IP2-2014-2709. The failure to accomplish testing using a procedure that ensured RCS loops were available for backup decay heat removal prior to stopping the operating RHR pump was a performance deficiency within the licensees ability to foresee and correct and should have been prevented. The finding was more than minor because if left uncorrected, would have the potential to become a more significant safety concern, specifically, a loss of decay heat removal cooling should the RHR pump fail to restart during the test without assurance that steam generators were available to remove decay heat. The inspectors evaluated the finding using IMC 0609, Attachment 0609.04, Initial Characterization of Findings, which directed the inspectors to screen the finding through IMC 0609, Appendix G, Shutdown Operations, using Attachment 1, Checklist 1, PWR Hot Shutdown Operation: Time to Core Boiling <2 Hours. No deficiencies were identified in Checklist 1 which required a phase 2 or phase 3 quantitative assessment as the licensee maintained adequate alternate mitigation capability and the finding screened to be of very low safety significance (Green). The inspectors concluded this finding had a cross-cutting aspect in the area of Human Performance, Design Margin, because the licensee did not put special attention in place to maintain safety-related equipment; specifically, when conducting testing that removed power from the running RHR loop without assurance that RCS loops remained filled and available for backup core cooling. |
Site: | Indian Point |
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Report | IR 05000247/2014002 Section 1R20 |
Date counted | Mar 31, 2014 (2014Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.2 |
Inspectors (proximate) | A Burritt A Patel E Burket E Gray G Newman J Furia J Stewart S Chaudhary S Pindale T. Lamb |
Violation of: | 10 CFR 50 Appendix B Criterion V Technical Specification Technical Specification - Procedures |
CCA | H.6, Design Margins |
INPO aspect | WP.2 |
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Finding - Indian Point - IR 05000247/2014002 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Indian Point) @ 2014Q1
Self-Identified List (Indian Point)
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