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 Start dateReporting criterionEvent description
05000281/LER-2020-001, Cancellation of LER 2020-001-00 for Surry Power Station Unit 2 Re Loss of Containment Cooling Affecting Containment Partial Pressure Indication6 November 2020
05000281/LER-2016-0019 October 2016
2 December 2016
10 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 9, 2016 at 0254 hours, with Unit 1 and Unit 2 at 100 percent power, Unit 2 experienced an automatic reactor trip initiated by a turbine trip due to generator differential lockout relay actuation. At the time of the trip, high wind and heavy rain conditions existed due to the effects of Hurricane Matthew. All three auxiliary feedwater pumps automatically started on low-low steam generator water level as expected. All plant systems functioned as required, and Unit 2 was stabilized at hot shutdown. The trip response was not affected by any previously inoperable systems, structures, or components.

The direct cause of the generator differential lockout was an electrical ground overcurrent initiated by water accumulation in the "A" phase of the "A" station service transformer leads termination enclosure. Affected electrical enclosures were drained, the system was tested, and modifications to the enclosures to prevent recurrence of water intrusion were completed prior to returning Unit 2 to power operation on October 13, 2016.

This report is being submitted pursuant to 10CFR50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System' and the Auxiliary Feedwater System.

05000281/LER-2015-00216 September 201510 CFR 50.73(a)(2)(iv)(A), System ActuationOn September 16, 2015, at 2014 hours with Units 1 and 2 operating at 100 percent power, Emergency Diesel Generator 2 automatically started and assumed power to the Unit 2 'H' emergency bus. The event occurred during quarterly performance of the Emergency Bus Undervoltage and Degraded Voltage Protection Test. The direct cause of the event was the defective "A" single phase relay sticking and preventing the relay contacts from changing state. The procedures for Emergency Bus Undervoltage and Degraded Voltage Protection Tests have been revised to physically validate the state of the emergency bus relays prior to testing additional relays. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(iv)(A) for valid actuation of an Emergency Diesel Generator.
05000281/LER-2015-00121 July 201510 CFR 50.73(a)(2)(iv)(A), System Actuation

On July 21, 2015 at 05:05, with Unit 1 at Hot Shutdown and Unit 2 at approximately 6% power, Unit 2 experienced a reactor trip initiated from a turbine trip during performance of the Turbine Overspeed Protection Control system circuitry testing. The turbine trip was caused by governor valves rapidly opening due to a speed error which had accumulated between the turbine speed and reference setpoint resulting in a rapid increase in impulse pressure. The root cause of this event was inadequate instructions in the Overspeed Protection Control testing section of the operating procedure. The testing will be removed from operating procedures and placed in test procedures that are not performed as part of routine turbine startup.

All systems functioned as required. Initiation of auxiliary or emergency systems was not required. Unit 2 was placed in hot shutdown and the health and safety of the public were not affected.

This report is being submitted pursuant to 10CFR50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System.

05000281/LER-2014-00213 October 201410 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 13, 2014 at 07:58, with Units 1 and 2 at 100% power, Unit 2 experienced a reactor trip due to a spurious opening of the Unit 2 "B" reactor trip breaker due to a loose screw on a reactor protection trip relay for the reactor trip breaker.

All three auxiliary feedwater pumps automatically started on low-low steam generator water level providing flow to the steam generators. The rapid increase in steam generator pressure on the relief valve setpoints resulted in the lifting of all three steam generator power operated relief valves. Unit 2 was placed in hot shutdown and the health and safety of the public were not affected. The loose screw on the reactor protection trip breaker relay was tightened and the breaker was closed successfully. Remaining connections on the Unit 2 relay control circuitry were checked for tightness. Unit 1 reactor trip breaker relay control circuitry will be checked for tightness at the next available opportunity. Torque requirements for terminal screws will be incorporated into the Surry Electrical Installation Specification and applicable procedures will be revised to include the torque requirements.

This report is being submitted pursuant to 10CFR50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System and the Auxiliary Feedwater System.

05000281/LER-2014-00130 April 201410 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On April 30, 2014, with Unit 2 in cold shut down for a refueling outage, the Unit 2A pressurizer safety valve failed its as-found test due to the lift setting being lower than the setpoint tolerance allowed by Technical Specifications.

On May 6, 2014, the Unit 2C pressurizer safety valve also failed its as-found test due to the lift setting being lower than the setpoint tolerance allowed by Technical Specifications.

The as-found pressurizer safety valve lift settings were evaluated and it was determined the valves were capable of performing their safety function with the low as-found lift settings. Therefore, the health and safety of the public were not affected.

This report is being submitted, pursuant to 10 CFR 50.73(a)(2)(i)(B), for operation prohibited by Technical Specifications.

05000281/LER-2013-00210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical SpecificationsAt 21:00 on June 23, 2013, with both Unit 1 and Unit 2 operating at 100%, an operator identified a discrepancy with the valve position on the Unit 2 Turbine Driven Auxiliary Feedwater Pump turbine trip throttle valve. The apparent cause of the Unit 2 trip throttle valve abnormal position is thread wear between the screw spindle (stem) and sliding nut. The vibrations from infrequently running adjacent equipment caused the valve to move in a closed direction. The trip throttle valve was returned to open and the handwheel secured in the open position. Due to partial closure of the trip throttle valve, the Unit 2 Turbine Driven Auxiliary Feedwater Pump was determined to be inoperable for greater than the Technical Specification limiting condition of operation and therefore, this report is being submitted, pursuant to 10 CFR 50.73(a)(2)(i)(B) for operation prohibited by Technical Specifications. Based on an assessment of this event, the risk impact was determined to be very small and, as a result, the health and safety of the public were not affected.
05000281/LER-2013-00110 CFR 50.73(a)(2)(iv)(A), System ActuationAt 08:03 on December 29, 2012, with both Unit 1 and Unit 2 operating at 100%, the supply breaker to the B reserve station service transformer (RSST) tripped open on an instantaneous over-current of the B and C phases due to a pelican contacting the overhead lines from the switchyard to the B RSST. This resulted in a lockout of the B RSST and loss of power to the E transfer bus and the Unit 2 H emergency bus from its normal off-site power supply. An under-voltage auto start signal was generated, and emergency diesel generator (EDG) 2 started and loaded on the Unit 2 H emergency bus as designed. Equipment performed as expected during the event, and there were no unexplained occurrences. Visual inspections verified there was no damage to the lines, supply breaker, or B RSST. The E transfer bus was reenergized at 12:23, and the normal source of power was restored to Unit 2 H emergency bus at 12:42. EDG 2 was returned to auto at 15:18. All electrical distribution systems were restored to a normal alignment. The work management process has been initiated to install bird diverters on the lines. This report is being submitted, pursuant to 10 CFR 50.73(a)(2)(iv)(A), for automatic actuation of EDG 2. This event did not affect the health and safety of the public.
05000281/LER-2008-00110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)
05000281/LER-1992-001, Corrected Page 3 to LER 92-001-00 Re 920130 Mechanical Failure Due to Oil Leak from Charging Pump a Bearing & Damper Remaining Closed on Charging Pump B26 March 1992
05000281/LER-1986-020, Forwards LER 86-020-01 & Reactor Trip & Feedwater Pipe Failure Rept14 January 1987
05000281/LER-1983-014, Forwards LERs 83-013/03L-0 & 83-014/03L-0.W/o LER 83-014/03L-018 April 1983
05000281/LER-1983-008, Forwards LER 83-008/03L-014 March 1983
05000281/LER-1983-007, Forwards LER 83-007/03L-017 March 1983
05000281/LER-1983-001, Forwards LER 83-001/03L-0 & Updated LERs 81-052/03X-1 & 81-074/03X-131 January 1983
05000281/LER-1982-076, Forwards LER 82-076/03L-014 January 1983
05000281/LER-1982-067, Forwards LER 82-067/03L-09 December 1982
05000281/LER-1982-056, Forwards LER 82-056/03L-07 October 1982
05000281/LER-1982-046, Forwards LER 82-046/03L-0 & Updated LER 80-010/01X-113 August 1982
05000281/LER-1982-037, Forwards LER 82-037/03L-012 July 1982
05000281/LER-1982-023, Forwards LER 82-023/03L-020 May 1982
05000281/LER-1981-075, Forwards LER 81-075/03L-08 December 1981
05000281/LER-1981-074, Updated LER 81-074/03X-1:on 811120,higher than Normal Activity Detected in Storm Drain Sys.Caused by Leaks from Stripper Feed Steam Heater Due to Failure of Heater Drain Receiver & Pumps to Prevent Overflow.Tubes Plugged31 January 1983
05000281/LER-1981-052, Updated LER 81-052/03X-1:on 810815,valve MOV-SW-202A Failed to Close Due to Grounded Motor.Grounding Caused by Flooding in Sump.Motor Replaced31 January 1983
05000281/LER-1980-010, Updated LER 80-010/01X-1:on 800721,containment Gaseous & Particulate Radiation Monitor Found to Have One Automatic Function Incapable of Operating During Fuel Movement.Caused by Bypass of Containment Exhaust Fan Relay in Design13 August 1982
05000281/LER-1976-015, Updated LER 76-15/03L:on 761006,leakage of Water Observed from Recirculation Spray HX a Piping.Caused by Cracking in Heat Affected Zones of Several Welds.Listed Piping Will Be Replaced19 November 1976
05000281/LER-1976-003, Updated LER 76-03/01T:on 760521,routine Chemistry Analysis of Primary Coolant Boron Concentration Indicated Unplanned Dilution Occurred.Caused by Three Tubes Cut on Steam Generator 2A.Tubes Plugged27 July 1976
05000281/LER-1975-012, Suppl to LER 75-12/01T:on 750706,reactor Trip Occurred. Caused by Sudden Closure of Trip Valve in Main Steam Line B Followed by Closure of Main Steam Line Valves a & C20 January 1976
05000281/LER-1975-005, Updated LER 75-05/010:on 750225,radial Trip of Max 2.5% Existed.Caused by Prolonged Recovery of Rod F-2.Control Room Alarm Did Not Function Due to Defective Circuit Card. Card Replaced & Staff Cautioned8 April 1975
05000280/LER-2019-0024 February 2020
05000280/LER-2017-0019 August 2017
6 October 2017
10 CFR 50.73(a)(2)(ii)
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On August 6, 2017, with Unit 1 at 100% power, a Reactor Coolant System (RCS) leak rate calculation determined the unidentified leak rate increased by 0.08 .gallons per minute. On August 8, a leak was obServed at an RCS hot leg.sample system valve,- and Unit 1 power level was reduced to investigate leakage indications. The. root isolation valve for the sample system valve was closed; however, leakage could not be verified as completely isolated. Further evaluation determined the leak to be through wall at the inlet of the sample system valve. Based upon the source of the leak and possible continued leakage, a Technical Specification shutdown clock was entered on August 9, at 13:38 hours. At 16:37 hours, Unit 1 was placed in Hot Shutdown.

The cause of the event was the RCS pressure boundary leakage at the tubing/socket weld area of the hot leg sample system valve. With the unit in Hot Shutdown, the leak was isolated and repaired, and Unit 1 was returned to power operation on August 11, 2017. An apparent cause evaluation is being conducted. The event was reported as a plant shutdown required by Technical Specifications pursuant to 10 CFR 50.72(b)(2)(i) and degraded condition pursuant to 10 CFR 50.72(b)(3)(ii)(A). This report is being provided pursuant to 10 CFR 50.73(a)(2)(i)(A) and 10 CFR 50.73(a)(2)(ii)(A).

05000280/LER-2016-00111 July 201610 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
On April 7, 2016 at 0638 hours, with Surry Power Station Units 1 and 2 operating at 100% power, the Emergency Service Water Pump (ESWP) 1B cooling water discharge valve flange was found to be cracked, and the pump was declared inoperable. During flange and valve suppOrt repair activities, four bolts on the cooling water discharge valve support base plate were found to be failed due to corrosion. The flange was replaced and the support base plates were anchored with stainless steel bolts. ESWP 1B was returned to operable status on April 9, 2016 at 1105 hours. The cause of the flange and support failure was corrosion of the base plate and anchor bolts from repetitive exposure to service water. On May 11, 2016, an Engineering evaluation determined that the piping and support had been non-functional for prior operability based on the potential for lateral displacement during a seismic event. Therefore, this report is being submitted, pursuant to 10 CFR 50.73(a)(2)(i)(B), for operations prohibited by Technical Specifications, and pursuant to 10 CFR 50.73(a)(2)(v)(B), an event or condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to remove residual heat. Based on the risk assessment of this event, the risk impact was determined to be of very low significance, and, as a result, the health and safety of the public were not affected.
05000280/LER-2015-00313 October 201510 CFR 50.73(a)(2)(iv)(A), System Actuation

On October 13, 2015 at 1815 hours, with Unit 1 at 100 percent power and Unit 2 at 93.5 percent power at the end of life coastdown, Unit 1 experienced a reactor trip initiated from a turbine trip by main generator trip. The main generator trip was due to a loss of the main generator field that caused a loss of field protection relay to trip.

All three auxiliary feedwater pumps automatically started on low-low steam generator water level providing flow to the steam generators. Main steam trip valves were closed due to primary cooldown in accordance with emergency operating procedures and the plant was stabilized using steam generator power operated relief valves. The direct cause of the loss of main generator field of the Unit 1 generator was an electrical fault in the main generator exciter spacer coupling. Corrective actions to prevent recurrence will be implemented through the corrective action program when the root cause evaluation is completed.

This report is being submitted pursuant to 10CFR50.73(a)(2)(iv)(A) as an event that resulted in the automatic actuation of the Reactor Protection System and the Auxiliary Feedwater System.

05000280/LER-2015-00214 August 2015

On August 14, 2015 at approximately 0830 hours, with Surry Power Station Units 1 and 2 operating at 100% power, a Virginia Electric and Power Company (Dominion) Nuclear Security Officer was told by a truck driver that he had portions of a disassembled weapon inside his backpack with the rest of the weapon located inside of his delivery truck. The driver informed the Security Officer of the contraband during a routine delivery truck search in the vehicle sally port, which is the vehicle search area for entry into the station's protected area. The truck driver was denied protected area access and he and the delivery truck were escorted off-site.

At 0850 hours on August 14, 2015, a one-hour notification was made to the NRC pursuant to 10CFR73, Appendix G, item 1(d), for an attempted introduction of contraband into a protected area.

This Licensee Event Report is being submitted pursuant to 10CFR73.71(a)(4) for a 60 day follow-up written report.

05000280/LER-2015-00127 January 201510 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(vi)
On January 27, 2015, with Units 1 and 2 operating at 100 percent power, it was identified that four sliding missile shields on the Main Steam Valve House (MSVH) were not included in the Abnormal Environmental Conditions procedure to be closed upon the threat of high winds. The shields are necessary to meet the design function of the MSVH for protection of the safety-related equipment and must be closed to perform their design function. A missile penetrating the MSVH could have prevented the MS and/or AFW systems from being able to mitigate the consequences of -an accident. Therefore, this event is reportable pursuant to 10 CFR 50.73(a)(2)(v). The shields were inappropriately excluded from the original revision of the procedure, which has now been revised to include the shields. This event posed no significant safety implications due to the low probability of missile damage inside the MSVH with the shields open. Therefore, the health and safety of the public were not affected by this event.
05000280/LER-2014-00129 March 201410 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

At 11:40 on March 29, 2014, with both Unit 1 and Unit 2 operating at 100% power, the Unit 1D service water header was declared inoperable as a result of indications received during testing. The direct cause of the indications was due to a mostly closed service water header isolation valve for the Unit 1D service water header. In October 2013, following valve replacement, the valve handwheel was re- oriented causing the valve to become mostly closed while indicating open. Therefore, the Unit 1D service water header was inoperable from October 21, 2013 until March 29, 2014 and Technical Specification limiting conditions of operation were exceeded twice during timeframes when one of two other operable service water headers was tagged out for maintenance. Also, as a result of the restricted flow condition, a service water pump that supplies cooling to a charging pump was also determined to be inoperable beyond its Technical Specification limiting conditions of operation.

  • Therefore, this report is being submitted, pursuant to 10 CFR 50.73(a)(2)(i)(B), for operations prohibited by Technical Specifications. Based on the risk assessment of this event, the risk impact was determined to be very small and, as a result, the health and safety of the public were not affected.
05000280/LER-2013-00110 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On December 6, 2012 at 11:15, with Surry Power Station Unit 1 at 100 and Unit 2 at 98 percent power, the monthly start test for Emergency Diesel Generator (EDG) 3 found the incoming voltage higher than expected. Following an unsuccessful attempt to lower voltage, the diesel was secured at 11:37. A lead associated with a relay in the voltage regulator circuit was found detached. The lead was reconnected, the generator tested satisfactorily, and EDG 3 was declared operable at 03:39 on December 7, 2012. The most probable cause was the inadvertent disconnection of the lead during removal of a data acquisition system after the previous run of EDG 3 on November 3, 2012. An evaluation determined EDG 3 could not perform its function with the lead detached. Therefore, EDG 3 was considered to be inoperable from November 3 until December 7, 2012, exceeding the Technical Specification limiting condition for operation (LCO). This report is being submitted pursuant to 10CFR50.73(a)(2)(i)(B), any operation or condition prohibited by the plant's Technical Specifications. In addition, the second train of emergency power for each unit was inoperable for testing while EDG 3 was inoperable and is reportable pursuant to 10CFR50.73(a)(2)(v)(D).

This event did not affect the health and safety of the public.

05000280/LER-2011-00110 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
at 98.3% reactor power, an automatic reactor trip occurred on Unit 1 and on Unit 2 due to the loss of offsite power resulting from damage inflicted in the switchyard from a tornado. All automatic safety systems, including Emergency Diesel Generators, performed as designed. The loss of offsite power resulted in violating several Technical Specifications including unavailability of independent offsite power. Following the unit trips, Pressurizer/Pressurizer spray temperature difference and Pressurizer heatup rate were also exceeded. A Notification of Unusual Event was declared at 1855 hours due to loss of offsite power to both emergency busses on both units. This event is reportable pursuant to 10CFR50.73(a)(2)(iv)(A) since the event resulted in automatic actuation of reactor protection systems, 10CFR50.73(a)(2)(i)(B) for operation or condition prohibited by Technical Specifications, and 10CFR73.71(a)(4) for delayed implementation of compensatory measures for loss of power to one source of surveillance equipment.
05000280/LER-2010-00121 May 2010On May 21, 2010, with Surry Power Station (SPS) Units 1 and 2 at 100% reactor power, a Virginia Electric and Power Company (Dominion) Nuclear Security Officer detected contraband in the bag of a Dominion Employee at the SPS security access control building, which is outside the protected area.5 Security noted that the employee was cooperative when stopped and unaware that the contraband was in the bag. The employee stated that the day before he had taken the contraband out of his vehicle and placed it in the side pocket of his bag. The employee stated that he packed his lunch for the next day and had forgotten to take the contraband out. There was no evidence collected in the investigation of this incident to suggest that the employee was untruthful when he stated that his acts on May 21, 2010 were unintentional and without malice. An evaluation was performed which determined that the cause of this incident was a human error due to less than adequate self-checking. This event meets the criteria specified in 10 CFR 73, Appendix G, item 1(d), as an attempted introduction of contraband into a protected area. A one-hour report Event Notification# EN45941 was made to the NRC. This Licensee Event Report is being submitted pursuant to 10 CFR 73.71(a)(4) for a 60 day follow-up written report.
05000280/LER-2009-00224 September 200910 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On September 24, 2009, with Units 1 and 2 at 100% reactor power, it was discovered that the three emergency service water (ESW) pump oil cooler outlet lines, which penetrate the pump base plates, were not sealed to prevent pump house water intrusion. The ESW pump house is designed to withstand flooding from hurricane driven tidal surges of 22.7 feet. With the pump base plates at approximately 18 feet above sea level, potential pump inoperability would occur if the water level rises above 18 feet. The cause evaluation identified that in the 1990's, the threaded interface seals on the outlet lines were no longer utilized.DThe evaluation also found the apparent cause to be inadequate procedural guidance for sealing the outlet lines.DFollowing discovery, seals were installed.DThe maintenance procedure has been strengthened to prevent recurrence.DAn evaluation determined this issue to be of very low risk significance, therefore, the health and safety of the public was not affected. This report is being submitted pursuant to 10 CFR 50.73(a)(2)(i)(B), any event or condition which was prohibited by Technical Specifications.

D

05000280/LER-1986-003, Forwards LER 86-003-00 & LER 86-002-0018 February 1986
05000280/LER-1983-068, Forwards Updated LER 83-068/03X-16 May 1983
05000280/LER-1983-020, Forwards LER 83-020/03L-06 May 1983
05000280/LER-1983-017, Forwards LER 83-017/03L-018 April 1983
05000280/LER-1983-016, Forwards LER 83-016/03L-08 April 1983
05000280/LER-1983-015, Forwards LER 83-015/03L-04 April 1983
05000280/LER-1983-014, Forwards LER 83-014/01T-023 March 1983
05000280/LER-1983-013, Forwards LER 83-013/03L-014 March 1983
05000280/LER-1983-012, Forwards LER 83-012/03L-010 March 1983
05000280/LER-1983-006, Forwards LER 83-006/03L-028 February 1983