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 Start dateReporting criterionEvent description
05000255/LER-2017-00219 May 2017
17 July 2017

On May 19, 2017, at 0206 hours, an unexpected Reactor Protection System (RPS) actuation occurred during pre-startup testing. The reactor was shutdown at the time, with all control rods inserted. The portion of the test that was in progress is designed to actuate the RPS from a loss of load input signal. To facilitate this part of the test with the reactor in a shutdown mode, one of two conditional steps in the procedure is to be taken. The generator motor operated disconnect 389 (MOD-389) is required to be in the open position, or protective trip circuity for the generator is required to be bypassed.

Due to a conditional step of the test procedure being misinterpreted by a Nuclear Control Operator (NCO), MOD-389 was left in the closed position and the generator protective trip circuity was not bypassed. This resulted in the RPS actuation occurring prior to the preplanned sequence. The RPS responded as designed. All components operated as expected for the plant conditions.

The cause of the unexpected RPS actuation was human performance errors during procedure performance, e.g., lack of self-validation/verification, misinterpretation of information, and lack of peer check verification.

Corrective actions from the event include the removal of the NCO's licensed operator qualifications until remediated and initiation of a standing order requiring peer check verification for all procedure conditional steps until the applicable administrative procedure is revised. Additionally, a case study of the event will be included in a 2017 operations high intensity training session.

05000255/LER-2017-00129 March 2017
24 May 2017

On March 29, 2017, during an evaluation of protection of Technical Specification (TS) equipment from the damaging effects of tornados, nonconforming conditions were identified in the plant design. Specifically, TS equipment did not meet current design basis for protection against potential tornado missile impact. Identified components/systems were declared inoperable and NRC Enforcement Guidance Memorandum (EGM) 15-002, "Enforcement Discretion for Tornado Generated Missile Protection Noncompliance," was implemented. Initial compensatory measures were implemented, per the guidance of NRC Interim Staff Guidance DSS-ISG-2016-01 Appendix A, within the time allowed by the applicable Limiting Conditions for Operation (LCOs) and the associated systems were then declared operable but nonconforming.

The six systems, containing TS required equipment, did not meet current design basis for protection against potential tornado missile impact. Credible tornado missile impacts could affect the following systems; Service Water, Fuel Oil, Emergency Diesel Generators, Auxiliary Feedwater, Component Cooling Water and Control Room Ventilation Filtration.

Comprehensive compensatory measures will be implemented in approximately 60 days of discovery, per the guidance of NRC Interim Staff Guidance DSS-ISG-2016-01 Appendix A.

Due to the historical nature of the issue, a specific cause for the identified vulnerabilities was not determined.

05000255/LER-2015-00116 September 201510 CFR 50.73(a)(2)(iv)(A), System Actuation

On September 16, 2015, at approximately 0117 hours, an anomaly within the digital electro-hydraulic (DEH) turbine control system initiated a turbine trip. As designed, the turbine trip actuated the reactor protection system to automatically trip the reactor due to a loss of load and the auxiliary feedwater system started automatically to recover steam generator levels.

The direct cause of the event is the turbine tripped due to actuation of the "DEH controller loss of power" turbine trip logic. Troubleshooting and analysis determined there was a failure of a power supply module on a circuit board in the DEH turbine control system. Subsequent to the power failure on the circuit board, a second failure, either a loss of power to the overspeed protection control (OPC) distributed processing units (DPUs) or a loss of communications between the primary and backup OPC DPUs, occurred resulting in an actuation of the "DEH controller loss of power" turbine trip logic.

The root cause of the event is that the design of the DEH system contains unnecessary trip logic associated with turbine overspeed monitoring. Corrective actions include a modification to remove the DEH system OPC loss of power and loss of communications trip logic.

05000255/LER-2013-00410 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On November 7, 2013, during an operating experience applicability review, a latent design deficiency was discovered. The design deficiency represents an unanalyzed condition during a postulated fire event. Potential fire induced cable faults could result in a loss of capability to safely shutdown the plant.

Palisades' station batteries contain shunts in the positive leg of output current flow. The shunts provide a voltage signal to ammeters located in the adjacent cable spreading room area. In the unlikely event of the postulated fire scenario, which is a primary fire in the cable spreading room or in a station battery room, the ammeter circuit wiring could experience fire-induced cable faults, allowing current flow greater than the rating of the wires. Current flow exceeding the rating of the wires would likely result in the wires overheating, potentially causing a secondary fire at some point along the path of the wires or causing damage to adjacent cables/wires. That is, a secondary fire could be created in an additional fire area as well as the originating fire area.

The cause of the unanalyzed condition for the postulated fire event was a failure to recognize the described failure mode and identify the fault consequences for the cables of concern during previous design reviews required for 10 CFR 50 Appendix R. Planned corrective actions to address this condition include the design and implementation of a permanent plant modification to install fuses in the ammeter indication circuits.

05000255/LER-2013-00313 August 201310 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

At 1102 on August 13, 2013, both control room ventilation filtration system trains were declared inoperable in accordance with Technical Specification (TS) 3.7.10, Condition B, due to the inability to fully close control room envelope (CRE) boundary door-15. At 1111 on August 13, 2013, door-15 was closed and TS 3.7.10, Condition B, was exited. TS 3.7.10 allows CRE boundary doors to be opened intermittently, under administrative control for preplanned activities, provided the doors can be rapidly restored to the design condition.

During preplanned maintenance activities, workers attempting to exit the CRE area were unable to open door-15 via normal operation of the door's hand wheel. Recent frequent operation of door-15 may have caused deformation of a cotter pin within the door's normal operating mechanism. Deformation of the cotter pin could cause the normal operation of door-15 to function intermittently. To allow exiting, workers opened door-15 using the emergency egress latch that activated an alarm condition on the door. During exiting, inadvertent operation of the door's hand wheel in the closed direction caused the door's latching pins to extend out causing interference between the door and the door frame preventing door-15 from fully closing.

Due to the door being in an alarmed condition, the door's latching pins were unable to be immediately retracted. After approximately nine minutes, the door's latching pins were retracted by use of the emergency egress latch and the door was restored to the design condition, i.e., closed.

The cotter pin was replaced. Future potential corrective actions include increased preventative maintenance frequency to replace the cotter pin and restricting the use of the emergency egress latch.

05000255/LER-2013-0025 May 201310 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

At 0027 on May 5, 2013, the safety injection/refueling water (SIRW) tank was declared inoperable in accordance with the operational decision-making issue (ODMI) process. Water leakage from the tank had exceeded the pre-established limit of the ODMI process that directed the tank be declared inoperable.

Leakage from the tank was quantified at approximately ninety gallons per day. Technical Specification (TS) 3.5.4.B requires restoration of an inoperable SIRW tank within one hour. If the tank is not returned to an operable status within one hour, TS 3.5.4.0 requires the plant be placed in Mode 3 within six hours and in Mode 5 within the subsequent thirty-six hours.

Due to the inability to repair the leak within the required one-hour time frame, a plant shutdown was initiated at approximately 0100 hours on May 5, 2013. The plant entered Mode 3 at 0457 hours on May 5, 2013. At 2358 hours on May 5, 2013, the plant entered Mode 5 to execute repairs.

Testing identified an approximate 3/16-inch through-wall crack in a nozzle reinforcing collar to floor plate weld of the tank. Follow-up analysis determined there was significant lack of fusion in the weld that resulted in the failure of the weld and subsequent water leakage. The welder that fabricated the weld did not ensure adequate fusion at the weld root.

The entire SIRW tank floor was replaced with the exception of an annulus ring around the perimeter.

Several initiatives were implemented to preclude potential weld issues during the fabrication of the new tank floor, including welder proficiency training on revised welding techniques and utilization of several types of weld testing methods.

05000255/LER-2013-00110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(i)(C), 50.54(x) TS Deviation

On February 10, 2013, due to a slowly lowering level trend in the component cooling water (CCW) surge tank, investigations began to identify a potential CCW leakage path. On February 14, 2013, at 2030 hours, the right train of the CCW system was declared inoperable due to the identification of an approximate 40 gallons per hour CCW leak into the service water system section of the "A" CCW heat exchanger. The "A" CCW heat exchanger is one of two essentially identical ASME Section III class 3 heat exchangers installed in the CCW system.

Technical Specification 3.7.7.A.1 requires restoration of an inoperable CCW system train within 72 hours. Due to the inability to repair the leak within the required 72 hour time frame, a plant shutdown was initiated at 1300 hours on February 15, 2013. The plant entered Mode 3 at 1649 hours on February 15, 2013. At 1111 hours on February 16, 2013, the plant entered Mode 5 to execute repairs.

The majority of CCW leakage was attributed to one tube, located in the center of the tubesheet, within the CCW heat exchanger. Very minor leakage was identified from the tube plug area of seven previously plugged tubes. Due to the inability to fully isolate CCW system flow into the heat exchanger, the failed tube could not be inspected to determine a definitive failure mechanism.

Mechanical type tube plugs were installed in the tubes where leakage was identified.

05000255/LER-2012-00210 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

On November 04, 2012, at 1115 hours, Primary Coolant System (PCS) loop 2 was declared inoperable due to the discovery of an un-isolable steam/water leak near a drain valve of an atmospheric dump valve from the "B" Steam Generator. The leak originated from a pin-hole size through-wall flaw in the socket weld on the inlet side of the drain valve. The drain valve is part of the ASME Section XI Class 2 piping system that provides steam to the turbine.

Due to the inoperable PCS loop, Technical Specification 3.4.4, Condition A, required the plant be placed in Mode 3 within six hours.

2 The plant entered Mode 3 at 1621 hours on November 4, 2012. At 1224 hours on November 5, 2012, the plant entered Mode 5 to execute repairs.

During fabrication of the socket weld in 1986, the welder did not utilize proper welding techniques to create a quality weld for the shield metal arc welding process used at that time. Lack of a quality weld resulted in a through-wall flaw. The drain valve was replaced using a gas tungsten arc welding process.

05000255/LER-2012-00110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On August 12, 2012, with the plant in Mode 3, a primary coolant system pressure boundary leak was identified in control rod drive mechanism (CRDM) number 24 upper housing assembly. Upon identification, the plant was placed in Mode 5 to effect repairs.

Initial examination, using liquid penetrant testing in the area of the leak, identified a 1/8" x 1/16" L-shaped crack indication on the outside surface of the type 316L stainless steel pipe section of the CRDM-24 upper housing assembly. Subsequent non-destructive and destructive examinations revealed a total of nine axially oriented crack indications, located in the proximity of an inside surface weld onlay. One of the nine crack indications was a through-wall crack at the leak point approximately 3" in length.

The CRDM-24 upper housing assembly was removed and replaced with an upper housing assembly of modified design. Examinations using ultrasonic testing of eight additional CRDM upper housing assemblies were performed on an area 1" below to 1-1/2" above the area of interest. No deficiencies were noted.

The direct cause for the cracking identified in CRDM-24 was transgranular stress corrosion cracking (TGSCC). TGSCC was the result of stress in the proximity of the inside surface weld onlay caused by manufacturing irregularities and misalignments between CRDM-24 upper housing assembly and supporting components. Based on the lack of crack indications in the additional eight upper housing assemblies examined, the failed CRDM-24 upper housing assembly was subject to an additional stress that has not yet been identified.

05000255/LER-2010-00310 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

On October 1, 2010, during a corrective action program extent of condition review, a postulated Appendix R fire scenario was identified in three fire areas that could potentially result in the loss of safety-related 2400 volt alternating current (VAC) bus 1C and/or bus 1D, with subsequent loss of equipment credited for Appendix R compliance to support safe shutdown in the event of such a fire. As part of the Appendix R common power supply analysis, coordination between load breakers and feeder breakers is required to protect the power supply because of a fire-generated fault on the load power cable. The fire scenario identifies how this coordination could be defeated on the safety-related 2400 VAC buses. The scenario occurs when the load breaker's control circuit is damaged by a fire which could potentially open the control circuit fuses and disable the breaker's trip circuit containing the over-current relay protection. The same fire could subsequently damage the 2400 VAC power cables, causing a cable fault. The load breaker cannot clear the fault with the trip circuit control power disabled. The clearing of the cable fault would propagate upstream to the next coordinated breaker, which would result in the bus feeder breaker opening, causing a loss of the 2400 VAC buses and associated electrical loads.

Compensatory actions taken include hourly fire watch tours and a standing order to immediately sound the site fire alarm and call out the fire brigade for a control room alarm that indicates a fire in any of the affected three fire areas.

05000255/LER-2008-00710 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident

On October 14, 2008, after completing reviews of evaluations performed by Entergy Nuclear Operations, Inc. (ENO) engineering, the Nuclear Regulatory Commission (NRC) closed an unresolved issue related to potentially non-conservative setpoints for the low suction pressure trip (LSPT) of the auxiliary feedwater (AFW) pumps. The potentially non-conservative setpoints, which were first identified on February 13. 2006, could have existed at certain Condensate Storage Tank (CST) levels and AFW pump flow rates.

The CST is the normal suction source of the AFW pumps. In the extreme unlikelihood of a tornado, a tornado-generated missile could have caused a rupture near the bottom of the CST. The rupture may have allowed rapid draining of the CST, without completely emptying the tank. Subsequent automatic operation of the AFW pumps after a plant trip could have caused the onset of vortexing within the CST, leading to air entrainment in the auxiliary feedwater suction piping and pumps. This entrained air could have rendered the AFW pumps inoperable. Consequently, the AFW system may not have been capable of supplying the steam generators with Lake Michigan water, as outlined in the Palisades Nuclear Plant design basis.

This condition is being reported in accordance with 10 CFR 50.73(a)(2)(v)(D) as a condition that could have prevented the fulfillment of the safety function of a system needed to mitigate the consequences of an accident.

05000255/LER-2008-00610 CFR 50.73(a)(2)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On October 9, 2008, Entergy Nuclear Operations, Inc. (ENO) engineering personnel completed a past operability evaluation that concluded during the 30 days between January 21, 2008, and February 19, 2008, emergency diesel generator (EDG) 1-2 would have been unable to operate satisfactorily for the EDG's required 30-day mission time. Therefore, it was inoperable. This period of inoperability corresponds to the time from when the Technical Specification (TS) surveillance test for EDG 1-2 was completed satisfactorily and ENO maintenance personnel discovered fragments of metal (broken pieces of a valve seat spring lock) in various locations throughout the valve assembly area of EDG 1-2 cylinder head, 2L.

Consequently, the required actions and associated completion times of TS 3.8.1, condition B, were not met.

Additionally, during the period EDG 1-2 was inoperable. EDG 1-1 was inoperable for approximately three hours for the performance of monthly surveillance testing. Therefore. both EDGs were simultaneously inoperable for a period of time longer than the two hours allowed by TS 3.8.1, condition E.

This occurrence is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications and 10 CFR 50.73(a)(2)(v)(D) as a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.

05000255/LER-2008-00410 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On July 15, 2008, with the plant in Mode 1 at 100% power, Entergy Nuclear Operations, Inc. personnel discovered that the Palisades Nuclear Plant region 1 spent fuel pool (SFP) storage racks contain less neutron absorber material than assumed in the SEP criticality analysis of record. This neutron absorber material is relied on to maintain the region 1 SFP storage racks within the Technical Specification (TS) 4.3.1.1.b criticality requirements. � The TS reflects credit for the neutron absorber material in maintaining SFP criticality within limits. At the time of discovery, SFP boron concentration was 2732 ppm.

� TS 4.3.1.1.b requires that Keff for region 1 fuel racks be less than or equal to 0.95 if fully flooded with unborated water.

With soluble boron required to maintain Keff less than or equal to 0.95 in the region 1 fuel racks, assuming nominal enrichment, PNP no longer complies with TS 4.3.1.1.b.

The degraded neutron absorber material did not involve an immediate safety concern at the time of discovery because the SFP boron concentration was 2732 ppm, and a SEP criticality operability assessment concluded that a soluble boron concentration of 150 ppm is required to maintain a Keff less than or equal to 0.95 in the region 1 racks. � In addition, plant procedures required that SFP boron concentration be maintained at a minimum of 2550 ppm in Modes 1 through 4. In Modes 5 and 6, 1800 ppm was required. A past operability evaluation confirmed that SFP boron concentration had been maintained greater than 2550 ppm in recent years. Compensatory measures are in place. This condition does not represent a safety system functional failure. This is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by TS.

05000255/LER-2008-00310 CFR 50.73(a)(2)(iv)(A), System Actuation

On May 23, 2008, at 1249 hours, with the plant in Mode 1 at 100% power, an actuation of the 346 generator negative sequence relay caused an actuation of the 386C coastdown lockout relay.

The 3860 relay actuation caused the main generator output breakers in the switchyard to open, causing a turbine trip, which actuated the reactor protective system to trip the reactor. As expected, the auxiliary feedwater system started automatically to recover steam generator level.

The cause of the generator negative sequence relay could not immediately be determined. The relay spuriously failed.

The relay was replaced and sent to Asea Brown Boyer' (ABB) for analysis. The problem could not be reproduced at ABB.

The event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an actuation of both the reactor protection system and the auxiliary feedwater system.

05000255/LER-2008-00210 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On March 26, 2008, with the plant in Mode 1 at 100% power, during planned maintenance on high pressure safety injection (HPSI) pump P-66A, operators experienced difficulty in removing the P-66A 2400VAC breaker 152-207 from its cubicle. A mechanism-operated cell (MOC) switch operator (bayonet) located inside the breaker cubicle was found with two broken connections, The condition of the MDC switch bayonet would have prevented operating a contact that provides a permissive to open HPSI subcooling control valve CV-3071, thereby rendering P-66A inoperable. It was concluded that the MOC switch bayonet failed when breaker 152-207 operated on January 3, 2008. The MOC switch bayonet was replaced on March 26, 2008.

The cause was determined to be that the MOC switch bayonet design is marginal for the force applied by the stored energy vacuum breaker 152-207. The contributing cause is a failure to validate that the MDC switch used during manufacturer testing matched the switches installed at the plant.

The opposite train MOC switch bayonet was inspected and no damage was found. Subsequently the MDC switch bayonets for the safety bus switchgear were inspected. Replacement of the MOC switch bayonet and others of the same type in stored energy breaker cubicles is planned.

05000255/LER-2003-00510 CFR 50.73(a)(2)(iv)(A), System Actuation

On August 14, 2003, at approximately 1607 hours EDT, with the plant operating at 100% power, an electrical power grid disturbance occurred, resulting in a momentary lowering of voltage on both 2400 volt safety related buses1C and 1D. The reduced voltage on the 2400 volt buses caused both emergency diesel generators to start. However, the 2400 volt safety related buses remained energized from offsite power throughout the event. Local grid conditions stabilized within approximately five minutes. The diesel generators were secured at 1650 hours EDT. The plant remained at full power throughout the event.

This event is reportable in accordance with 10 CFR 50.73(aX2)(iv)(A) as an automatic actuation of the emergency AC electrical power system.

05000255/LER-2003-00310 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

On March 25, 2003, at 1116 hours, with the plant in Mode 6, a loss of offsite power occurred while installing a signpost. The signpost penetrated a buried conduit, damaging a control power cable associated with both offsite power feeds. As a result, the safety-related and non-safety related buses de-energized, which caused a loss of shutdown cooling flow. The emergency diesel generators started and loaded safety-related buses, as expected. An Alert was declared at 1126 hours. Shutdown cooling -flow through the core was restored in approximately 20 minutes. The Alert was downgraded to an Unusual Event at 1231 hours. The Unusual Event was exited on March 27, 2003, at 1737 hours, when offsite power was fully restored.

This occurrence is reportable in accordance with 10 CFR 50.73(a)(2)(v)(B) as an event that prevented the fulfillment of the safety function of a system needed to remove residual heat, and in accordance with 10 CFR 50.73(a)(2)(iv)(A), as an event that resulted in automatic actuation of the emergency AC electrical power system.

NRC FORM 368 (7-2001)

05000255/LER-2003-00210 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On March 11, 2003, in conjunction with performance of fuel handling area ventilation system (FHAVS) (VG) surveillance testing prior to the 2003 refueling outage, it was determined that the FHAVS was not being tested in full accordance with the ventilation filter testing program specified by Technical Specification (TS) 5.5.10.

Review of the previous three years revealed that surveillance testing of the FHAVS specified by TS SR 3.7.12.1 had not fully met the ventilation filter testing program when the FHAVS was required to be operable during the April-May 2001 refueling outage. Pursuant to TS SR 3.0.1, failure to have met TS SR 3.7.12.1 is a failure to have met TS LCO 3.7.12 requirements for an operable FHAVS for core alterations and movement of irradiated fuel assemblies that occurred during the 2001 refueling outage. This occurrence is reportable in accordance with 10 CFR 50.73 (a)(2)(i)(B) as a condition prohibited by Technical Specifications.

The surveillance procedure was revised and the surveillance requirements successfully completed prior to entering the applicable conditions of TS LCO 3.7.12 for the 2003 refueling outage in March 2003.

05000255/LER-2003-00110 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On January 15, 2003, at 2015 hours, with the plant in Mode 1, it was determined from a review of surveillance procedure basis information, that all four steam generator (SG) reactor protection system (RPS) low-level trip setpoints in each SG were set such that the trip could occur below the allowable value specified in Technical Specification (TS) 3.3.1. The SG low-level trip setpoints were declared inoperable. It was determined that this condition had existed since 1998.

TS 3.3.1 requires four associated instrument channels, for the SG low-level RPS trip functions, to be operable in Modes 1 and 2, and in Modes 3, 4 and 5 when more than one full-length control rod is capable of being withdrawn and the primary coolant system boron concentration is less than refueling boron concentration. TS 3.3.1 does not provide a condition for four SG level instrument channels being inoperable. Therefore, TS 3.0.3 was entered. Nuclear Management Company, LLC, (NMC), requested enforcement discretion to extend the completion times in TS 3.0.3 by an additional 36 hours to avoid a plant shutdown. The Nuclear Regulatory Commission Staff verbally exercised discretion on January 16, 2003 at 0017 hours.

This occurrence is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

05000255/LER-2002-00310 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications

On December 21, 2002, it was discovered during surveillance testing, that the pipe caps for two test taps on the right channel containment hydrogen monitor instrument lines were not installed. The open test taps rendered the right channel containment hydrogen monitor inoperable. The right channel containment hydrogen monitor is believed to have been in this condition for approximately 20 months, exceeding the 30-day completion time of Technical Specification 3.3.7.A for restoring an inoperable channel of containment hydrogen monitoring to operable status. A review of the status of the left channel containment hydrogen monitor during the 20-month period that the right channel was inoperable revealed one occasion, in November 2002, during which the left channel was inoperable for approximately 9 days, exceeding the 72-hour completion time of Technical Specification 3.3.7.D for restoring one of two channels of containment hydrogen monitoring to operable status.

Upon discovery, the test tap pipe caps were reinstalled and the right channel containment hydrogen monitor was declared operable.

This occurrence is reportable in accordance with 10 CFR 50.73(a)(2)(i)(B) as a condition prohibited by Technical Specifications.

05000255/LER-2002-0021 December 200210 CFR 50.73(a)(2)(iv)(A), System Actuation

On December 1, 2002, at approximately 2154 hours, with the plant operating at 100% power, an automatic reactor trip occurred on main generator loss of load. The loss of load occurred when a transmission tower's static line hanger failed, allowing one of two static lines to contact a 345 KV transmission line, tripping the main generator. The static line also contacted the rear bus in the switchyard that supplies the plant non-1E 4160 volt startup transformers. The rear bus tripped on a fault-to-ground causing a loss of non-1E 4160 volt AC buses. Consequently, both main feedwater pumps tripped, and the auxiliary feedwater system started automatically on low steam generator level, as expected.

The plant was maintained at or near normal operating pressure and temperature subsequent to the trip, on natural circulation, since startup power for primary coolant pumps was also lost. The plant was returned to service on December 5, 2002.

This event is reportable in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an automatic reactor trip and automatic actuation of the auxiliary feedwater system.

05000255/LER-1987-017, Forwards Semiannual Radioactive Effluent Release Rept... Jan-June 1987 & Corrected Semiannual Rept for Jul-Dec 1986. LER 87-017 Also Encl Due to Corrective Action Taken Re Failure to Make Flow Rate Estimates During Release28 August 1987
05000255/LER-1986-016, Forwards LER 86-016-00 & Requests Interpretation of 10CFR50.73(a)(2)(iv) Reportability.Reportability of Event Disputed W/Region III Based on NUREG-1022,Suppl 1.Actuation of Single Component Is Not ESF Actuation6 May 1986
05000255/LER-1986-010, Withdrawn LER 86-010-00 Re Missing Pipe Hangers on Integrated Leak Rate Test Instrument Line.Results of Analysis Using ASME Code Case N-411 Revealed That Line,W/O Pipe Support,Statically Qualified17 April 1986
05000255/LER-1986-004, Forwards LER 86-004-01 Re Failure of Main Steam Safety Relief Valves to Meet as Found Acceptance Criteria30 April 1986
05000255/LER-1985-023, Forwards LER 85-023 Possible Low Temp Overpressure Protection Sys Setpoint Error. W/O Encl18 November 1985
05000255/LER-1984-023, Forwards LER 84-023-03 Re Incorrect Setpoint for Reactor Protection Sys Low Primary Coolant Flow Trip.Commitment to Determine Correct three-pump Low Flow Trip Setpoint by 850930 Delayed Until Late 1985.W/o Encl19 September 1985
05000255/LER-1984-001, Responds to NRC Re Noncompliance Noted in IE Insp Rept 50-255/84-05.Corrective Actions Addressed in LER 84-00121 May 1984
05000255/LER-1983-027, Forwards LER 83-027/01T-09 May 1983
05000255/LER-1983-026, Forwards LER 83-026/01T-09 May 1983
05000255/LER-1983-025, Forwards LER 83-025/03L-09 May 1983
05000255/LER-1983-023, Forwards LER 83-023/01T-027 April 1983
05000255/LER-1983-022, Forwards LER 83-022/01T-021 April 1983
05000255/LER-1983-021, Forwards LER 83-021/03L-021 April 1983
05000255/LER-1983-020, Forwards LER 83-020/01T-05 April 1983
05000255/LER-1983-019, Forwards LER 83-019/01T-028 March 1983
05000255/LER-1983-018, Forwards LER 83-018/03L-028 March 1983
05000255/LER-1983-017, Forwards LER 83-017/03L-028 March 1983
05000255/LER-1983-016, Forwards LER 83-016/03L-028 March 1983
05000255/LER-1983-015, Forwards LER 83-015/03L-023 March 1983
05000255/LER-1983-012, Forwards LER 83-012/03L-01 March 1983
05000255/LER-1983-011, Forwards LER 83-011/03L-028 February 1983
05000255/LER-1983-010, Forwards LER 83-010/03L-025 February 1983
05000255/LER-1983-009, Forwards LER 83-009/03L-025 February 1983
05000255/LER-1983-008, Forwards LER 83-008/01T-025 February 1983
05000255/LER-1983-007, Forwards LER 83-007/01T-017 February 1983
05000255/LER-1983-006, Informs That Safety Injection & Refueling Water Tank Support Structure Insp Will Not Be Performed for Tank in Present Partially Loaded Configuration.Insp Will Not Be Performed Until Structure in Fully Loaded Condition,Per LER 819 December 1983
05000255/LER-1983-005, Forwards LER 83-005/03L-08 February 1983
05000255/LER-1983-004, Forwards LER 83-004/03L-07 February 1983
05000255/LER-1983-003, Forwards LER 83-003/03L-07 February 1983