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 Discovered dateReporting criterionTitleEvent description
ENS 5702111 March 2024 17:37:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Manual Reactor TripThe following information was provided by the licensee via phone and email: On March 11, 2024, at 1337 EDT, with Unit 1 in Mode 1 at 35 percent power performing power ascension activities, the reactor was manually tripped due to the 'A' reactor feed pump (RFP) tripping on low suction pressure. Due to the power level at the time, the 'B' RFP had not been placed in service. Closure of containment isolation valves (CIVs) in multiple systems and actuation of high-pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. The 'B' RFP was placed in service and is controlling reactor water level. Decay heat is being removed by discharging steam to the main condenser using turbine bypass valves. Unit 2 is not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the Reactor Protection System actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The NRC resident inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the 'A' RFP is under investigation. The reactor electric plant remains in a normal lineup with both emergency diesel generators available. There were no temperature or pressure technical specification limits approached.
ENS 5698922 February 2024 17:03:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentAccident Mitigation - High Pressure Coolant Iinjection Declared InoperableThe following information was provided by the licensee via email: At 1103 CST on February 22, 2024, a potential through-wall steam leak was identified on the high pressure coolant injection (HPCI) steam supply 1-inch drain line. As a result, HPCI was declared inoperable. Since HPCI is a single-train system, this is a condition that could have prevented the fulfillment of a safety function; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). Reactor core isolation cooling (RCIC) and low pressure emergency core cooling systems (ECCS) remain operable. Additional investigation is in progress. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5697417 February 2024 13:37:0010 CFR 50.72(b)(3)(ii)(A), Seriously DegradedPrimary Containment DegradedThe following information was provided by the licensee via email and phone call: At 0837 EST, on 02/17/2024, during a refueling outage at 0 percent power while performing local leak rate testing (LLRT) on the reactor core isolation cooling (RCIC) isolation valves, which is part of the containment boundary, it was determined that the Unit 1 primary containment leakage rate did not meet 10 CFR 50 Appendix J requirements specified in Technical Specification 5.5.12. This event is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(ii)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5693629 January 2024 17:02:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram

The following information was provided by the licensee via email: At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram caused by a main turbine trip. Investigation is still ongoing. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: All control rods were fully inserted. The licensee indicated that the turbine trip may have been caused by a power load imbalance, however the cause of the incident is under investigation. The scram was not complex. Decay heat is currently being removed thru bypass valves dumping to the main condenser. Initially unit 2 lost the use of the bypass valves due to lack of condenser vacuum. Unit 2 used the high pressure coolant injection (HPCI) system in the condenser storage tank (CST) to CST mode to remove decay heat. Residual heat removal was used to keep the torus cool. Condenser vacuum was regained and unit 2 is back to removing decay heat with the turbine bypass valves. There was no impact to unit 3. The licensee confirmed there was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * *UPDATE ON 01/29/24 AT 1935 EST FROM PAUL BOKUS TO NATALIE STARFISH* * *

The following information was provided by the licensee via email: Licensee adds 8-hour non-emergency 10 CFR 50.72(b)(3)(iv)(A) specified system actuation report to original 4-hour non-emergency 10 CFR 50.72(b)(2)(iv)(B) RPS Actuation report. At approximately 1202 EST on 01/29/24, unit 2 experienced a reactor scram by a main turbine trip. All control rods inserted. Reactor core isolation cooling system (RCIC) was manually initiated for level control. HPCI was manually initiated for pressure control. Primary containment isolation system (PCIS) Group II and III isolations occurred (specified system actuation). Investigation is ongoing. The NRC Resident Inspector has been notified.

ENS 568972 November 2023 01:11:0010 CFR 50.73(a)(1), Submit an LER60 Day Notification for an Invalid Specified System ActuationThe following information was provided by the licensee via email and phone: At 2011 EDT on 11/01/23, with Unit 2 in Mode 3 at 0 percent power, Unit 2 received multiple spurious actuations. These actuations consisted of a partial group 1 and a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial Group 1 isolation resulted in the closure of two main steam isolation valves (MSIVs); all other MSIVs were already closed. The partial group 5 isolation auto closed one of the reactor water cleanup (RWCU) isolation valves. The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building secondary containment isolation valves (SCIVs). Additionally, at 2238 EDT, Unit 2 again received multiple spurious actuations. These actuations consisted of a partial group 5 primary containment isolation and a partial secondary containment isolation. The partial group 5 isolation auto closed one of the RWCU isolation valves The partial secondary containment isolation resulted in the closure of the inboard refueling floor and reactor building SCIVs. And again, at 2354 EDT, Unit 2 received spurious actuations which consisted of a partial secondary containment isolation which resulted in the closure of the inboard refueling floor and reactor building SCIVs. The spurious actuations seen on 11/1/23 are triggered at -35 inches reactor water level (RWL) for group 5 and secondary containment isolations and at -101 inches RWL for group 1 isolations. It was determined that a combination of the RWL fluctuating above and below the wide range instrument reference leg tap, the reactor vessel pressure being lowered, and reactor core isolation cooling introducing colder water conditions near the reference leg tap of the wide range instrument caused the spurious actuations. Using multiple RWL indications for each of the instances mentioned above, the actuations were confirmed to be spurious as RWL was being controlled in a band of +55 inches to +85 inches at the time of the actuations. This event is being reported in accordance with 10 CFR 50.73(a)(2)(iv)(A) as an event that resulted in an invalid actuation of a partial group 1, a partial group 5, and partial secondary containment logic. The NRC Resident has been notified.
ENS 5689618 December 2023 07:23:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System InoperableThe following information was provided by the licensee email: At 0223 EST, on 12/18/2023, while Unit 2 was at 100 percent power in mode 1, the high pressure coolant injection (HPCI) outboard steam isolation valve closed resulting in the HPCI system being declared inoperable. The cause of the outboard steam isolation valve closing is under investigation. HPCI does not have a redundant system, therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The safety function was restored at 0512, on 12/18/23, and HPCI has been declared operable. Reactor core isolation cooling (RCIC) and low pressure emergency core cooling systems (ECCS) were operable during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5688713 December 2023 07:02:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor ScramThe following information was provided by the licensee via phone and email: At 0102 CST, while operating at 100 percent (reactor) power, River Bend Station experienced an automatic reactor scram caused by a turbine trip signal. The cause of the turbine trip signal is not known at this time and is being investigated. At 0108, reactor core isolation cooling (RCIC) was initiated due to a loss of reactor feed pumps following feedwater heater string isolation. At 0114, reactor water level control was transferred back to feedwater and RCIC was secured. Reactor water level is being maintained by feedwater pumps and reactor pressure is being maintained by turbine bypass valves. The scram was uncomplicated and all other plant systems responded as designed. This event is being reported under 10 CFR 50.72(b)(2)(iv)(B), as any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical and 10 CFR 50.72(b)(3)(iv)(A) specified system actuation as result of expected post scram (reactor water) level 3 isolations and manual initiation of RCIC. No radiological releases have occurred due to this event from the unit. The NRC Senior Resident Inspector has been notified of this event. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The cause of the turbine trip, while still under investigation, was likely due to an electrical transient involving the main generator. Walkdowns in the switchyard post-scram identified damage to one of the output breaker disconnects.
ENS 568261 November 2023 10:48:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Manual Reactor Trip Due to Trip of Reactor Feed PumpThe following information was provided by the licensee via email: At 0648 EDT on 11/1/23, with Unit 2 in MODE 1 at 56 percent power, the reactor was manually tripped due to a trip of the 'B' reactor feed pump (RFP). The 'A' RFP had been previously isolated due to a leak. Closure of containment isolation valves (CIVs) in multiple systems and the actuation of high pressure coolant injection (HPCI) and reactor core isolation cooling (RCIC) occurred as a result of reaching the actuation setpoint on reactor water level as designed. The trip was not complex, with all safety systems responding normally post-trip. Operations responded and stabilized the plant. Reactor water level is being maintained with RCIC. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 1 was not affected. Due to the emergency core cooling system (ECCS) discharging into the reactor this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). Also, the reactor protection system actuation while critical is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Additionally, it is reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of CIVs, RCIC and HPCI. There was no impact on the health and safety of the public or plant personnel. The Resident Inspector was notified.
ENS 567102 September 2023 10:32:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram Due to Feedwater TransientThe following information was provided by the licensee via email: On 9/2/2023 at 0632 EDT, a feedwater transient occurred resulting in an reactor protection system (RPS) automatic reactor scram on low level (Level 3, 159.3 inches). Following the scram, reactor water level dropped below Level 2 (108.8 inches) resulting in a Group 2 recirculation sample system isolation, Group 3 traveling in-core probe (TIP) isolation valve isolation, Group 6 and 7 reactor water cleanup isolation, and Group 9 containment purge isolations. All control rods inserted as expected. High pressure core spray and reactor core isolation cooling initiated and injected as expected. ECCS systems have been secured and normal reactor pressure and level control has been established for hot shutdown. Nine Mile Point Unit 2 is stable and in Mode 3. These 4 hour and 8 hour non-emergency reports are being made in accordance with 10 CFR 50.72(b)(2) (iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident was informed. There was no impact on Unit 1.
ENS 5667310 August 2023 04:39:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor TripThe following information was provided by the licensee via email: At 0039 (EDT) on 8/10/23, with Unit 1 in Mode 1 at 100 percent power, the reactor automatically tripped during a reactor protection system (RPS) bus shift. All systems responding normally post-trip. There was no equipment inoperable at the time of the trip. Operations responded and stabilized the plant. Reactor water level being maintained via feedwater. Decay heat is being removed by cycling safety relief valves. An actuation of high-pressure core spray, division 3 diesel generator, and reactor core isolation cooling occurred during the scram and main steam line isolation closure. The reason for the auto-start was reaching Level 2 (130 inches in the reactor pressure vessel) during the transient. The systems automatically started as designed and injected to the reactor vessel when the Level 2 signal was received. The RPS actuation is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). The emergency core cooling system (ECCS) injection is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(3)(iv)(A). The ECCS actuation is being reported as a eight-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5632124 January 2023 07:21:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection InoperableThe following information was provided by the licensee via email: At 0121 CST on 01/24/2023, it was discovered that the Unit 1 High Pressure Coolant Injection System (HPCI) was inoperable; therefore, the condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. 1-FCV-073-0006B, HPCI Steam Line Condensate Outboard Drain Valve, failed closed during normal plant configuration. This valve is normally open. The HPCI steam line is not being drained with the valve in the current position. The Unit 1 Nuclear Unit Senior Operator entered Unit 1 Technical Specifications LCO 3.5.1 Condition C with required actions C.1 to immediately verify by administrative means that the Reactor Core Isolation Cooling (RCIC) system is operable and C.2 to restore HPCI to operable status in 14 days. RCIC has been verified operable by administrative means. There was no impact to the safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5611619 September 2022 06:32:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentSafety System InoperabilityThe following information was provided by the licensee via email: At 0132 CDT on September 19, 2022, River Bend Station (RBS) was operating at 100% power when the high pressure core spray (HPCS) system was declared inoperable in accordance with technical specification 3.8.9, condition E (declare HPCS and standby service water system pump 2C inoperable immediately) due to a E22-S003, HPCS transformer feeder malfunction. The HPCS is a single train system at RBS, therefore this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfilment of a safety function. The reactor core isolation cooling system has been verified to be operable. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: RBS has entered a 14-day limiting condition for operation due to the loss of HPCS and they have upgraded their on-line plant risk model to "yellow".
ENS 5605418 August 2022 01:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentSafety System Inoperability

The following information was provided by the licensee via email: At 2108 EDT on August 17, 2022 the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The Division 2 EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) room cooler and Division 2 Control Center HVAC (CCHVAC) chiller. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. At the time of the event, Division I CCHVAC was inoperable for maintenance (but was running for a maintenance run) and the event caused an inoperability of Division 2 CCHVAC. This resulted in an inoperability of both divisions of CCHVAC. Failure of the Division 2 MDCT Fan brake inverter occurred due to a trip of the DC input breaker. The breaker was reset at 2128 EDT restoring Division 2 UHS Operability. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfilment of the safety function of structures or systems that are needed to mitigate the consequences of an accident based on a loss of a single train safety system and loss of both divisions of a safety system. The Senior NRC Resident Inspector has been notified

  • * * RETRACTION ON 09/08/2022 AT 0856 EDT FROM JEFF MYERS TO MIKE STAFFORD * * *

The following information was provided by the licensee via email: On 8/17/22 at 2108 EDT the Division 2 (Div. 2) mechanical draft cooling tower (MDCT) brake inverter input breaker tripped for an unknown cause. The result of the loss of power was the inoperability of the MDCT fan brakes which impacts the ultimate heat sink (UHS) (TS 3.7.2). The UHS cascades to the EECW (emergency equipment cooling water) (TS 3.7.2) which is a support system for Div. 2 CCHVAC (Control Cell) Chiller A/C system (TS 3.7.4). This resulted in the inoperability of the Div. 2 CCHVAC Chiller. The cause for the breaker to trip is an intermittent electrical transient. Immediate corrective action was to reset the breaker, and the long-term action is to implement a modification to mitigate susceptibility to voltage variations. Div. 1 has implemented this long-term mod and no unexpected trips have occurred to date. Div. 1 CCHVAC Chiller was previously inoperable from equipment issues which was repaired, and the unit was in service for a 24-hour confidence run. Although licensed personnel had not completed the administrative actions for documenting operability during the 24-hour confidence run to monitor parameters, the (post maintenance test) PMT related to the maintenance was already completed, which included a 4-hour run in accordance with surveillance 24.413.01, Div. 1 and Div. 2 Chilled Water Pump and Valve, to verify normal operation and motor current. These PMT's were completed prior to the identified inoperability of the Div. 2 UHS due to the tripped breaker on the brake power supply. At the time of the MDCT brake inverter trip, the Operations' Senior License and the Night Shift Manager were aligned that, although still operating as part of the 24-hour confidence run, the unit was in service and capable of performing its safety function, but the administrative tasks were not completed, the Limited Condition of Operation (LCO) sheet had not been cleared, and no log entries were made. Since the Div. 1 Chiller was, in fact, operable at the time of the trip of the breaker on the inverter, this would allow the use of Technical Specification (TS) 3.0.9 'Barriers'. Per Operations Department Expectation (ODE)-12 `LCOs' (standard guidance and expectations for preparing and implementing an LCO), Operations determined that the MDCT brakes are barriers to a tornado event and TS 3.0.9 could be utilized. By invoking TS 3.0.9, as long as all other supported systems in the other division are operable, Div. 2 supported systems relying upon the UHS can remain operable and the Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) system can be used as backup to the High Pressure Coolant Injection (HPCI) system. Based on this information, there was no loss of safety function with CCHVAC A/C system or HPCI. Therefore, the NRC non-emergency 10CFR50.72(b)(3)(v)(D) report was not required and the NRC report 56054 can be retracted. The NRC Resident Inspector has been notified. Notified R3DO (Orlikowski)

ENS 5599716 July 2022 00:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (HPCI) InoperableThe following information was provided by the licensee via email: At 2020 Eastern Daylight Time (EDT) on July 15, 2022, the HPCI System was declared inoperable. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The Reactor Core Isolation Cooling (RCIC) System and Automatic Depressurization System (ADS) were operable during this time. HPCI availability was restored at 2023. Additional investigation is in-progress. There was no impact on the health and safety of the public or plant personnel. Unit 2 is not affected by this event. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: HPCI is considered inoperable but available at this time, resulting in a 14-day Shutdown LCO (Limiting Condition for Operation), due to the HPCI inoperability.
ENS 5599212 July 2022 14:17:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection InoperableThe following information was provided by the licensee via fax or email: At 0917 CDT on 7/12/2022, during the performance of U1 (Unit 1) High Pressure Coolant Injection (HPCI) rated flow test, the 1-FCV-73-19 (HPCI governor valve) failed to operate as expected. This condition results in U1 HPCI being inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). The Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) system remain operable. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. U1 entered TS LCO 3.5.1 Condition C, 14-day Shutdown LCO (Limiting Condition for Operation), due to the HPCI inoperability.
ENS 558597 March 2022 04:40:0010 CFR 50.73(a)(1), Submit an LERInvalid Actuation 60-DAY Telephone NotificationThe following information was provided by the licensee via fax or email: This 60-day telephone notification is being made in lieu of an LER submittal per 10 CFR 50.73(a)(1). This notification is made pursuant to the reporting requirements specified in 10 CFR 50.73(a)(2)(iv)(A) for invalid actuations of systems listed in 10 CFR 50.73(a)(2)(iv)(B). At approximately 0040 Eastern Standard Time (EST) on March 7, 2022, Unit 1 received inadvertent High-Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) initiation signals. Subsequently, at approximately 0148 EST on March 7, 2022, Unit 1 received inadvertent Low-Pressure Coolant Injection (LPCI) and Core Spray initiation signals. In addition, all four Emergency Diesel Generators auto started, Group 10 (Instrument Air) Primary Containment Isolation System actuations occurred, and the Residual Heat Removal (RHR) Service Water Booster pumps tripped resulting in a brief interruption (approximately 9 minutes) to the Shutdown Cooling (SDC) heatsink. Jumpers, installed per planned refueling outage activities, prevented discharge of Emergency Core Cooling Systems into the reactor. HPCI, RCIC, and RHR Loop `A' were removed from service and under clearance. RHR SDC remained operable via RHR Loop `B' and forced circulation was maintained in the reactor. At the time of these events, Unit 1 was shutdown for refueling and the `A' and `C' reactor water level transmitters had been isolated in preparation for planned replacement. Leak-by of the instrument isolation valves occurred on both transmitters. Leak-by on the `C' instrument occurred at a faster rate with the `A' instrument providing the confirmatory signals resulting in Low Level 2 (LL2) and Low Level 3 (LL3) indication at approximately 0040 EST and 0148 EST, respectively. All actuations occurred as designed for LL2 and LL3 signals. During these events, reactor water level remained stable at the Reactor Vessel Head Flange and the `B' and `D' reactor water level transmitters remained off-scale-high, as expected under these conditions. Therefore, the actuations were not initiated in response to actual plant conditions, it was not an intentional manual initiation, and there were no parameters satisfying the requirements for initiation of the system (i.e., there was no low reactor water level condition). Considering the above, these actuations were invalid. There was no impact on the health and safety of the public or plant personnel.
ENS 558215 April 2022 06:23:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Scram on LOW LevelThe following information was provided by the licensee via telephone and email: On 4/5/2022, at time 0223, during maintenance on Feedwater Level Control Valve 2FWS-LV10B, a Feedwater transient occurred resulting in an RPS Automatic Reactor Scram on Low Level (Level 3, 159.3 inches). Following the scram, reactor water level dropped below Level 2 (108.8 inches) resulting in a Group 2 Recirculation Sample System Isolation, Group 3 TIP ((Traversing Incore Probe)) Isolation Valve Isolation, Group 6 and 7 Reactor Water Cleanup Isolation and Group 9 Containment Purge Isolations. All control rods inserted as expected. High Pressure Core Spray and Reactor Core Isolation Cooling initiated and injected as expected. ECCS Systems have been secured and normal reactor pressure and level control has been established for hot shutdown. Nine Mile Point Unit 2 is stable in Mode 3. These 4 hour and 8-hour non-emergency ENS ((Emergency Notification System)) reports are being made in accordance with 10 CFR 50.72(b)(2)(iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). The NRC Resident was informed. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: There was no impact on Unit 1.
ENS 5578010 March 2022 01:13:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (HPCI) Inoperable

The following information was provided by the licensee: At 2013 EST on March 9, 2022, the HPCI System was declared inoperable following evaluation of routine HPCI surveillance testing data indicating that the required response time for reaching rated conditions was not met. Therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The Reactor Core Isolation Cooling (RCIC) System and Automatic Depressurization System (ADS) are operable. There was no impact on the health and safety of the public or plant personnel. Investigation is in-progress to determine the cause. Unit 1 is not affected by this event. Unit 1 is in a refueling outage. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 05/04/22 AT 1135 EDT FROM CHARLIE BROOKSHIRE TO DAN LIVERMORE * * *

The following information was provided by the licensee via email: At 20:13 EST on March 9, 2022, the HPCI System was declared inoperable following evaluation of routine HPCI surveillance testing data indicating that the required response time for reaching rated flow and pressure was not met. Subsequent to this, it was determined that the required response time was overly conservative for assuring the safety function of the system could be fulfilled. The required response time was revised. The operability determination for this event has been updated indicating that system operability was never lost for this event. There was not a condition that could have prevented the system from fulfilling the safety function. The NRC Resident Inspector has been notified. Notified R2DO (Miller).

ENS 556821 January 2022 17:10:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray System Declared Inoperable

The Licensee provided the following information via fax: During performance of a surveillance of the High Pressure Core Spray (HPCS) service water system on January 1, 2022, the HPCS system was declared inoperable for performance of the surveillance. During the surveillance, pump discharge pressure and flow were above the action range curve specified in the surveillance. For the given flow rate, pump discharge pressure was too high. This condition prevents declaring the HPCS service water system and HPCS system operable. The HPCS service water and HPCS systems remain inoperable. The station entered Technical Specification (TS) 3.7.2.A and TS 3.5.1.B at 0910 (PST) on January 1, 2022. In accordance with TS 3.5.1.B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. TS 3.5.1 Action B provides a 14-day completion time to restore HPCS to an operable status. All other Emergency Core Cooling systems (ECCS) are operable. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The HPCS system is a single train system at Columbia. The NRC resident has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: The licensee is investigating the cause of the high pump discharge pressure and verifying instrumentation accuracy.

  • * * RETRACTION ON 1/6/22 AT 1715 EST FROM CHASE WILLIAMS TO TOM KENDZIA * * *

This Notification is to retract EN 55682, Unplanned High Pressure Core Spray (HPCS) Inoperability. On 1/1/2022 at (1735 EST), Columbia Generating Station notified the NRC under 10 CPR 50.72(b)(3)(v)(D) of the inoperability of a single train of safety system (HPCS) for performance of the surveillance. During the surveillance pump discharge pressure and flow were above the action range curve specified in the surveillance. Engineering performed an analysis of this event and concluded the HPCS was operable during the event and would have performed its required safety function. The results of initial IST testing of HPCS-P-2 via OSP-SW/IST-Q703 on 01/01/22 resulted in measured parameters falling outside of the acceptable range specified for this pump. Systematic error was suspected as the cause of the failure and the test was reperformed following taking actions to eliminate the suspected systematic errors. The second performance of the test on 01/01/22 resulted in acceptable pump performance. Evidence exists that the initial performance of the test failed due to imprecise averaging techniques due to difficulties in averaging continuously changing values on the test instrument. The second performance of OSP-SW/IST-Q703 should be considered a successful test and the test of record as the systematic error was eliminated and measured parameters are considered valid. The NRC Resident Inspector has been notified. The HOO notified R4DO (Rolando-Otero).

ENS 555583 June 2021 06:41:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Inoperable Due to LOW Level InstrumentationAt 0241 (EDT) on June 3, 2021, during performance of a High Pressure Coolant Injection (HPCI) Condensate Storage Tank (CST) level functional surveillance, the HPCI torus suction inboard isolation valve was slow to open during swap of suction from the CST to the Torus. On June 9, 2021, it was determined that as a result of the June 3, 2021, slow swap condition, TS 3.3.5.1 Required Action D.1 to declare HPCI inoperable within 1 hour was applicable due to inoperable CST low level instrumentation channels. At 1817 (EDT) on June 3, 2021, HPCI suction was swapped to the torus, making TS Required Action D.1 no longer applicable. Reactor Core Isolation Cooling (RCIC) was available throughout this condition. At 0900 (EDT) on November 3, 2021, it was determined that an NRC event report due to HPCI inoperability should have been made. This event is being reported as a late 8-hour non-emergency notification pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The cause of the slow valve opening was later determined to be corrosion products on contacts of a relay in the CST low level instrumentation logic. On June 4, 2021 at 1451 (EDT), the HPCI CST Level Functional Test was completed Satisfactorily, restoring HPCI Instrumentation to Operable. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 554519 September 2021 05:33:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Spray InoperableAt 0033 CDT on September 9, 2021, Grand Gulf Nuclear Station (GGNS) was operating at 70 percent power when the High Pressure Core Spray (HPCS) was declared inoperable. The inoperability determination was made due to control room annunciations. In accordance with GGNS Technical Specification 3.5.1.B.1, the Reactor Core Isolation Cooling system was verified to be operable. Troubleshooting is in progress. This event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition which could have prevented the fulfillment of a safety function. The NRC Resident Inspector has been notified.
ENS 554488 September 2021 05:59:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentUnit 1 High Pressure Coolant Injection (HPCI) System InoperableAt 0159 EDT on 09/08/2021, the HPCI pump discharge valve failed to reopen during a valve surveillance, resulting in the HPCI system being declared INOPERABLE. HPCI does not have a redundant system; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v). Reactor Core Isolation Cooling system and low pressure Emergency Core Cooling Systems were OPERABLE during this time. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5542322 August 2021 09:29:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHPCI Declared InoperableAt 0529 EDT on August 22, 2021, HPCI ((High Pressure Coolant Injection System)) was declared inoperable due to receiving the HPCI Inverter Circuit Failure annunciator. The cause of the annunciator was a fuse failure. The cause of the fuse failure is unknown at this time and is under investigation. Concurrent with the HPCI fuse failure was a similar fuse failure within the Division 2 EDG ((emergency diesel generators)) Load Sequencer which renders the Division 2 EDGs inoperable. Relation to the HPCI issue is unknown and is part of the investigation. The RCIC ((Reactor Core Isolation Cooling System)) was verified operable per Tech Spec 3.5.1 E.1. In addition, offsite circuits were verified operable per Tech Spec 3.8.1.B. Division 1 EDGs remain operable. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. There was no impact on the health and safety of the public or plant personnel. The Senior NRC Resident Inspector has been notified.
ENS 553943 August 2021 14:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor TripAt 1026 EDT on 8/3/21, with Unit 1 in MODE 1 at 100 percent power, the reactor automatically tripped due to low reactor water level. The low reactor water level condition was due to a loss of both reactor feed pumps. The cause of the loss of feed pumps is under investigation. Additionally, the low reactor water level resulted in the automatic actuation of High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) systems, and Containment Isolation Valves (CIVs) in multiple systems. All safety systems responded normally. Operations responded and stabilized the plant. Reactor water level is being maintained via RCIC system. Decay heat is being removed by discharging steam to the main condenser using the turbine bypass valves. Unit 2 is not affected. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). It is also reportable under 10 CFR 50.72(b)(3)(iv)(A) as an event that results in a valid actuation of the HPCI and RCIC systems and CIVs. There was no impact on the health and safety of the public or plant. The Licensee notified the NRC Resident Inspector. The Unit will proceed to Mode 4 while the cause of the loss of feed pumps is under investigation.
ENS 5522430 April 2021 03:54:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (Hpci) Declared InoperableOn 4/29/21 at 2354 (EDT), an alarm was received for U2 HPCI Inverter Power Failure. (It was) identified that the High Pressure Coolant Injection (HPCI) flow controller had lost power due to a failure of an inverter. Without the flow controller, HPCI would not auto start to mitigate the consequences of an accident; thus, HPCI was declared inoperable. All other emergency core cooling systems and reactor core isolation cooling (RCIC) system remain operable. HPCI is a single train system with no redundant equipment in the same system; therefore, this failure is reportable as an event or condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident per 10CFR50.72(b)(3)(v)(d). The NRC Resident has been informed of this notification.
ENS 5482610 August 2020 17:58:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationNotice of Unusual Event Due to Loss of Offsite Power Due to High Winds

At 1258 CDT on August 10, 2020, Duane Arnold Energy Center declared an Unusual Event due to a loss of offsite power due to high winds. The event at the single unit plant resulted in an automatic scram from 82 percent power (Mode-1) to zero percent power (Mode-3). They are headed to Mode-4. There is damage on site, but the Reactor Building is intact. All rods inserted and cooling is being addressed via Reactor Core Isolation Cooling (RCIC) for level control and Safety Relief Valves are removing decay heat to the torus. Both Standby Diesel Generator are running. The licensee notified the NRC Resident Inspector, the Iowa Department of Emergency Management, and the Linn County and Benton County Emergency Management agencies. Notified DHS SWO, FEMA Operations Center, CISA Central, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE ON 08/10/2020 AT 1554 EDT FROM CURTIS HANSEN TO OSSY FONT * * *

This report is being made under CFR 50.72 (b)(2)(iv)(B) for an automatic reactor scram due to loss of offsite power due to high winds. In addition, this report is being made under CFR 50.72 (b)(3)(iv)(A) and (B) due to PCIS ((Primary Containment Isolation System)) Groups 1, 2, 3, 4 and 5 (activating) due to loss of offsite power. All isolations went to completion. RCIC injecting for level control. All rods fully inserted during the scram. The plant electrical line up is both SBDGs (Standby Diesel Generators) are running. Decay heat is being removed via SRVs (Safety Relief Valves) to the torus. Progress towards shutdown cooling. NRC Senior Resident (Inspector) notified at 1448. Notified R3DO (Pelke).

ENS 548124 August 2020 03:12:0010 CFR 50.72(a)(1)(i), Emergency Class DeclarationUnusual Event Declared Due to a Loss of Offsite Power

At 2312 EDT, on August 3, 2020, Brunswick Unit 1 declared an Unusual Event due to a loss of offsite power. The unit was at approximately 20 percent power and was not synced to the grid when the unit automatically scrammed. All control rods fully inserted. Emergency Diesel Generators started and began powering the safety buses. Safety systems actuated as expected. The Unit also experienced a loss of Fuel Pool Cooling and Cleanup System, but one pump was returned to service. Unit 2 remains at 100 percent power and is unaffected. The licensee notified State and local governments, as well as the NRC Resident Inspector. Notified DHS SWO, FEMA Operations Center, CISA IOCC, FEMA NWC (email), DHS Nuclear SSA (email), and FEMA NRCC SASC (email).

  • * * UPDATE FROM MARK TURKAL TO DONALD NORWOOD AT 0120 EDT ON 8/4/2020 * * *

At approximately 2302 EDT, a loss of offsite power occurred on Unit 1. This resulted in a Reactor Protection System (RPS) actuation. Per design, emergency diesel generators 1 and 2 properly started and loaded to their respective emergency buses. The Reactor Core Isolation Cooling (RCIC) system was manually started and is being used to control reactor water level. The High Pressure Coolant Injection (HPCI) system was manually started and is being used for pressure control. As previously reported, an Unusual Event was declared at 2312 EDT due to the loss of offsite power. At the time of the event, Unit 1 was in the process of shutting down for maintenance associated with a ground on the main generator. Due to the RPS actuation while critical, this event is being reported as a four-hour, nonemergency notification per 10 CFR 50.72(b)(2)(iv)(B). As a result of the reactor trip, reactor water level reached low level 1 (LL1). The LL1 signal causes a Group 2 (i.e., floor and equipment drain isolation valves), Group 6 (i.e., monitoring and sample isolation valves) and Group 8 (i.e., shutdown cooling isolation valves) isolations. The LL1 isolations occurred as designed; the Group 8 valves were closed at the time of the event. Per design, the loss of offsite power also caused a Group 1 (i.e., main steam isolation valve) isolations. Due to the Emergency Diesel Generator and Primary Containment Isolation System (PCIS) actuations, this event is also being reported as an eight-hour, nonemergency notification in accordance with 10 CFR 50.72(b)(3)(iv)(A). Unit 2 was not affected. There was no impact to the health and safety of the public or plant personnel. The safety significance of the event is minimal. All safety related systems operated as designed. Investigation of the cause of the loss of offsite power is in progress. The licensee notified the NRC Resident Inspector. Notified R2DO (Inverso).

  • * * UPDATE ON 8/4/2020 AT 1534 EDT FROM JOSEPH ELKINS TO ANDREW WAUGH * * *

At 1454 EDT on August 4, 2020, the Unusual Event was exited when offsite power was restored to Unit 1. Per design, when the loss of offsite power to Unit 1 occurred, all four emergency diesel generators (EDGs) started and EDGs 1 and 2 properly suppled emergency buses 1 and 2. Since Unit 2 was not affected by the loss of power, EDGs 3 and 4 ran unloaded. With restoration of offsite power to Unit 1, EDG 2 has been secured. EDGs 1, 3, and 4 are being secured as required by plant operating procedure. Notified R2DO (Inverso), NRR EO (Miller), IRD MOC (Grant), DHS SWO, FEMA OC, DHS NICC WO, CISA IOCC (email), DHS SWO (email), FEMA NWC (email), FEMA Ops Center (email), FEMA-NRCC-sasc (email), NRCC THD Desk (email), NuclearSSA (email). ********************************************************************************************************************************

ENS 546913 May 2020 12:21:0010 CFR 50.72(b)(2)(iv)(B), RPS System ActuationAutomatic Reactor Scram Due to Main Turbine TripAt 0821 EDT on May 3, 2020, the Susquehanna Steam Electric Station Unit 1 reactor automatically scrammed due to a trip of the Main Turbine. The Unit 1 reactor was operating at 76 percent reactor power following a ramp schedule to full power subsequent to a maintenance outage. The Control Room received indication of a Main Turbine trip with both divisions of the Reactor Protection System actuated and all control rods inserted. The Reactor Recirculation Pumps tripped on End of Cycle - Recirculation Pump Trip. Reactor water level lowered to -1 inch causing Level 3 (+13 inches) isolations. No Emergency Core Cooling System or Reactor Core Isolation Cooling actuations occurred. The operations crew subsequently maintained reactor water level at the normal operating band using Reactor Feed Water. No Steam Relief Valves opened. The reactor is currently stable in Mode 3. Investigation into the trip of the Main Turbine is in progress. The NRC Resident Inspector was notified. A voluntary notification to the Pennsylvania Emergency Management Agency and press release will occur. This event requires a 4-hour Emergency Notification System (ENS) notification in accordance with 10 CFR 50.72(b)(2)(iv)(B) and an 8-hour ENS notification in accordance with 10 CFR 50.72(b)(3)(iv)(A) and 10 CFR 50.72(b)(3)(iv)(B).
ENS 5429225 September 2019 06:38:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentLoss of High Pressure Core Spray SystemAt 2338 PDT on September 24, 2019, the High Pressure Core Spray (HPCS) system was declared inoperable due to a leak on DSA-PCV-2C (2 inch Diesel Starting Air Pressure Control Valve). With one of two air headers isolated and being drained for maintenance, this leak caused the remaining starting air header for HPCS-GEN-DG3 (HPCS Diesel Generator) to lower to less than the operability limit. Upon declaring the HPCS system inoperable, TS 3.5.1 Action B was entered. In accordance with Action B, the Reactor Core Isolation Cooling (RCIC) system was verified to be operable. Action B provides a 14 day completion time to restore HPCS to an operable status. All other Emergency Core Cooling Systems (ECCS) were operable during this event. This event is being reported as an event or condition that could have prevented the fulfillment of a safety function credited for mitigating the consequences of an accident per 10 CFR 50.72(b)(3)(v)(D). The HPCS system is a single train system at Columbia. The leak was isolated and starting air header pressure restored to the HPCS diesel generator at 0104 PDT on September 25, 2019, and all associated Technical Specifications were exited. The NRC Resident Inspector was notified.
ENS 541983 August 2019 23:47:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Trip and Manual Actuation of Reactor Core Isolation CoolingAt 1947 (EDT) on 8/3/19, with Hope Creek in Mode 1 at 37 percent power, the reactor was manually scrammed due to loss of condenser vacuum. All control rods fully inserted into the core. All safety systems responded as designed and expected. Reactor level was stabilized using Reactor Core Isolation Cooling (RCIC) and Reactor Feedwater Pumps. Currently reactor water level is being maintained by the feedwater system and decay heat is being removed by the main condenser using the main turbine bypass valves. Due to the Reactor Protection System actuation while critical, this event is being reported as a four-hour, non-emergency notification per 10 CFR 50.72(b)(2)(iv)(B). Due to the manual actuation of RCIC, this event is also being reported as an eight-hour, non-emergency notification per 10 CFR 50. 72(b )(3)(iv)(A). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified. The plant is in its normal shutdown electrical lineup with all safe shutdown equipment available. The licensee will be notifying the state of Delaware, state of New Jersey and the Lower Alloway Creek township.
ENS 541973 August 2019 07:26:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
En Revision Imported Date 8/7/2019

EN Revision Text: AUTOMATIC REACTOR SCRAM ON LOW REACTOR WATER LEVEL At 0226 (CDT), an automatic scram on low reactor water level occurred due to a trip of the 'B' Reactor Feed pump. All control rods fully inserted. Reactor water level 2 was reached and the High Pressure Core Spray system, Reactor Core Isolation Cooling system, Division 3 diesel generator, Standby Gas Treatment Systems 'A' and 'B' and all shutdown safety related service water pumps started as expected. Reactor Core Isolation Cooling and High Pressure Core Spray injected as expected. All level 2 containment isolation signals occurred as expected and all level 2 containment valves closed as expected. Reactor water level is currently being controlled in band by condensate. Reactor pressure is being maintained by main turbine Bypass Valves. This event is being reported under 10 CFR 50.72(b)(2)(iv)(A), for ECCS discharge to RCS; 10 CFR 50.72(b)(2)(iv)(B), for RPS actuation, and 10 CFR 50.72(b)(3)(iv)(A), for specified system actuation. The NRC Senior Resident Inspector has been notified. No safety relief valves lifted during the transient. The plant is in a normal shutdown electrical lineup with all safety equipment available. The licensee notified the Illinois Emergency Management Agency per their communications protocol.

  • * * UPDATE FROM DAVID LIVINGSTON TO HOWIE CROUCH AT 0321 EDT ON 8/4/19 * * *

Following automatic initiation of the High Pressure Core Spray (HPCS) System as described above, the HPCS System was manually secured following station procedures after verification that additional RPV (reactor pressure vessel) injection was no longer required. Securing HPCS injection in this manner prevents automatic restart of the system in the event of a subsequent low RPV level condition, rendering it inoperable. As the HPCS system is considered a single train safety system, this meets the reportability requirements of 10 CFR 50.72(b)(3)(v)(D). This reportable condition was identified following review of post-scram actions. The HPCS system has been restored to a Standby lineup. The licensee will be notifying the NRC Resident Inspector. Notified R3DO (Pelke).

  • * * UPDATE FROM JAMES FORMAN TO KERBY SCALES AT 1545 EDT ON 8/6/19 * * *

Following the scram, the Primary Containment to Secondary Containment and the Drywell to Primary Containment differential pressure limits were exceeded. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.6.1.4, Primary Containment Pressure, and 3.6.5.4, Drywell Pressure, Actions A.1, B.1, and B.2 were entered. Primary Containment to Secondary Containment differential pressure and Drywell to Primary Containment differential pressure were restored to within the LCO limits at 1505 on 8/3/19 and the associated TS Actions were exited. This event is reportable under 10 CFR 50.72(b)(3)(ii)(B) as an unanalyzed condition that could have prevented the fulfillment of the primary containment function due to being outside the initial conditions to ensure that drywell and containment pressures remain within design values during a loss of coolant accident. This event is also reportable under 10 CFR 50.72(b)(3)(v)(C) as an event or condition that could have prevented the fulfillment of the drywell and primary containment functions to control the release of radioactive material for the same reason. The licensee notified the NRC Resident Inspector. Notified R3DO (Pelke).

ENS 5411613 June 2019 01:27:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (Hpci) InoperableAt 2127 EDT on June 12, 2019, during routine testing, the HPCI turbine experienced an overspeed trip and then subsequently restarted and ramped to the required speed. As a result, the response time of the system exceeded the 60-second acceptance criteria, thereby rendering the system inoperable. This condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The Reactor Core Isolation Cooling (RCIC) System and Automatic Depressurization System (ADS) are operable. The safety significance of this event is minimal. Troubleshooting activities are in progress. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 541025 June 2019 04:00:0010 CFR 21.21(d)(3)(i), Failure to Comply or Defect
10 CFR 21.21(a)(2), Interim Report for Comply or Defect in Component
En Revision Imported Date 10/14/2019

EN Revision Text: PART 21 INTERIM NOTIFICATION - FAILURE OF A SIGNAL CONVERTER SUPPLIED TO COOPER NUCLEAR PLANT The following is a summary of the information received from Engine Systems, Inc. via facsimile: ESI was notified on April 6, 2019 that a signal converter (also called a signal conditioner) that sends the Reactor Core Isolation Cooling turbine speed to the turbine controller had failed. The converter is at the manufacturer's facility undergoing testing at this time and they have been unable to complete their evaluation within 60-days. The evaluation is expected to be completed by July 31, 2019. The converter was only supplied to Cooper Nuclear Plant.

  • * * UPDATE FROM DAN ROBERTS TO DONALD NORWOOD AT 1710 EDT ON 7/19/2019 * * *

The following is a synopsis of information received via facsimile: On June 5, 2019, Engine Systems, Inc. (ESI) issued an interim report regarding an identified deviation for which ESI was unable to complete an evaluation within the 60-day requirement. Per the interim report, ESI committed to complete the evaluation by July 31, 2019. The evaluation is now complete and the deviation is determined to be reportable in accordance with 10 CFR Part 21. ESI supplied the component which failed to comply or contained a defect. That part was a Signal Converter Transmitter, P/N SCT/4-20MA/4-20MA/24DC/-LIM-TA(DCM). This component was only supplied to Cooper Nuclear Station. The nature of the defect was that a power inverter transformer, internal to the signal converter transmitter, failed shorted. The transformer failure adversely affected other circuit board mounted components which prevented the device from functioning properly. The signal converter transmitter is a component of a turbine control panel. Within the panel, the transmitter is used to sense the customer's remote speed setpoint input signal and convert the signal which is transmitted to the turbine control. Since the signal converter transmits the customer's remote speed setpoint input to the turbine control, operability of the device is critical to operation of the RCIC turbine control system. Therefore, a failure of the signal converter would adversely affect the RCIC turbine control system and thus may affect the safe shutdown of the reactor. At Cooper Nuclear Station, the failed component has been removed and replaced with a spare transmitter from a different batch. No further action is necessary. For ESI, the previous design transformer (used in the failed transformer) was discontinued by the transformer manufacturer in 2016 which required the signal converter transmitter manufacturer to source a new transformer. The new transformer has the same functionality with a slightly different form factor which minimizes the potential for common cause failure with the original style transformer. Therefore, no additional actions are required since a different transformer is in current use. ESI has included a verification of the current transformer design in the commercial grade dedication package. The names and addresses of the individuals reporting this information are: John Kriesel Engineering Manager Engine Systems, Inc.; 175 Freight Rd. Rocky Mount, NC 27804 Dan Roberts Quality Manager Engine Systems, Inc.; 175 Freight Rd. Rocky Mount, NC 27804 Notified R4DO (Proulx) and the Part 21/50.55 Reactors E-mail group.

  • * * UPDATE FROM DAN ROBERTS TO DONALD NORWOOD AT 1643 EDT ON 10/11/2019 * * *

The following is a synopsis of information received via facsimile: Subsequent to the issue of the report on July 19, 2019, ESI became aware of another potential defect with the same device. As a result, ESI has amended the report to expand the extent of condition. ESI supplied the component which failed to comply or contained a defect. That part was a Signal Converter Transmitter, P/N SCT/4-20MA/4-20MA/24DC/-LIM-TA(DCM). This component was only supplied to Cooper Nuclear Station. The nature of the defect was that four circuit board mounted components (two transistors, a capacitor, and a diode) failed, causing the device to go to zero output. These prevented the device from functioning properly. Corrective actions for Cooper Nuclear: As stated above, no further action is necessary. Corrective actions for ESI for the subsequent failure: ESI has been unable to positively determine the root cause; however, correspondence with the signal converter manufacturer indicates this may be related to the previous style transformer. While no anomalies were detected with the transformer, the failed components are electrically connected to the transformer. Verification of the current style transformer is performed in the commercial grade dedication package. The names and addresses of the individuals reporting this information are: John Kriesel Engineering Manager Engine Systems, Inc.; 175 Freight Rd. Rocky Mount, NC 27804 Dan Roberts Quality Manager Engine Systems, Inc.; 175 Freight Rd. Rocky Mount, NC 27804 Notified R4DO (Kellar) and the Part 21/50.55 Reactors E-mail group.

ENS 540961 June 2019 04:45:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram Due to Low Reactor Water Level

At 2345 CDT at River Bend Station (RBS) Unit 1, a manual Reactor scram was inserted in anticipation of receiving an automatic Reactor Water Level 3 (9.7") scram due to the isolation of the 'B' Heater String with the 'A' Heater String already isolated. The 'B' heater string isolation caused loss of suction and subsequent trip of the running Feed Water Pumps 'A' and 'C'. All control rods fully inserted with no issues. Subsequently Reactor level was controlled by the Reactor Core Isolation Cooling (RCIC) system. Feed Water Pump 'C' was restored 4 minutes after the initial trip and the RCIC system secured. Currently RBS-1 is stable and is being cooled down using Turbine Bypass Valves. No radiological releases have occurred due to this event from the unit. The plant is currently under a normal shutdown electrical lineup. The licensee notified the NRC Resident Inspector.

  • * * UPDATE AT 1603 EDT ON 6/10/19 FROM ALFONSO CROEZE TO JEFF HERRERA * * *

This amended event notification is being made to provide additional information that was not included in the original notification made on 6/1/19 at 0315 EDT. This event was reportable under 10 CFR 50.72(b)(3)(iv)(A) which was not annotated or described in the original report. Forty-two minutes after the Feed Water Pump 'C' was started, the pump tripped causing a Reactor Water Level 3 (9.7") RPS actuation. Feed Water was restored five minutes later using the Feed Water Pump 'A'. The NRC Resident Inspector has been notified. Notified the R4DO (Warnick).

ENS 5394217 March 2019 12:35:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEn Revision Imported Date 4/24/2019

EN Revision Text: HIGH PRESSURE COOLANT INJECTION SYSTEM DECLARED INOPERABLE At 0735 CDT on March 17, 2019, the High Pressure Coolant Injection (HPCI) system was isolated due to a water-side leak from the HPCI Gland Seal Condenser. Unit 3 declared the HPCI system Inoperable and entered Technical Specification LCO 3.5.1 Condition C with required actions to verify the Reactor Core Isolation Cooling system is Operable, and to restore the HPCI system to Operable status within 14 days. All other Unit 3 Emergency Core Cooling Systems (ECCS) remain Operable. This condition is being reported pursuant to 10 CFR 50.72(b)(3)(V)(D), 'Any event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident.' This is also reportable as a 60-day written report in accordance with 10 CFR 50.73(a)(2)(V)(D). There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified of this event.

  • * * RETRACTION FROM WESLEY CONKLE TO HOWIE CROUCH ON 4/23/19 AT 1549 EDT * * *

ENS Event Number 53942, made on March 17, 2019, is being retracted. NRC Notification 53942 was made to ensure that the Eight-Hour Non-Emergency reporting requirements of 10 CFR 50.72 (b)(3)(v)(D) were met when the licensee discovered an event, that at the time of discovery, could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident. At 0735 CDT, on March 17, 2019, during the performance of a routine surveillance, a momentary pressure transient of 844 psig from the Feedwater system was introduced into the High Pressure Coolant Injection (HPCI) system discharge and suction piping that ruptured the seal on the gland seal condenser and flooded the U3 HPCI Room. Unit 3 HPCI was declared inoperable due to isolation of the waterside of the HPCl system. On April 11, 2019, a Past Operability Evaluation was completed which determined that the HPCI System remained operable. The evaluation of the potential pressure transient and room flooding concluded that the HPCI System could have performed its specified safety function of vessel injection throughout the time that the gland seal was ruptured. Therefore, this event is not reportable under 10 CFR 50.72(b)(3)(v)(D). TVA's evaluation of this event is documented in the Corrective Action Program in Condition Report 149973. The licensee has notified the NRC Resident Inspector. Notified R2DO (Ehrhardt).

ENS 5392310 March 2019 04:59:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Scram Resulting in Rps and Eccs ActuationAt 2259 CST on 3/9/2019, Browns Ferry Unit-3 received an automatic SCRAM on Main Generator Breaker Failure and Turbine Load Reject. Unit-3 declared a Notification of Unusual Event SU1 for loss of offsite AC power to Unit-3 specific 4kV Shutdown Boards for greater than 15 minutes. Primary Containment Isolation Systems (PCIS) Groups 1, 2, 3, 6, and 8 isolation signals were received. Upon receipt of these signals, all required components actuated as required. Main steam relief valves lifted on the initial transient. High Pressure Coolant Injection (HPCI) and Reactor Core Isolation Cooling (RCIC) initiated on low reactor water level. HPCI remains in service for reactor level and pressure control. RCIC is not in service at this time, the station is investigating low flow from the pump. All four Unit-3 Diesel Generators started and loaded as expected. Residual Heat Removal System is in service for suppression pool cooling. 4kV Station Unit Boards have been restored from the 161kV system. Actions are in progress to restore 4kV Shutdown Boards to offsite power. This event is reportable within 1 hour in accordance with 10 CFR 50.72(a)(1)(i) for declaration of the Licensees Emergency Plan. Complete as documented on EN 53922. This event requires a 4 hour report per 10 CFR 50.72(b)(2)(iv)(B), 'Any event or condition that results in actuation of the reactor protection system (RPS) when the reactor is critical except when the actuation results from and is part of a pre-planned sequence during testing or reactor operation.' This event also requires an 8 hour report per 10 CFR 50.72(b)(3)(iv)(A). 'Any event or condition that results in valid actuation of any of the systems listed in paragraph (b)(3)(iv)(B), (1) Reactor protection system (RPS) including: reactor scram or reactor trip, (2) General containment isolation signals affecting containment isolation valves in more than one system or multiple main steam isolation valves (MSIVs), (4) ECCS (Emergency Core Cooling System) for boiling water reactors (BWRs) including: core spray systems; high-pressure coolant injection system; low pressure injection function of the residual heat removal system, (5) BWR reactor core isolation cooling system; isolation condenser system; and feedwater coolant injection system, and (8) Emergency AC electrical power systems, including: Emergency diesel generators (EDGs).' The NRC resident inspector has been notified. As of the event report, the MSIVs were opened and decay heat was being removed via the bypass valves to the condenser.
ENS 538616 February 2019 00:04:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentUnit One Hpci System Inoperable Due to Blown FuseOn February 5, 2019, at 1804 (CST), during a Unit 1 High Pressure Coolant Injection (HPCI) operability surveillance, a fuse blew in the logic for the motor speed changer for the turbine. The Unit 1 HPCI system was taken out of service for planned maintenance earlier in the day. The fuse issue was not related to any maintenance activities. Had HPCI been demanded, this fuse failure would not have allowed HPCI to reach its required speed. HPCI remains inoperable pending resolution of the issue. The Reactor Core Isolation Cooling (RCIC) system was confirmed operable. There were no other systems inoperable at the time of the event. HPCI had been last successfully tested on November 6, 2018. This event is being reported as a condition that could have prevented fulfillment of a safety function in accordance with 10 CFR 50.72(b)(3)(v)(D). The HPCI system is a single train system and the loss of HPCI could impact the plant's ability to mitigate the consequences of an accident. The NRC Senior Resident Inspector has been notified. Inoperable HPCI places the unit in a 14 day Technical Specification Limiting Condition of Operability.
ENS 538188 January 2019 05:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentReactor Core Isolation Cooling Declared InoperableOn January 8, 2019, at 0945 EST Pilgrim Nuclear Power Station discovered that the Reactor Core Isolation Cooling (RCIC) system failed to meet its surveillance test requirements and was declared inoperable; therefore, this condition is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v), 'event or condition that could have prevented the fulfillment of a safety function: (D), mitigate the consequences of an accident.' There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.
ENS 5378812 December 2018 06:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
En Revision Imported Date 12/17/2018

EN Revision Text: MANUAL REACTOR SCRAM DUE TO FAILED OPEN TURBINE BYPASS VALVE At 1351 CST, the reactor was manually shutdown due to 'A' Turbine Bypass Valve opening. The Main Steam Line Isolation Valves were manually closed to facilitate reactor pressure control. Reactor level is being maintained through the use of Reactor Core Isolation Cooling System, Control Rod Drive System, and High Pressure Core Spray System. High Pressure Core Spray System was manually started to initially support reactor water level control. Reactor Pressure is being controlled through the use of the Safety Relief Valves and the Reactor Core Isolation Cooling System. The plant is stable in MODE 3. The cause of the 'A' Turbine Bypass Valve opening is under investigation at this time. The NRC Resident Inspector has been notified.

  • * * UPDATE ON 12/14/18 AT 1140 EST FROM GERRY ELLIS TO TOM KENDZIA * * *

This is an update to EN # 53788 to correct an error on the event classification block of the form. The original notification did not have the block for 8 hour notification for Specified System Actuation checked. The actuation of Reactor Core Isolation Cooling System was discussed in original notification. The licensee notified the NRC Resident Inspector. Notified R4DO (Taylor).

ENS 5377613 October 2018 05:00:0010 CFR 50.73(a)(1), Submit an LER60-Day Optional Telephonic Notification of Invalid Specified System ActuationThis 60-day telephone notification is being made per the reporting requirements specified by 10 CFR 50.73(a)(2)(iv)(A) and 10 CFR 50.73(a)(1) to describe an invalid actuation of a Primary Containment Isolation System (PCIS) Group 1 for Main Steam Isolation Valves (MSIVs), Group 3 for Reactor Water Cleanup (RWCU), Group 6 for Secondary Containment isolation, Group 7 for Reactor Water Sampling, Diesel Generator, Reactor Core Isolation Cooling (RCIC) System logic, and Residual Heat Removal (RHR) logic. Group 1, Group 6, Diesel Generator actuation, RCIC actuation and RHR actuation are within scope of 10 CFR 50.73(a)(2)(iv). Group 3 and Group 7 are not within scope as they affect only one system. Cooper Nuclear Station (CNS) was shut down in Mode 5 at the time of the event with the reactor cavity flooded. On October 13, 2018, at 0028 Central Daylight Time, CNS received full PCIS Groups 1, 3, and 6, and a half Group 7 on the Division 1 side. The MSIVs and RWCU isolation valves were already closed for maintenance. The Secondary Containment isolated. Control Room Emergency Filter and the Standby Gas Treatment Systems initiated. The inboard Reactor Water Sample valve isolated. Diesel Generator #1 started but was not required to connect to the critical bus. Reactor Core Isolation Cooling System logic actuated with no expected response due to being isolated for shutdown conditions. Division 1 RHR pump logic actuated. Division 1 RHR system was operating in shutdown cooling mode. The actuation caused the Division 1 RHR outboard injection and heat exchanger bypass valves to open. Shutdown cooling was unaffected and remained in service throughout the event. The plant systems responded as expected with no Emergency Core Cooling System injection. At the time of the event, an in-service inspection of welds inside the reactor vessel was taking place using a robot scanner that uses two vortex thrusters to hold the robot to the vessel wall. The robot inadvertently passed over an instrument penetration, drawing suction on the process leg, resulting in low reactor water level indications and the subsequent invalid Level 1 and 2 system actuations. Actual reactor vessel water level remained steady at cavity flooded conditions. The NRC Resident Inspector has been notified of this event.
ENS 5367619 October 2018 05:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Trip Due to Feedwater Regulating Valve Failing ClosedAt 1725 CDT, a Feedwater Regulating valve failed closed, resulting in a reactor level transient, which initiated a reactor trip, Primary Containment Isolation System signals to valves in Groups 2, 3, and 4 and initiation of High Pressure Coolant Injection and Reactor Core Isolation Cooling. All control rods inserted and level has been restored to normal. The cause of the feedwater valve failure is under investigation. All other systems responded as expected. This report is being made under 10 CFR 50.72 (b)(2)(iv)(B), (b)(3)(iv)(A) and (b)(2)(iv)(A). The Senior Resident Inspector has been informed. Decay heat is being removed via the main condenser and reactor vessel water level is being maintained by the condensate and feedwater systems.
ENS 5363030 September 2018 04:00:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Scram Due to a Loss of Two Condensate PumpsOn Sunday, September 30, 2018, at 1130 EDT, an automatic scram was received on U3 following a loss of two condensate pumps. Following the reactor scram, water level lowered from normal level of 23" to below 1" which resulted in automatic Group II and Group III isolations. Reactor water level lowered to -48" which resulted in initiation of the High Pressure Coolant Injection and Reactor Core Isolation Cooling systems. Reactor water level and reactor pressure have been restored to their normal bands. All systems responded properly to the event. Unit 3 remains in Mode 3 with reactor pressure being controlled on the turbine bypass valves. The cause and details of the event are under investigation. This report is being made in accordance with 10 CFR 50.72(b)(2)(iv)(A), 10 CFR 50.72(b)(2)(iv)(B), and 10 CFR 50.72(b)(3)(iv)(A). All control rods inserted. Decay heat is being removed via the main condenser. The NRC Resident Inspector has been notified. A notification to the media and a press release were made. Unit 2 was unaffected and continues coastdown to refueling.
ENS 5362526 September 2018 04:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Core Injection (Hpci) System Inoperable

On 9/26/2018 at 1530 EDT, it was discovered that the HPCI system was inoperable due to a blown fuse in the 10C617 Panel, E21-F15A. Therefore, this condition Is being reported as an eight-hour, non-emergency notification per 10 CFR 50.72(b)(3)(v)(D). The blown fuse also impacts 'A' channel Residual Heat Removal (RHR) subsystem and 'A' Core Spray (CS) subsystem. These Emergency Core Cooling subsystems have been declared inoperable. Remaining Emergency Core Cooling subsystems and the Reactor Core Isolation Cooling (RCIC) system remain OPERABLE.

There was no impact on the health and safety of the public or plant personnel." The licensee notified the NRC Resident Inspector and will notify the local authorities.

ENS 5361721 September 2018 04:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded
High Pressure Coolant Injection System Inoperable

On 9/21/18, at 1755 EDT, Peach Bottom Atomic Power Station Unit 3 declared the High Pressure Coolant Injection system (HPCI) inoperable due to an inoperable differential pressure indicating switch (DPIS). The DPIS is used to isolate the HPCI system when there is a high steam line flow condition. Operations declared the HPCI system inoperable and entered Technical Specification 3.5.1 Condition C for HPCI being inoperable. Technical Specification 3.3.6.1 was also entered for HPCI instrumentation being inoperable. Other standby systems (Reactor Core Isolation Cooling and Low Pressure Emergency Core Cooling Systems) are OPERABLE. HPCI is a single train system. Therefore, per NUREG-1022, this condition is being reported pursuant to 10CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of the safety function of a system required to mitigate the consequences of a design event. This condition has been entered into the corrective action program (IR 4175355). Investigation of the exact cause of the indication issue is in progress. The NRC Resident has been informed of this notification.

  • * * UPDATE AT 1317 EDT ON 09/22/2018 FROM CRAIG TAULMAN TO JEFF HERRERA * * *

On 09/22/18 at 0955 EDT, RCS (Reactor Coolant System) pressure boundary leakage was identified as the cause of the HPCI high steam flow indication issue. Technical Specification 3.4.4 was entered which will require the initiation of a nuclear plant shutdown. This indicates a degradation of a principal safety barrier. Current Unit 3 reactor power is 35%. This condition is being reported pursuant to 10 CFR 50.72(b)(2)(i) and 50.72(b)(3)(ii). This condition is being tracked in the corrective action program (IR 4175355). The NRC Resident has been informed". Peach Bottom will be notifying State and local agencies regarding the event. Notified the R1DO (Greives).

ENS 5326515 March 2018 19:24:0010 CFR 50.72(b)(3)(ii)(B), Unanalyzed ConditionFailure to Meet Appendix R RequirementsAt 1524 (EDT) on Thursday, March 15, 2018, Operations was notified of a failure to meet Appendix R requirements for Peach Bottom Atomic Power Station (PBAPS) Unit 2 and Unit 3. Valves associated with the feedwater system for both units were not properly considered as Hi-Lo Pressure interface valves as required by the Appendix R program. This results in the susceptibility to a hot short condition that could open valves, diverting flow from the reactor, damage piping and prevent injection. U3 (Unit 3) Fire Safe Shutdown Credited Reactor Core Isolation Cooling (RCIC) System is affected. U2 (Unit 2) is affected by a potential leak path through the Reactor Water Cleanup system. This event is being reported as an occurrence of an event or condition that results in the nuclear power plant being in an unanalyzed condition that significantly degrades plant safety under 10 CFR 50.72(b)(3)(ii). The Station (PBAPS) is performing hourly fire watches for the impacted areas and is also evaluating this condition for corrective action. The licensee notified the NRC Resident Inspector.
ENS 5318831 January 2018 00:22:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Manual Reactor Scram Due to Main Turbine Load OscillationsOn 1/30/2018 at 1750 (CST), the Reactor Pressure Control Malfunctions ONEP (Off Normal Event Procedure) was entered due to main turbine load oscillations of approximately 30 MWe peak to peak. At 1822 (CST), a manual reactor scram was inserted by placing the Reactor Mode Switch in Shutdown due to continued main turbine load oscillations. Reactor SCRAM ONEP, Turbine Trip ONEP, and EP-2 were entered. Reactor water level was stabilized at 36 inches narrow range on startup level and reactor pressure stabilized at 933 psig using main turbine bypass valves. Reactor Water Level 3 (11.4 inches) was reached which is the setpoint for Group 2 (RHR to Radwaste Isolation) and Group 3 (Shutdown Cooling Isolation). No valve isolated in these systems due to all isolation valves in these groups being in their normally closed position. The lowest Reactor Water level reached was -36 inches wide range. No other safety system actuations occurred and all systems performed as designed. That event is being reported under 10CFR 50.72(b)(2)(iv)(B) as any event or condition that results in actuation of the Reactor Protection System (RPS), when the reactor is critical and also reported under 10CFR 50.72(b)(3)(iv)(A), as any event or condition that results in actuation of RPS. The MSIVs are open with decay heat being removed via steam to the main condenser using the bypass valves. Off site power is stable, and the plant is in a normal shutdown electrical lineup. RCIC (Reactor Core Isolation Cooling) was out of service for maintenance, and the reactor water level did not reach the system activation level. The cause of the main turbine load oscillations being investigated. The licensee notified the NRC Resident Inspector.
ENS 5316210 January 2018 15:28:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(iv)(A), System Actuation
Automatic Reactor Scram Due to Turbine Control Valve Fast Closure Scram SignalAt 0928 CST on January 10, 2018, the Unit 3 reactor automatically scrammed due to a Reactor Protection System (RPS) signal generated from Turbine Control Valve Emergency Trip System pressure low. The reactor had been operating near 73 percent power for an emergent issue for Turbine Control Valve (TCV) No. 3. With TCV No. 3 out of service and closed, the unit was operating with RPS in a half scram condition. A subsequent failure of the TCV No. 2 sensing line resulted in RPS coincidence logic being met for TCV fast closure SCRAM. The investigation of the TCV No. 2 sensing line failure continues. All control rods fully inserted into the core. Main Steam Isolation Valves remained open with Main Turbine Bypass Valves controlling reactor pressure. Reactor Feedwater pumps remained in service to control reactor water level. Primary Containment Isolation Signals Groups 2, 3, 6, and 8 containment isolation and initiation signals were received. Upon receipt of these signals all required components actuated as required. Neither High Pressure Coolant Injection nor Reactor Core Isolation Cooling initiation signals were received. This event is reportable within 4 hours per 10 CFR 50.72(b)(2)(iv)(B) 'any event or condition that results in actuation of the Reactor Protection System (RPS) when the reactor is critical except when the actuation results from and is part of a preplanned sequence during testing or reactor operation.' It is also reportable within 8 hours per 10 CFR 50.72(b)(3)(iv)(A) and requires an LER within 60 days per 10 CFR 50.73(a)(2)(iv)(A). The NRC Resident inspector has been notified.
ENS 5312317 December 2017 08:16:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection (Hpci) System Declared Inoperable

On December 17, 2017 at 0316 EST, the Unit 2 HPCI system was isolated and declared inoperable due to a packing failure of the HPCI Turbine Steam Supply Valve (i.e., 2-E41-F001). Isolation of the HPCI system due to the packing failure prevents the HPCI system from performing its design safety function. As such, this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of a system that is needed to mitigate the consequences of an accident. Unit 2 HPCI system has been isolated and depressurized. The HPCI system will remain inoperable until the valve can be repaired. The safety significance of this condition is minimal. All other Emergency Core Cooling Systems (ECCS) and the Reactor Core Isolation Cooling (RCIC) system remain operable. This event did not result in any adverse impact to the health and safety of the public. The NRC Resident Inspector has been notified.

  • * * RETRACTION ON 1/29/18 AT 1514 EST FROM MARK TURKAL TO DONG PARK * * *

Based upon further evaluation, Duke Energy is retracting Event Notification 53123. Engineering has determined that the packing failure of the HPCI Turbine Steam Supply Valve did not prevent the HPCI system from performing its safety function. Environmental conditions resulting from the steam leak would not have caused automatic HPCI isolation or otherwise have degraded HPCI operation. Additionally, the amount of steam diverted through the packing leak was negligible with respect to total steam flow and did not affect HPCI system performance. HPCI would have remained operable throughout its entire mission time. Therefore, this condition does not represent an event or condition that could have prevented fulfillment of a safety function needed to mitigate the consequences of an accident and is not reportable in accordance with 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified of this retraction. Notified R2DO (Heisserer).

ENS 5311512 December 2017 15:18:0010 CFR 50.72(b)(3)(iv)(A), System ActuationAutomatic Start of Edg Due to Loss of Esf TransformerAt approximately 0918 CST on Tuesday, December 12, 2017, the Grand Gulf Nuclear Station experienced a loss of the Engineered Safety Features (ESF) Transformer 11 which was powering the Division 1 ESF bus. Subsequently, the station experienced an automatic start of the Division 1 Emergency Diesel Generator (EDG), partial isolation of the primary and secondary containment buildings and the isolation of the Reactor Core Isolation Cooling System (RCIC). It is not currently understood why the RCIC system isolated during this event. A team is investigating this issue separately from the loss of the ESF 11 transformer. The cause of the event is under investigation at this time. No other issues or unexpected events occurred. The NRC Resident Inspector has been notified of the event.
ENS 530598 November 2017 00:10:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentUnit 1 High Pressure Coolant Injection InoperableOn November 7, 2017 at 1810 (CST), Unit 1 High Pressure Coolant Injection (HPCI), was manually isolated following failure of the remote turbine trip pushbutton to function. Unit 1 HPCI Operability Testing was in progress to the point of securing the HPCI turbine with the remote manual pushbutton. The pushbutton failed to trip the turbine resulting in operator action to lower the flow controller setpoint and isolating the HPCI steam line. HPCI remains isolated and is Inoperable pending resolution of the Turbine Trip circuitry. This event is being reported as a condition that could have prevented fulfillment of a safety function in accordance with 10CFR50.72(b)(3)(v)(D). The HPCI system is a single train system and the loss of HPCI could impact the plant ability to mitigate the consequences of an accident. The Reactor Core Isolation Cooling (RCIC) system was confirmed operable. The NRC Senior Resident Inspector has been notified.