ENS 56116
ENS Event | |
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06:32 Sep 19, 2022 | |
Title | Safety System Inoperability |
Event Description | The following information was provided by the licensee via email:
At 0132 CDT on September 19, 2022, River Bend Station (RBS) was operating at 100% power when the high pressure core spray (HPCS) system was declared inoperable in accordance with technical specification 3.8.9, condition E (declare HPCS and standby service water system pump 2C inoperable immediately) due to a E22-S003, HPCS transformer feeder malfunction. The HPCS is a single train system at RBS, therefore this event is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as an event or condition that could have prevented the fulfilment of a safety function. The reactor core isolation cooling system has been verified to be operable. The NRC Resident Inspector has been notified. The following additional information was obtained from the licensee in accordance with Headquarters Operations Officers Report Guidance: RBS has entered a 14-day limiting condition for operation due to the loss of HPCS and they have upgraded their on-line plant risk model to "yellow". |
Where | |
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River Bend Louisiana (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
LER: | 05000458/LER-2022-004 High Pressure Core Spray Inoperable Due to Transformer Failure 05000458/LER-2022-004-01 High Pressure Core Spray Inoperable Due to Transformer Failure |
Time - Person (Reporting Time:+2.08 h0.0867 days <br />0.0124 weeks <br />0.00285 months <br />) | |
Opened: | Thong Le 08:37 Sep 19, 2022 |
NRC Officer: | Ernest West |
Last Updated: | Sep 19, 2022 |
56116 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |