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 Start dateReporting criterionTitleEvent descriptionSystemLER
ENS 5657013 June 2023 03:33:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentAccident Mitigation - High Pressure Coolant Injection Declared Inoperable

The following information was provided by the licensee via email: At 2333 EDT on June 12, 2023, the division 2 Mechanical Draft Cooling Tower (MDCT) Fan `D' was declared inoperable due to a trip of the fan while running in high speed. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High-Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI room cooler. The cause of MDCT Fan `D' trip is currently unknown with trouble shooting being developed for remediation of the condition. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Senior Resident Inspector has been notified.

  • * * RETRACTION AT 1540 EDT ON 8/8/2023 FROM WHITNEY HEMINGWAY TO BILL GOTT * * *

The purpose of this notification is to retract a previous event notification (EN) 56570 reported on June 13, 2023, at 0602 EDT. The cause of the fan trip was a failed vibration switch. At 0429 EDT on June 14, 2023, the vibration switch was replaced, the MDCT fan "D" was tested satisfactory for operability, and the UHS, emergency diesel generator 13/14, and MDCT were declared operable. Following the initial EN, further analysis of the condition was performed utilizing a previously performed gothic analysis model (to perform HPCI room heat-up calculations) which bounded this condition. Based on the initial conditions at the time of the indication loss, specifically HPCI room and suppression pool temperature, it was determined that the resulting worst case post-accident room temperature was sufficiently low enough to provide margin to HPCI operability without the room cooler in service for the required mission time. No other concerns were noted during the event. HPCI remained operable and there was no loss of safety function. The fan trip did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). Therefore, the NRC non-emergency 10CFR50.72(b)(3)(v)(D) report was not required and the NRC report 56570 can be retracted, and no licensee event report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The licensee notified the NRC Resident Inspector. Notified R3DO (Nguyen)

High Pressure Coolant Injection
Emergency Diesel Generator
Emergency Equipment Cooling Water
ENS 5642923 March 2023 15:45:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Design Flaw Discovered in Mechanical Draft Cooling Tower Fan BrakesThe following information was provided by the licensee via fax: While in Mode 1 at 100 percent power at 1145 EDT on March 23, 2023, it was determined that all mechanical draft cooling Tower (MDCT) fan brakes would not perform their design function during a tornado due to a design flaw with the control system. The MDCT fan brakes are required to prevent fan overspeed from a design basis tornado. The MDCT fans are required to support the operability of the ultimate heat sink (UHS). At the time of discovery, the provisions of LCO 3.0.9 were being utilized for loss of the 'D' MDCT fan brake (barrier loss). When it was identified the condition was a design flaw common to all MDCT fan brakes, the 24-hour allowance for restoration was entered. A design change is currently being implemented to restore MDCT fan brake operability. This condition is reportable per 10 CFR 50.72(b)(3)(v)(A), (B), & (D). The NRC Resident Inspector has been notified.
ENS 562954 January 2023 06:48:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Inoperable

The following information was provided by the licensee via email: At 0148 EST on January 4, 2023 it was identified that P4400F603B, Division 2 Emergency Equipment Cooling Water (EECW) Supply Isolation Valve, lost position indication. Division 2 EECW System was declared inoperable due to the potential that this valve may not be capable of performing its safety function to automatically isolate the safety related Division 2 EECW system from the non-safety related Reactor Building Closed Cooling Water (RBCCW) system. Because the Division 2 EECW system provides cooling to the High Pressure Coolant Injection (HPCI) room cooler, HPCI was also declared inoperable; therefore, this condition is being reported as an eight-hour, non--emergency notification per 10 CFR 50.72(b)(3)(v)(D). At 0240 EST, position indication was restored and Division 2 EECW and HPCI was returned to operable following inspection of the associated motor control center (MCC) and testing of the associated fuses. The cause of the loss of indication is under investigation. The Senior NRC resident inspector has been notified.

  • * * RETRACTION ON 3/6/23 AT 1740 EST FROM GREGORY MILLER TO KERBY SCALES * * *

The following retraction was received from the licensee via email: The purpose of this notification is to retract a previous Event Notification, EN 56295, reported on 1/4/2023. Following the initial EN, further analysis of the condition was performed utilizing a gothic analysis model to perform HPCI room heat-up calculations. Based on the initial conditions at the time of the indication loss, specifically HPCI room and Suppression Pool temperature, it was determined that the resulting worst case post-accident room temperature was sufficiently low enough to provide margin to HPCI operability without the room cooler in service for the required mission time. No other concerns were noted during the event. Therefore, HPCI remained operable and there was no loss of safety function. The event did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). Therefore, the NRC non-emergency 10 CFR 50.72(b)(3)(v)(D) report was not required and the NRC report 56295 can be retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The NRC Senior Resident Inspector has been notified. Notified R3DO (Ruiz).

High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 5624128 November 2022 09:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Inoperable

The following information was provided by the licensee via email: At 0400 EST on November 28, 2022, during the performance of Division 2 Residual Heat Removal (RHR) cooling tower fan operability and RHR Service Water valve lineup verification, it was reported that the Mechanical Draft Cooling Tower (MDCT) Fan 'B' was making a loud metallic noise. The cause of the metallic noise is unknown at this time. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on inoperable cooling water to the HPCI room cooler, per LCO 3.0.6. Investigation into the Division 2 MDCT Fan 'B' abnormal noise is in progress. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JEFF MYERS TO LLOYD DESOTELL AT 1615 EST ON 12/09/2022 * * *

The following information was provided by the licensee via email: The purpose of this notification is to retract a previous Event Notification 56241 reported on 11/28/2022. On 11/28/22, an event notification to the NRC was made when mechanical draft cooling tower (MDCT) Fan B was declared inoperable and issued Limited Condition of Operation (LCO) 2022-0428 for Division 2 MDCT Fan B abnormal noise. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS) (Technical Specification (TS) 3.7.2). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system (TS 3.7.2), which cools various safety related components, including the High-Pressure Coolant Injection (HPCI) system room cooler (TS LCO 3.0.6). Subsequent inspection and evaluation determined that the brake noise is expected while fans are running at low speeds. This is supported by plant technical procedure, 24.205.10 `Div. 2 RHR Cooling Tower Fan Operability and RHRSW Valve Line-up Verification' (line item 2.2 in Precautions and Limitations) which states `Chatter from the brakes of the MDCT Fans is expected and no cause for discontinuing the test.' The equipment vendor stated that brake chatter is possible and common given that the internal components are free to move along the splined connections. Internal Operating Experience from experienced station operators and maintenance technicians confirmed that the condition is normal and expected. Both Division 2 MDCTs exhibited the same behavior at low speed and passed surveillance testing satisfactorily. No other concerns were noted during fan operation. Therefore, HPCI remained operable and there was no loss of safety function. The event did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). EN 56241 is retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The NRC Resident Inspector has been notified. Notified R3DO (Stoedter).

Service water
High Pressure Coolant Injection
Residual Heat Removal
Emergency Equipment Cooling Water
ENS 5605418 August 2022 01:08:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentSafety System Inoperability

The following information was provided by the licensee via email: At 2108 EDT on August 17, 2022 the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The Division 2 EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) room cooler and Division 2 Control Center HVAC (CCHVAC) chiller. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. At the time of the event, Division I CCHVAC was inoperable for maintenance (but was running for a maintenance run) and the event caused an inoperability of Division 2 CCHVAC. This resulted in an inoperability of both divisions of CCHVAC. Failure of the Division 2 MDCT Fan brake inverter occurred due to a trip of the DC input breaker. The breaker was reset at 2128 EDT restoring Division 2 UHS Operability. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfilment of the safety function of structures or systems that are needed to mitigate the consequences of an accident based on a loss of a single train safety system and loss of both divisions of a safety system. The Senior NRC Resident Inspector has been notified

  • * * RETRACTION ON 09/08/2022 AT 0856 EDT FROM JEFF MYERS TO MIKE STAFFORD * * *

The following information was provided by the licensee via email: On 8/17/22 at 2108 EDT the Division 2 (Div. 2) mechanical draft cooling tower (MDCT) brake inverter input breaker tripped for an unknown cause. The result of the loss of power was the inoperability of the MDCT fan brakes which impacts the ultimate heat sink (UHS) (TS 3.7.2). The UHS cascades to the EECW (emergency equipment cooling water) (TS 3.7.2) which is a support system for Div. 2 CCHVAC (Control Cell) Chiller A/C system (TS 3.7.4). This resulted in the inoperability of the Div. 2 CCHVAC Chiller. The cause for the breaker to trip is an intermittent electrical transient. Immediate corrective action was to reset the breaker, and the long-term action is to implement a modification to mitigate susceptibility to voltage variations. Div. 1 has implemented this long-term mod and no unexpected trips have occurred to date. Div. 1 CCHVAC Chiller was previously inoperable from equipment issues which was repaired, and the unit was in service for a 24-hour confidence run. Although licensed personnel had not completed the administrative actions for documenting operability during the 24-hour confidence run to monitor parameters, the (post maintenance test) PMT related to the maintenance was already completed, which included a 4-hour run in accordance with surveillance 24.413.01, Div. 1 and Div. 2 Chilled Water Pump and Valve, to verify normal operation and motor current. These PMT's were completed prior to the identified inoperability of the Div. 2 UHS due to the tripped breaker on the brake power supply. At the time of the MDCT brake inverter trip, the Operations' Senior License and the Night Shift Manager were aligned that, although still operating as part of the 24-hour confidence run, the unit was in service and capable of performing its safety function, but the administrative tasks were not completed, the Limited Condition of Operation (LCO) sheet had not been cleared, and no log entries were made. Since the Div. 1 Chiller was, in fact, operable at the time of the trip of the breaker on the inverter, this would allow the use of Technical Specification (TS) 3.0.9 'Barriers'. Per Operations Department Expectation (ODE)-12 `LCOs' (standard guidance and expectations for preparing and implementing an LCO), Operations determined that the MDCT brakes are barriers to a tornado event and TS 3.0.9 could be utilized. By invoking TS 3.0.9, as long as all other supported systems in the other division are operable, Div. 2 supported systems relying upon the UHS can remain operable and the Automatic Depressurization System (ADS) and Reactor Core Isolation Cooling (RCIC) system can be used as backup to the High Pressure Coolant Injection (HPCI) system. Based on this information, there was no loss of safety function with CCHVAC A/C system or HPCI. Therefore, the NRC non-emergency 10CFR50.72(b)(3)(v)(D) report was not required and the NRC report 56054 can be retracted. The NRC Resident Inspector has been notified. Notified R3DO (Orlikowski)

High Pressure Coolant Injection
Reactor Core Isolation Cooling
HVAC
Automatic Depressurization System
Emergency Equipment Cooling Water
ENS 5589411 May 2022 22:14:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection InoperableThe following information was provided by the licensee via email: During performance of High Pressure Coolant Injection (HPCI) Pump and Valve Operability surveillance in accordance with procedure 24.202.01, the turbine tripped without operator action. The plant was operating in Mode 1 at 10 percent power with the HPCI turbine running in a test mode at 5100 gpm with all surveillance criteria met. The surveillance was near completion at the point where the HPCI turbine is manually tripped. Before the manual trip was performed, the HPCI turbine tripped without operator action. Prior to performance of the surveillance, HPCI was provisionally operable with only satisfactory completion of Post Maintenance Testing (PMT) surveillance remaining to declare HPCI operable. HPCI surveillance testing was performed at low reactor pressure (165 psig) in Mode 2 satisfactorily. Investigation into the cause of this trip is in progress. HPCI has been declared inoperable from the time of release of the surveillance. Reactor Coolant Isolation Cooling (RCIC) was verified to be operable prior to and after the surveillance in accordance with Technical Specifications 3.5.1 condition E.1. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.High Pressure Coolant Injection
ENS 5542322 August 2021 09:29:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHPCI Declared InoperableAt 0529 EDT on August 22, 2021, HPCI ((High Pressure Coolant Injection System)) was declared inoperable due to receiving the HPCI Inverter Circuit Failure annunciator. The cause of the annunciator was a fuse failure. The cause of the fuse failure is unknown at this time and is under investigation. Concurrent with the HPCI fuse failure was a similar fuse failure within the Division 2 EDG ((emergency diesel generators)) Load Sequencer which renders the Division 2 EDGs inoperable. Relation to the HPCI issue is unknown and is part of the investigation. The RCIC ((Reactor Core Isolation Cooling System)) was verified operable per Tech Spec 3.5.1 E.1. In addition, offsite circuits were verified operable per Tech Spec 3.8.1.B. Division 1 EDGs remain operable. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. There was no impact on the health and safety of the public or plant personnel. The Senior NRC Resident Inspector has been notified.High Pressure Coolant Injection
Emergency Diesel Generator
Reactor Core Isolation Cooling
ENS 5540311 August 2021 10:34:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHPCI Inoperability

At 0634 EDT on August 11, 2021 (high pressure coolant injection) HPCI was declared inoperable due to a pump flow controller problem. The cause of the controller problem is unknown at this time and is under investigation. (Reactor core isolation cooling) RCIC was verified operable per Tech Spec 3.5.1 E.1. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM WHITNEY HEMMINGWAY TO KAREN COTTON ON 10/6/2021 AT 1036 EDT * * *

The purpose of this notification is to retract a previous report made on August 11, 2021 (EN 55403). At 0634 EDT on August 11, 2021, an unplanned inoperability of the High Pressure Coolant Injection system (HPCI) was reported pursuant to 10 CFR 50.72(b)(3)(v)(D) by EN 55403. HPCI was declared inoperable due to receipt of an alarm associated with the pump flow controller. The HPCI system operating procedure states that HPCI should be declared inoperable when this alarm is received. The cause of the alarm, a loose transmitter connection, was identified and corrected. Following clearance of the alarm, HPCI was declared operable at approximately 1930 EDT on August 11, 2021. This alarm indicated a fault in the signal from the transmitter to the HPCI flow controller; in this case, the HPCI flow controller would have continuously called for maximum HPCI flow. The controller is configured with a high limiter to prevent an overspeed trip. An engineering evaluation of the event identified that HPCI was capable of performing its required safety functions while this alarm was present. The condition was that the HPCI flow controller would have continuously called for maximum HPCI flow upon HPCI initiation, however operators would be able to manually control HPCI flow upon HPCI initiation. Additionally HPCI would have run until Reactor Pressure Vessel (RPV) level reached Level 8 where it would trip until RPV level decreased to Level 2 then automatically restart. The licensee notified the NRC Resident Inspector. Notified R3DO (Peterson).

High Pressure Coolant Injection
Reactor Pressure Vessel
ENS 555583 June 2021 06:41:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Inoperable Due to LOW Level InstrumentationAt 0241 (EDT) on June 3, 2021, during performance of a High Pressure Coolant Injection (HPCI) Condensate Storage Tank (CST) level functional surveillance, the HPCI torus suction inboard isolation valve was slow to open during swap of suction from the CST to the Torus. On June 9, 2021, it was determined that as a result of the June 3, 2021, slow swap condition, TS 3.3.5.1 Required Action D.1 to declare HPCI inoperable within 1 hour was applicable due to inoperable CST low level instrumentation channels. At 1817 (EDT) on June 3, 2021, HPCI suction was swapped to the torus, making TS Required Action D.1 no longer applicable. Reactor Core Isolation Cooling (RCIC) was available throughout this condition. At 0900 (EDT) on November 3, 2021, it was determined that an NRC event report due to HPCI inoperability should have been made. This event is being reported as a late 8-hour non-emergency notification pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The cause of the slow valve opening was later determined to be corrosion products on contacts of a relay in the CST low level instrumentation logic. On June 4, 2021 at 1451 (EDT), the HPCI CST Level Functional Test was completed Satisfactorily, restoring HPCI Instrumentation to Operable. There was no impact on the health and safety of the public or plant personnel. The NRC Resident Inspector has been notified.High Pressure Coolant Injection
Reactor Core Isolation Cooling
ENS 5429325 September 2019 16:03:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Declared Inoperable

At 1203 EDT, on September 25, 2019, during a Division 2 Emergency Equipment Service Water (EESW) pump and valve surveillance test, the Division 2 Emergency Equipment Cooling Water (EECW) Temperature Control Valve was found to be approximately 80 percent open rather than in its required full open position during fail safe testing. The Division 2 EESW system is required to support operability of the Division 2 EECW system. The Division 2 EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. An investigation is underway into the cause of the failure. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Senior Resident Inspector has been notified. The licensee is in 72-hour shutdown action statement.

  • * * RETRACTION ON 11/21/19 AT 1547 EST FROM PAUL ANGOVE TO BRIAN LIN * * *

Subsequent engineering evaluation has determined that the EECW TCV was capable of passing sufficient flow to perform its design basis functions, including supporting the HPCI room cooler, while approximately 80% open. Therefore, HPCI remained operable and there was no loss of safety function. The event did not involve a condition that could have prevented the fulfillment of the safety function of structures or systems that are needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). EN 54293 is retracted and no Licensee Event Report under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The NRC Resident Inspector has been notified. Notified R3DO (Cameron).

Service water
High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 5418830 July 2019 14:14:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentUnplanned High Pressue Coolant Injection InoperabilityOn July 30, 2019, at 1014 EDT, the Division 2 Mechanical Draft Cooling Tower (MDCT) Fan D was declared inoperable due to a trip of the fan while placing in it high speed. The MDCT Fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. Investigation revealed that a high speed breaker control power fuse had blown. The control power fuse was replaced, the MDCT Fan D was tested satisfactorily, and HPCI was declared operable at 1431 EDT. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The licensee has notified the NRC Senior Resident InspectorHigh Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 538111 January 2019 05:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Gland Seal Exhauster - Automatic Trip Function InoperableOn January 1, 2019 at approximately 0454 EST, while performing planned maintenance activities on the Feedwater Distributed Control System (FW DCS), it was discovered that the automatic trip instrumentation of the Gland Seal Exhauster (GSE) was inoperable. The automatic GSE trip is assumed in the safety analysis for the Control Rod Drop Accident (CRDA) and is required when Thermal Power is less than or equal to 10%. The automatic trip function of the GSE was inoperable for 1 minute, 19 seconds. No Control Rod movement occurred while the automatic trip of the GSE was inoperable. There was no adverse impact to public health and safety or to plant employees and there was no radiological release. This report is being made pursuant to 10CFR50.72(b)(3)(v)(C) and 10CFR50.72(b)(3)(v)(D). The NRC Resident Inspector has been notified.Feedwater
Control Rod
ENS 537724 December 2018 14:35:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEn Revision Imported Date 1/31/2019

EN Revision Text: HPCI INOPERABLE DUE TO MECHANICAL DRAFT COOLING TOWER FAN BRAKE INVERTER FAILURE At 0935 EST on December 4, 2018, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. Investigation into why the Division 2 MDCT fan over speed brake inverter failed is in progress. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Resident Inspector has been notified. Fermi 2 is in a 14-day LCO for inoperability of HPCI and a 72-hour LCO for UHS inoperability.

  • * * RETRACTION ON 1/30/19 AT 1605 EST FROM CHRIS ROBINSON TO BETHANY CECERE * * *

The purpose of this notification is to retract EN 53772 made on December 4, 2018. Subsequent to the initial notification, the event and site Technical Specifications (TS) were reviewed further. An evaluation determined that TS Limiting Condition for Operation (LCO) 3.0.9 for barriers could be applied to the MDCT fan brakes. As a result of applying TS LCO 3.0.9 to the MDCT fan brakes, it was not necessary to declare the UHS inoperable. With the Division 2 UHS operable on December 4, 2018, the HPCI system was also operable. With HPCI operable, there was no event or condition that could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident under 10 CFR 50.72(b)(3)(v)(D). Therefore, EN 53772 is retracted and no Licensee Event Report (LER) under 10 CFR 50.73(a)(2)(v)(D) is required to be submitted. The licensee has notified the NRC Resident Inspector. Notified R3DO (Cameron).

High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 535373 August 2018 04:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection Declared InoperableAt 0940 EDT on August 3, 2018, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. Investigation into why the Division 2 MDCT fan over speed brake inverter failed is in progress. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) based on an unplanned HPCI inoperability. The NRC Resident Inspector has been notified.High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 5343531 May 2018 18:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Water Cleanup System Declared InoperableOn May 31, 2018 at 1420 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow condition. At 1519 EDT, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C), and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.Primary containment
Reactor Water Cleanup
ENS 5342927 May 2018 10:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Reactor Water Cleanup System Declared InoperableOn May 27, 2018 at 0630 EDT, the Reactor Water Cleanup (RWCU) System Isolation Differential Flow - High function was declared inoperable as a result of indicating downscale. This condition would have prevented the primary containment isolation valves for the RWCU system from automatically isolating on a high differential flow instrumentation signal. At 0753, RWCU was shutdown and the affected penetration flow paths were isolated in accordance with station procedures per Fermi Technical Specifications. The cause of the event is under investigation. There was no radiological release associated with this event. All other RWCU primary containment isolation instrumentation functions remained operable and the associated RWCU system primary containment isolation valves were capable of being remotely closed by the control room operators throughout the event. However, the condition is reportable pursuant to 10 CFR 50.72(b)(3)(v)(C) and 10 CFR 50.72(b)(3)(v)(D). The NRC Resident Inspector was notified.Primary containment
Reactor Water Cleanup
ENS 5333614 April 2018 14:40:0010 CFR 50.72(b)(2)(iv)(B), RPS System Actuation
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(iv)(A), System Actuation
10 CFR 50.72(b)(2)(iv)(A), System Actuation - ECCS Discharge
Automatic Reactor Scram and Emergency Core Cooling System Injection

At 1040 EDT, Fermi 2 automatically scrammed on RPV (Reactor Pressure Vessel) Level 3 following a loss of the Division 1 Station System Transformer (SST) #64. All control rods fully inserted. HPCI (High Pressure Coolant Injection) and RCIC (Reactor Core Isolation Cooling) automatically started as designed on Reactor Water Level (RWL) 2 and restored RWL. The lowest RWL reached was 101.8 inches (above Top of Active Fuel). HPCI injected for approximately 35 seconds. RWL is currently being maintained in the normal level band with RCIC. No Safety Relief Valves (SRVs) actuated. All isolations and actuations for RWL 3 and 2 occurred as expected. Investigation into loss of SST #64 continues. At the time of the scram, all Emergency Core Cooling Systems (ECCS) and Emergency Diesel Generators (EDGs) were operable, and no safety related equipment was out of service. This report is being made in accordance with 10CFR50.72(b)(2)(iv)(A), any event that results in ECCS discharge into the reactor coolant system as a result of a valid signal and 10CFR50.72(b)(2)(iv)(B), any event that results in the actuation of the Reactor Protection System (RPS) when the reactor is critical. Following the loss of power and reactor scram, the Division 2 EECW (Emergency Equipment Cooling Water) Temperature Control Valve (TCV) controller was in Emergency Manual and maintaining max cooling. Operators placed the controller in Auto and the TCV is controlling normally. The NRC Senior Resident has been notified. Decay heat is being removed via Division 2 steam dumps to the condenser. The plant is in a modified shutdown electric lineup with offsite power available and stable. Emergency diesel generators did automatically start and load.

  • * * UPDATE ON 4/14/2018 AT 1838 EDT FROM JEFF MYERS TO HOWIE CROUCH * * *

This update provides additional clarification of the applicable reporting criteria for this event associated with Primary Containment Isolation Actuations. All isolations and actuations for RWL (Groups 4, 13, and 15) and RWL 2 (Groups 2, 10, 11, 12, 14, 16, 17, and 18) occurred as expected. This report is also being made in accordance with 10CFR50.72(b)(3)(iv)(A), any event or condition that results in valid actuation of any systems listed in paragraph (b)(3)(iv)(B): RPS, HPCI, and RCIC. RPV pressure is being maintained by the bypass valves to the main condenser. All actuations that occurred were fully completed and restored. The licensee notified the NRC Resident Inspector. Notified R3DO (Stone).

  • * * UPDATE ON 4/15/2018 AT 1950 EDT FROM KELLEY BELENKY TO DAVID AIRD * * *

This update provides additional information regarding the specified system actuations and an additional applicable reporting criteria. The loss of Division 1 Station System Transformer (SST) #64 at 1040 EDT on 4/14/2018 resulted in the automatic initiation of Emergency Diesel Generators (EDG) 11 and 12. The EDGs started as expected and continue to supply their associated busses. This is reportable pursuant to 10CFR50.72(b)(3)(iv)(A), as an event or condition that resulted in a valid actuation of any system listed in paragraph (b)(3)(iv)(B), including EDGs. In addition, the loss of the Division 1 SST #64 resulted in the expected transfer from the normal to alternate power source for the Low Pressure Coolant Injection (LPCI) swing bus, rendering LPCI loop select inoperable. The alternate power source continued to energize the LPCI swing bus throughout the event until the system was realigned to the normal power source at 1239 EDT on 4/14/2018. This condition is reportable pursuant to 10CFR50.72(b)(3)(v)(D). The licensee notified the NRC Resident Inspector. Notified R3DO (Stone).

Reactor Coolant System
Reactor Protection System
Emergency Diesel Generator
Primary containment
Emergency Core Cooling System
Safety Relief Valve
Main Condenser
Control Rod
Low Pressure Coolant Injection
ENS 529589 September 2017 14:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentMechanical Draft Cooling Tower Fans Declared InoperableAt 1000 EDT on September 9, 2017, the Division 2 Mechanical Draft Cooling Tower (MDCT) fans were declared inoperable due to failure of the over speed fan brake inverter. The brakes prevent fan over speed from a design basis tornado. The MDCT fans are required to support operability of the Ultimate Heat Sink (UHS). The UHS is required to support operability of the Division 2 Emergency Equipment Cooling Water (EECW) system. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) system room cooler. An unplanned HPCI inoperability occurred based on a loss of the HPCI Room Cooler. Investigation into why the Division 2 MDCT fan over speed brake inverter failed is in progress. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident based on a loss of a single train safety system. The licensee entered two (2) LCO Action Statements (AS); 14-day LCO AS 3.5.1 for ECCS (HPCI Inoperable) and 72-hour AS 3.7.2 for UHS. The licensee has two spare inverters on-site. After replacement and successful post-maintenance testing the licensee expects to exit both AS before 72-hours. The NRC Resident Inspector has been notified.High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 5233128 October 2016 19:00:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Standby Liquid Control Technical Specification Not MetOn October 28, 2016, at 1500 EDT, the Standby Liquid Control system was declared inoperable. Technical Specification (TS) Limiting Condition for Operation (LCO) 3.1.7 Condition B was entered due to sodium pentaborate concentration not within limits. Standby Liquid Control sodium pentaborate concentration was found to be low outside of the acceptable region following a Standby Liquid Control system tank high level alarm in the Main Control Room. Sodium pentaborate was added to the Standby Liquid Control tank by chemistry personnel and the concentration was then verified to be acceptable. Standby Liquid Control was declared Operable on 10/28/16 at 1935 EDT. The cause of the out-of-acceptable concentration was due to make-up water leaking by a closed valve. (The licensee cycled this valve and closed an upstream valve.) Declaring the Standby Liquid Control system inoperable is reportable under 10 CFR 50.72(b)(3)(v)(A), (C), and (D) as an event or condition that could have prevented the fulfillment of a safety function of a system needed to shut down the reactor and maintain it in a safe shutdown condition, control the release of radioactive material, and mitigate the consequences of an accident. The licensee has notified the NRC Resident Inspector.Standby Liquid Control
ENS 5167623 January 2016 00:35:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentLow Pressure Coolant Injection Pump Isolation Valve Would Not ReopenWhile performing a Technical Specification surveillance functional test of the Low Pressure Coolant Injection (LPCI) pump and valve surveillance, the Division 1 LPCI outboard Isolation Valve E1150F017A was closed for stroke time testing and would not reopen. Not being able to be open this valve renders the LPCI Loop Select function inoperable. Time of the event was 1935 (EST). This inoperability of LPCI loop Select results in entry into Technical Specification 3.0.3. Power reduction activities were briefed at time 2020, however, no power reduction commenced due to resolving the issue with the LPCI outboard Isolation Valve E1150F017A. During the investigation there was a loose screw found preventing the close contactor from fully releasing and allowing the open contactor to engage. No other abnormalities were found during this investigation. This screw was removed and the close contactor functioned normally and the valve was opened. The valve was retested satisfactory and the station exited Technical Specification 3.0.3 at 2145. This report is made pursuant to 10 CFR 50.72(b)(3)(v)(D), an event or condition that could have prevented the fulfillment of the safety function of systems needed to mitigate the consequences of an accident. The NRC Resident Inspector was notified.Low Pressure Coolant Injection05000341/LER-2016-002
ENS 517556 January 2016 20:14:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Power Reduction Due to Automatic Opening of the Turbine Bypass Valves

On January 6, 2016, at approximately 1514 EST, with Fermi 2 in Mode 1 operating at 100 percent reactor thermal power, the East and West Turbine Bypass Valves (TBVs) automatically opened for 3 minutes and 32 seconds in response to the number one High Pressure Turbine Stop Valve (TSV) drifting from full open to 25 percent open. Reactor power was subsequently lowered to 91.0 percent reactor thermal power and the bypass valves closed. Per Technical Specification Bases 3.3.1.1, TBVs must remain shut while reactor thermal power is at or above 29.5 percent to consider the TSV closure and Turbine Control Valve (TCV) fast closure Reactor Protection System (RPS) functions operable. The condition was recognized at the time of the event and the RPS functions were not declared inoperable since the functions were verified to remain enabled. Since the RPS functions were not declared inoperable, Fermi 2 did not report this event within 8 hours of occurrence. However, after further evaluation, it was determined that this event met the reporting criterion. Accordingly, this event is being reported pursuant to 10 CFR 50.72(b)(3)(v)(A). The licensee informed the NRC Resident Inspector. The cause of the High Pressure Turbine Stop Valve drifting was due to an actuator malfunction that has since been corrected. This event was determined to be reportable at 1200 EST on 02/24/16. See EN #51756 for a similar event that occurred on 02/21/16.

  • * * UPDATE FROM JEFF GROFF TO STEVEN VITTO ON 03/02/2016 AT 1530 EST * * *

Upon further review, it was determined that this event also meets the reporting criterion of 10CFR50.72(b)(3)(v)(D) for a condition that could have prevented the fulfillment of a safety function of structures or systems that are needed to mitigate the consequences of an accident. Although this event was determined to be reportable at 1200 EST on 02/24/16, it met the reporting requirement on the date of the event (01/06/2016). The licensee informed the NRC Resident Inspector. Notified R3DO (Valos).

Reactor Protection System
ENS 508749 March 2015 19:21:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Tech Spec Required Shutdown Due to Swing Bus Automatic Throwover Failure

While performing a Technical Specification surveillance functional test of the (Low Pressure Coolant Injection) LPCI swing bus automatic throwover scheme, the throwover function failed, rendering LPCI Loop Select inoperable. Time of (the) event was 1521 (EDT). Inoperable LPCI Loop Select results in entry into Tech Spec 3.0.3. Power reduction activities were briefed and power reduction commenced at 1615. Maintenance is currently implementing a contingency work order to correct the auto throwover failure. This report is made pursuant to 10 CFR 50.72(b)(2)(i), initiation of plant shutdown required by the plant's Technical Specifications; and 10 CFR 50.72(b)(3)(v)(D), an event or condition that could have prevented the fulfillment of the safety function of systems needed to mitigate the consequences of an accident. Offsite and Emergency power remain available. The NRC Resident Inspector was notified.

  • * * UPDATE FROM KELLEY BELLENKY TO DANIEL MILLS AT 0123 EDT ON 3/10/2015 * * *

On March 9, 2015, at approximately 1521 (EDT), while performing a functional test of the LPCI swing bus automatic throwover scheme, the throwover function failed, rendering LPCI Loop Select inoperable. Tech Spec 3.0.3 was entered and power reduction commenced at 1615 (EDT). Power was lowered to approximately 80%. Maintenance led a troubleshooting process that found and corrected the equipment problem. At approximately 2311 (EDT), the limiting condition for operating was cleared and LPCI Loop Select was declared operable. Tech Spec 3.0.3 was exited at that time. The licensee notified the NRC Resident Inspector. The plant has returned to 100% power. Notified R3DO (Orth).

  • * * UPDATE FROM DAVID COSIO TO CHARLES TEAL AT 1253 EDT ON 3/10/15 * * *

The LCO and LPCI operability declared was at 2211 EDT NOT 2311 EDT. Notified R3DO (Orth).

ENS 5175621 February 2015 05:30:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
Power Reduction Due to Automatic Opening of a Turbine Bypass Valve

On February 21, 2015, at approximately 0030 EST, with Fermi 2 in Mode 1 operating at 100 percent reactor thermal power, the West Turbine Bypass Valve (TBV) automatically opened in response to the number two High Pressure Turbine Stop Valve (TSV) cycling from full open to closed and then to 22 percent open. Reactor power was subsequently lowered to 91.5 percent reactor thermal power and the bypass valve closed. Per Technical Specification Bases 3.3.1.1, TBVs must remain shut while reactor thermal power is at or above 29.5 percent to consider the TSV closure and Turbine Control Valve (TCV) fast closure Reactor Protection System (RPS) functions operable. The condition was recognized at the time of the event and the RPS functions were declared inoperable. The Limiting Condition for Operation was exited at 0031 EST following TBV closure. Since the RPS functions were verified to remain enabled, Fermi 2 did not report this event within 8 hours of occurrence. However, this event was subsequently determined to meet the reporting criterion and is being reported pursuant to 10 CFR 50.72(b)(3)(v)(A). The licensee informed the NRC Resident Inspector. The cause of the High Pressure Turbine Stop Valve cycling was due to a communication card failure that has since been corrected. This event was determined to be reportable at 1200 EST on 02/24/16. See EN #51755 for a similar event that occurred on 01/06/16.

  • * * UPDATE FROM JEFF GROFF TO STEVEN VITTO ON 03/02/2016 AT 1530 EST * * *

Upon further review, it was determined that this event also meets the reporting criterion of 10CFR50.72(b)(3)(v)(D) for a condition that could have prevented the fulfillment of a safety function of structures or systems that are needed to mitigate the consequences of an accident. Although this event was determined to be reportable at 1200 EST on 02/24/16, it met the reporting requirement on the date of the event (02/21/2015). The licensee informed the NRC Resident Inspector. Notified R3DO (Valos).

Reactor Protection System
ENS 498016 February 2014 17:54:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentEmergency Equipment Cooling Water in Manual Override Due to Human Performance Error

At 1254 (EST) on February 6, 2014, while shutting down Division 2 Emergency Equipment Cooling Water (EECW), a human performance error occurred resulting in the Division 2 EECW isolation override switch being placed in manual override. Division 2 EECW remained running and continued to operate normally. The Division 2 EECW system cools various safety related components including the High Pressure Coolant Injection (HPCI) system room cooler. With the Division 2 EECW isolation override switch in manual override, Division 2 EECW may have been prevented from performing its safety function during a loss of power event. An unplanned HPCI inoperability occurred due to the Division 2 EECW inoperability which may have prevented HPCI from performing its safety function. A 14 day Limiting Condition for Operation (LCO) was entered for HPCI via T.S. LCO 3.5.1 and subsequently exited 36 seconds later upon returning the Division 2 EECW isolation override switch to normal. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on a loss of a single train safety system. The NRC Resident Inspector has been notified. The licensee reported that the individuals involved have been removed from licensee duties pending further investigation.

  • * * RETRACTION FROM PAUL GRESH TO DONALD NORWOOD AT 0931 EDT ON 4/4/14 * * *

The Fermi 2 Engineering staff has completed a comprehensive evaluation of the momentary mispositioning of the Division 2 EECW system overide switch initially reported on February 6, 2014. The evaluation determined that HPCI room temperature would remain below the HPCI room steam leak detection isolation logic setpoint in the unlikely event that the momentary mispositioning resulted in the temporary interruption of the cooling water flow to the HPCI system room cooler. Over the brief period of time for which EECW would have been unavailable to support the effective operation of the room cooler, its function was not necessary for HPCI to perform its required safety functions. Therefore, event notification 49801 is retracted. The licensee notified the NRC Resident Inspector. Notified R3DO (Passehl).

High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 488863 April 2013 14:53:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentCooling Water Makeup Pump Failed to Start During a Surveillance Test

At 1053 (EDT) on April 3, 2013, during the performance of a surveillance test on the Division 2 Emergency Equipment Cooling Water (EECW) system the EECW system was declared inoperable due to the Division 2 EECW makeup pump failing to start during the surveillance. The EECW system cools various safety related components, including the High Pressure Coolant Injection (HPCI) room cooler. A 14 day Limiting Condition for Operation (LCO) was entered for HPCI via (Technical Specification) LCO 3.5.1. Investigation into why the makeup pump did not start is currently in progress. This report is being made pursuant to 10 CFR 50.72 (b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on a loss of a single train safety system. The NRC Resident Inspector has been notified.

  • * * UPDATE FROM BRETT JEBBIA TO VINCE KLCO ON 5/28/13 AT 1613 EDT * * *

An evaluation of Event 48886 has determined that the Division 2 Emergency Cooling Water (EECW) system was capable of supporting HPCI Room Cooler and HPCI operation for a period of time in excess of that required to perform the required safety functions as assumed in the accident analysis. Therefore, this event is retracted. The licensee notified the NRC Resident Inspector. Notified the R3DO (Orth).

High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 472426 September 2011 05:04:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Indication of Hpci Minimum Flow Valve Position LostOn September 6, 2011 at approximately 0104 EDT during surveillance testing of the High Pressure Coolant Injection (HPCI) system, control room position indication was lost on the HPCI Minimum Flow Valve, E4150F012 as the valve was stroking closed following shutdown of HPCI. The Minimum Flow Valve main power fuses were checked (found blown) and replaced in accordance with plant procedures. During stroke time testing of E4150F012, control room position indication was again lost when the operator depressed the open pushbutton. HPCI had been removed from service for quarterly surveillance testing at 2219 EDT September 5, 2011. The unplanned inoperability condition began at 0104 EDT when position indication was lost on the Minimum Flow Valve during system shutdown. The valve was locally verified closed to comply with the action of LCO 3.6.1.3 to isolate the penetration. A 14-day LCO was entered and back dated to the time that HPCI was removed from service for surveillance testing. This report is being made pursuant to 10 CFR 50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on loss of a single train safety system. RCIC was and has remained operable. The NRC Resident Inspector has been notified. The failure is currently under investigation.High Pressure Coolant Injection05000341/LER-2011-001
ENS 4651528 December 2010 17:20:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Inoperable Due to Inoperable Minimum Flow ValveOn December 28, 2010 at approximately 1220 hours, during surveillance testing of the High Pressure Coolant Injection (HPCI) system, abnormal control room position indication was observed on the HPCI Minimum Flow Valve, E4150F012 as the valve was stroking closed. HPCI had been removed from service for quarterly surveillance testing at 0950 hours. The unplanned inoperability condition began at 1220 hours when position indication was lost on the minimum flow valve. The valve was manually closed to comply with the action of LCO 3.6.1.3 to isolate the penetration. A 14 day LCO was entered and back dated to the time that HPCI was removed from service per LCO 3.5.1. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on loss of a single train safety system. RCIC was and has remained operable. The failure is currently under investigation. The licensee notified the NRC Resident Inspector.High Pressure Coolant Injection05000341/LER-2010-004
ENS 4503530 April 2009 14:39:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHpci Declared Inoperable Due to Failure of Test Line Pressure Control Valve During Surveillance Test

During plant startup on 4/29/09 at 2239 (EDT), the startup had progressed to the point where plant conditions were adequate to allow performance of SR 3.5.1.9, High Pressure Coolant Injection (HPCI) System flow testing against system head corresponding to reactor pressure. A Note to SR 3.5.1.9 allows 12 hours to perform this test after adequate reactor steam dome pressure and flow have been established for test performance. During the test performance, the test line pressure control valve did not properly operate to establish the required system head. The HPCI system was shutdown and returned to Standby. Earlier, on 4/29/09, SR 3.5.1.10, low pressure HPCI flow testing was successfully completed. Troubleshooting of the test line pressure control valve was begun. At 1039 (EDT) on 4/30/09, the 12 hour allowance of the Note to SR 4.5.1.9 expired and the HPCI system was declared inoperable for failure to complete the required surveillance. The HPCI system remains in Standby and is configured to perform its safety function. However, this event represents a potential loss of a single train safety system pending repair of the test line pressure control valve and completion of flow testing. With HPCI inoperable, the Unit is in the 14-day Tech. Spec. Action Statement 3.5.1. The licensee is revising their surveillance procedure to allow for manual operation of the failed control valve and estimates that the required testing will be completed within 4 hours. The Unit will remain in Mode 2 pending completion of this test. The licensee informed the NRC Resident Inspector.

  • * * RETRACTION PROVIDED BY D. DUNCAN TO JASON KOZAL 05/01/09 AT 1128 * * *

High Pressure Coolant Injection (HPCI) Surveillance Requirement 3.5.1.9, HPCI system flow testing against system head corresponding to reactor pressure, was satisfactorily completed and HPCI declared OPERABLE May 1, 2009 at 0221 hours. There was no loss of HPCl safety function. Therefore this event is retracted. Notified R3DO (Hills).

High Pressure Coolant Injection
ENS 4481128 January 2009 12:30:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentHigh Pressure Coolant Injection System Inoperable

On January 28, 2009 at 0730 the Division 2 Emergency Equipment Cooling Water System (EECW) was declared inoperable due to a blown control power fuse in the bucket for the P4400F604 - Div 2 EECW Supply to Control Rod Drive (CRD) pumps. This is a normally open valve and is required to close upon EECW initiation to remove non-essential loads. The blown control power fuse would have prevented this action from occurring. The ECCW System cools various safety related components including the High Pressure Coolant Injection (HPCI) System Area Cooler. An unplanned HPCI inoperability occurred due to the Division 2 EECW inoperability based on a loss of the HPCI System Area Cooler. A 14 day Limiting Condition for Operation (LCO) was entered for HPCI per LCO 3.5.1. The control power fuse was replaced, EECW and HPCI were declared operable, and LCO 3.5.1 exited on January 28, 2009 at 1025. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on loss of a single train safety system. The NRC Resident Inspector has been notified.

  • * * RETRACTION FROM JIM KONRAD TO DONALD NORWOOD AT 1449 ON 3/11/09 * * *

The As-Found condition of the Division 2 Emergency Equipment Cooling Water (EECW) Control Rod Drive (CRD) Pump Supply Valve and High Pressure Coolant Injection (HPCI) System Room Cooler were evaluated. The HPCI System Room Cooler was operable with P4400-F604, Division 2 EECW to the CRD supply valve open. Based on an Engineering evaluation of EECW flow during a Loss of Coolant Accident (LOCA) and Non-LOCA conditions with the valve open, there is adequate flow margin in the EECW system. The HPCI Room Cooler had adequate cooling flow to perform its design function. The HPCI room temperature would have been maintained below the HPCI equipment room high temperature isolation setpoint. Additionally, plant procedures provide directions for bypassing the HPCI equipment room high temperature trip. Consequently, there was no loss of HPCI safety function. Declaring HPCI inoperable was conservative and based on initial considerations. Therefore, event notification 44811 is retracted. The Licensee notified the NRC Resident Inspector. Notified R3DO (Lara).

High Pressure Coolant Injection
Emergency Equipment Cooling Water
Control Rod
ENS 446985 December 2008 02:18:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentUnplanned Hpci InoperabilityOn December 4, 2008 at 1735 during steam line warming as part of a planned HPCI pump and valve surveillance, a 4 hour Limiting Condition for Operation was entered for the HPCl Steam Supply Outboard Isolation Valve Bypass Valve (E4150F600) per LCO 3.6.1.3 with the action being to isolate the penetration. This was due to abnormal indications observed from the Main Control Room during movement of the valve. On December 4, 2008 at 2118, unplanned HPCI inoperability occurred due to isolating the HPCI Steam Supply Inboard Isolation Valve (E4150F002) to satisfy LCO 3.6.1.3 1 for the HPCI Steam Supply Outboard Isolation Valve Bypass Valve (E4150F600) inoperability. A 14 day LCO was entered for HPCI per LCO 3.5.1. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function to mitigate the consequences of an accident based on loss of a single train safety system. The NRC Resident Inspector has been notified.05000341/LER-2008-005
ENS 4409926 March 2008 14:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentControl Room Pressure Boundary Door Blocked OpenAt 1045 EDT, it was recognized that Auxiliary Building Door R5-6 is a Control Center Pressure Boundary door. The door was blocked open at approximately 1400 on 3/24/2008 to support draining for on going maintenance on Division 1 CCHVAC Chiller. Upon recognizing this condition, Tech Spec 3.7.3 Action B.1 was entered for an inoperable Control Center Pressure Boundary at 1045 EDT (03/26/2008), with a 24 hour action to restore the boundary to operable status. Actions were taken to close Door R5-6 at 1120 hours (03/26/2008), and Tech Spec 3.7.3 Action B.1 was exited. This event is being reported per 10CFR50.72(b)(3)(v) as a condition that at the time of discovery could have prevented the fulfillment of the safety function of the Control Room Emergency Filtration (CREF) system. The accident mitigation function of CREF could not be assured during the time Door R5-6 was open without administrative controls to close it, if necessary. The licensee notified the site NRC Resident Inspector.05000341/LER-2008-003
ENS 4406213 March 2008 18:45:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentReactor Building to Torus Vacuum Breaker Pressure Switches May Not Perform Design FunctionMarch 13, 2008 at 1445 hours, engineering analysis identified that the pressure switches that operate to open the Reactor Building (RB) to Suppression Chamber (Torus) vacuum breaker isolation valves would not perform their design function. The condition impacted the function of both RB to Torus vacuum breaker isolation valves. One vacuum breaker isolation valve has been opened to maintain the function of the vacuum breaker in that line. A plan is being implemented to correct the deficiency and is expected to be completed within the required 72 hour Limiting Condition for Operation expiration time for the current condition. This is being reported in accordance with 10 CFR 50.72(b)(3)(v)(D) as a condition that could have prevented the fulfillment of the safety function of structures or systems needed to mitigate the consequences of an accident. The licensee informed the NRC Resident Inspector.05000341/LER-2008-002
ENS 4278317 August 2006 23:00:0010 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(v)(C), Loss of Safety Function - Release of Radioactive Material
Emergency Diesel Generators Inoperable Due to Undersized Breaker Control TransformersAt 1900 hrs on 8/17/06, all four Emergency Diesel Generators (EDGs) were declared INOPERABLE. The inoperability is a result of undersized control transformers for each of the Emergency Diesel Generator Service Water (DGSW) Pumps. The concern is that the DGSW pump contactors will not receive adequate voltage at the starters to ensure the starters pickup under degraded voltage conditions. A 2 hour Limiting Condition for Operability (LCO) was entered per LCO 3.8.1 to restore both EDGs in one division to OPERABLE status. At 2100 hours on 8/17/06 the two hour time requirement expired and a 12 hour LCO to place the plant in Mode 3 (Hot Shutdown) was entered. At 0042 hrs on 8/18/06, compensatory measures have been put in place to restore operability to both division 2 EDGs. The compensatory measures include placing the local control switch for both division 2 DGSW Pumps in run. Placing the local control switches in run ensures sufficient voltage will be available at the starters to ensure the starters pickup following a loss of offsite power, load shed, and restoration of power to the applicable busses. With operability restored to division 2 EDGs, the new expiration time for the LCO has been revised to 72 hours based on discovery of one or both EDGs in one division inoperable concurrent with CTG 11-1 (station blackout Combustion Turbine Generator 11-1) not available. After 72 hours, if operability is not restored to either CTG 11-1 or both division 1 EDGs, the plant will be required to enter Mode 3 within the following 12 hours. This report is being made pursuant to 10CFR50.72.(b)(3)(v) as an event or condition that at the time of discovery could have prevented the fulfillment of the safety function of structures or systems that are needed to (A) Shut down the reactor and maintain it in a safe shutdown condition; (B) Remove Residual Heat; (C) Control the release of radioactive material; or (D) Mitigate the consequences of an accident. The NRC resident inspector has been notified. The licensee stated that the current 72 hour LCO will expire at 1900 EDT 08/20/06.Service water
Emergency Diesel Generator
05000341/LER-2006-004
ENS 426226 June 2006 20:00:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentFailure to Meet Emergency Equipment Service Water Surveillance Requirement

On June 6, 2006 at 1600 EDT the Division 2 Emergency Equipment Service Water System (EESW) was in service for a planned surveillance test when the system failed to achieve required flows as specified in the surveillance. These flow rates are acceptance criteria and therefore resulted in system inoperability. EESW cools the Emergency Equipment Cooling Water (EECW) System which in turn cools various safety related components including the High Pressure Coolant Injection (HPCI) System Area Cooler. Unplanned HPCI inoperability occurred due to the Division 2 EECW/EESW inoperability based on loss of the HPCI System Area Cooler. A 14 day Limiting Condition for Operation (LCO) was entered for HPCI per LCO 3.5.1. This report is being made pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on loss of a single train safety system." The licensee notified the NRC Resident Inspector.

  • * * RETRACTION AT 08:14 ON 6/15/2006 FROM JEFF GROFF TO ABRAMOVITZ * * *

On June 6, 2006 at 1600 EDT, during the performance of the quarterly pump and valve operability surveillance test on Division 2 of the Emergency Equipment Service Water System (EESW), the minimum pump flow required by the procedure to perform the test could not be established. Because minimum pump flow could not be established, Division 2 of EESW was declared inoperable. EESW cools the Emergency Equipment Cooling Water (EECW) System which in turn cools various safety related components including the High Pressure Coolant Injection (HPCI) System Area Cooler. HPCI was declared inoperable based on loss of the HPCI System Area Cooler due to the Division 2 EECW/EESW inoperability. A 14 day Limiting Condition for Operation (LCO) was entered for HPCI per LCO 3.5.1. A report was made to the NRC pursuant to 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident, based on loss of a single train safety system. On June 7, 2006, the test was re-performed with the valve in the bypass line around the heat exchanger Temperature Control Valve (TCV) throttled open. The required pump flow was established and the surveillance was successfully completed at 1815 EDT. Further Engineering evaluation concluded that minimum pump flow could not be established on June 6, 2006 due to normal pump wear and heat exchanger fouling. The pump flow required for performing the pump and valve operability surveillance test was established to monitor pump degradation and is higher than the flow required for the EESW system to perform its safety function. It has been verified that the measured flow exceeds the system design basis required flow with an adequate margin and that the pump and heat exchanger remain adequate to support the HPCI room cooling operation. The HPCI safety function was maintained throughout this period; therefore, this event is being retracted. The licensee notified the NRC Resident Inspector. Notified the R3DO (Louden).

Service water
High Pressure Coolant Injection
Emergency Equipment Cooling Water
ENS 4222423 December 2005 03:25:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition
Eecw Temperature Control Valve Not Fully Open

While performing Div. 1 & 2 Emergency Equipment Cooling Water (EECW)/Emergency Equipment Service Water (EESW) Valve Lineup Verification surveillance on 12/22/05, the temperature control valve (TCV) on both divisions of EECW were found to be approximately 95% open rather than their required full open position. The system design requires that the TCV, or the associated TCV bypass valve, be in the full open position during system startup to avoid a potentially damaging pressure transient from occurring. Both divisions of EECW and all supported systems (including HPCl, both divisions Core Spray, and both divisions of RHR) were declared INOPERABLE at 2225 EST. Multiple LCO Required Actions were entered, including entry into LCO 3.0.3. At 2250 EST, Div. 1 EECW was restored to OPERABLE status by fully opening the TCV bypass valve and isolating the TCV, and LCO 3.0.3 was exited. At 2252 EST, Div. 2 EECW was restored to OPERABLE status by fully opening the TCV bypass valve and isolating the TCV, and all associated LCO Required Actions were exited. Reactor power remained at 100% throughout the event. The NRC resident inspector has been notified. This report is being made pursuant to 10CFR50.72(b)(3)(ii)(B) as an unanalyzed condition and 10CFR50.72(b)(3)(v)(D) as a condition that at the time of discovery could have prevented the fulfillment of a safety function needed to mitigate the consequences of an accident. The licensee is investigating the cause of the valve not being fully open. The licensee notified the NRC Resident Inspector.

  • * * UPDATE PROVIDED BY YEAGER TO ROTTON AT 1524 ON 01/05/06 * * *

This is a retraction of NRC Event #42224. Based on further engineering review, it is concluded that no potential damage from a pressure transient would occur as a result of the TCV being approximately 95% open. System startup pressure transient concerns reflected in the operating procedures originated from a previously-experienced pressure transient resulting from void collapse against a closed TCV. System startup with the as-found TCV position still provides a sufficiently-open flow path to preclude void collapse against a closed boundary. Additionally, Engineering has determined that system operation with a 90% open TCV would have no significant impact on total system flow and the cooling function. Therefore, both divisions of EECW and all other supported systems (including HPCI, both divisions of Core Spray, and both divisions of RHR) were operable with the TCV in the approximately 95% open position. The licensee notified the NRC Resident Inspector. Notified R3DO (Ring).

Service water
Core Spray
Emergency Equipment Cooling Water
ENS 4178016 June 2005 13:23:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an AccidentBoth Rhr Lpci Divisions Inoperable Due to Valve FailureOn June 16, 2005 at 0923 EDT, with the plant in Mode 1 at 100% reactor power, both divisions of Residual Heat Removal (RHR) were declared inoperable for the Low Pressure Coolant Injection (LPCI) mode of operation due to a failure of E1150-F017B, Division 2 LPCI Outboard Injection Valve. While performing the Division 2 RHR Pump & Valve Operability Surveillance following a planned Division 2 RHR system outage, E1150-F017B closed properly but failed to open during its required stroke time test. With this valve closed and unable to automatically open, LPCI injection into the RPV from both divisions of RHR would be prevented if LPCI Loop Select Logic selected the Division 2 loop for injection. Therefore, this failure rendered both divisions of RHR inoperable for the LPCI function. LCO 3.5.1.J was entered, which requires immediate entry into LCO 3.0.3. The cause of the failure was subsequently identified and E1150-F017B was returned to its normally open position. At 1146 EDT, Division 1 RHR was declared operable for the LPCI function, and LCO 3.5.1.J and LCO 3.0.3 were exited. The plant remained at 100% power throughout the event. The NRC resident inspector has been notified. This report is being made pursuant to 10CFR 50.72(b)(3)(v)(D).Residual Heat Removal
Low Pressure Coolant Injection
05000341/LER-2005-004
ENS 402101 October 2003 00:50:0010 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown
Plant Shutdown Required by Technical Specifications Due to Inoperable Control Center Hvac

With the plant in Mode 1 and 100% reactor power at 2043 (EDT) on September 30, 2003, while shifting divisions of Control Center HVAC (CCHVAC), the Division 1 chiller failed to start and Division 1 CCHVAC was declared INOPERABLE. At 2050, a restart of Division 2 CCHVAC was attempted and the Division 2 chiller failed to start. Division 2 CCHVAC was declared INOPERABLE, and the plant entered LCO 3.0.3 as required by LCO 3.7.4 Condition D. Plant shutdown was initiated at 2146. Division 1 CCHVAC was declared OPERABLE at 2315, and LCO 3.0.3 was exited. Plant shutdown was terminated at 2315 with the reactor at 84% power. Division 2 CCHVAC remains INOPERABLE and under investigation, with plant operating under LCO 3.7.4 Condition A. Plans are to return to 100% reactor power. All ECCS systems remained OPERABLE during this event. The NRC Resident Inspector has been notified. This report is being made pursuant to 10 CFR 50.72(b)(2)(i) and 10 CFR 50.72(b)(3)(v)(D).

  • * * UPDATE 1428 EDT ON 10/20/03 FROM JEFF YEAGER TO S. SANDIN * * *

The licensee is retracting the notification required per 10 CFR 50.72(b)(3)(v) based on the following: At 2050 hours on September 30,2003 with the plant operating at 100 percent reactor power air conditioning chillers for both divisions of the Control Center Air Conditioning System failed to start. Technical Specification (TS) LCO 3.0.3 was entered as directed by LCO 3.7.4, Control Center Air Conditioning System, Condition D.1 and a plant shutdown initiated at 2146 hours. Notification was made in accordance with 10 CFR 50.72(b)(2)(i), a Plant Shutdown Required by Technical Specifications. The chiller for Division 1 Control Center Air Conditioning System was started after approximately one hour and subsequently declared operable at 2315 hours. TS 3.0.3 was exited and power reduction was terminated at 84 percent reactor power. Notification was also made in accordance with 10 CFR 50.72(b)(3)(v), Event or Condition that Could Have Prevented Fulfillment of a Safety Function. Investigation revealed an oil pressure permissive was not met for start of the chiller due to a small amount of air leaking into a pressure switch while shutdown. This delayed meeting the oil pressure permissive for starting the chiller. Subsequent start attempts removed the air, allowing the pressure permissive to be met and the chiller to be restarted. This restart of the chiller was accomplished from the main control room in accordance with plant procedures. Therefore, Division 1 Control Center Air Conditioning was capable of performing its intended function. This condition is therefore not reportable under 10 CFR 50.72(b)(3)(v). The original notification, Event Number 40210, is retracted. The licensee informed the NRC Resident Inspector. Notified R3DO (Jim Creed).

HVAC