05000285/FIN-2016001-02
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Finding | |
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Title | Licensee-Identified Violation |
Description | Technical Specification 2.6(1) requires containment integrity to be maintained unless the reactor is in a cold or refueling shutdown condition. If containment integrity is not maintained and the reactor does not meet these cold or refueling shutdown conditions, then containment integrity must be restored within one hour or the reactor is required to be in hot shutdown within the next six hours. From November 22, 2013, through June 27, 2014, a test connection cap was left off of a containment penetration which constituted a loss of containment integrity. Upon discovery of this condition on June 27, 2014, the licensee entered Technical Specification 2.6(1) and Abnormal Operating Procedure 12 for loss of containment integrity. The cap was re-installed and containment integrity was restored within one hour. The violation is more than minor because it is associated with the configuration control attribute of the Barrier Integrity Cornerstone. Failure to install the containment penetration cap following local leak rate testing on November 22, 2013, resulted in a loss of containment integrity until it was discovered missing on June 27, 2014. This adversely affected the cornerstone objective to provide reasonable assurance that physical design barriers (i.e., containment) protect the public from radionuclide releases caused by accidents or events. The violation was reviewed by a Senior Reactor Analyst and was determined to be of very low safety significance because the test connection fitting was a 14-inch diameter opening. Inspection Manual Chapter 0609, Significance Determination Process, Appendix H, identifies that small lines (less than 1 to 2 inches in diameter) would not generally contribute to large early release frequency. Therefore, this finding screens to Green. The licensee entered the issue into their corrective action program as Condition Report 2014-07958. |
Site: | Fort Calhoun |
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Report | IR 05000285/2016001 Section 4OA7 |
Date counted | Mar 31, 2016 (2016Q1) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | Licensee-identified |
Inspection Procedure: | |
Inspectors (proximate) | B Cummings C Roque-Cruz G George I Anchondo J Josey J Melfi P Elkmann R Hagar S Alferink S Janicki S Schneider |
Violation of: | Technical Specification - Procedures Technical Specification |
INPO aspect | |
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Finding - Fort Calhoun - IR 05000285/2016001 | |||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Fort Calhoun) @ 2016Q1
Self-Identified List (Fort Calhoun)
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