05000269/FIN-2014007-01
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Finding | |
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Title | Failure to Evaluate the Under Voltage Relays at the Worst Case Minimum Drop Out Bus Voltage |
Description | The team identified a Green non-cited violation of 10 CFR 50, Appendix B, Criterion III, Design Control, for the licensees failure to ensure that at the worst-case voltage, protective devices and thermal overload relays for safety-related loads would not trip prior to and after the transfer to the emergency power source. This transfer occurs for a sustained degraded voltage below the under voltage relay voltage settings for the duration of the time delay setting or the manual actions credited. The licensee revised their voltage calculations to account for previously unanalyzed loads. The licensee entered this issue into its corrective action program as problem identification program (PIP) O-14-2280. The team determined that the performance deficiency was more than minor because it was associated with the Design Control attribute of the Mitigating Systems Cornerstone and affected the cornerstone objective of ensuring the availability, reliability, and capability of systems that respond to initiating events to prevent undesirable consequences. Specifically, the team identified that the voltages evaluated in the licensees analysis were nonconservative and could result in lower unanalyzed voltages that could result in connected safety-related loads stalling, becoming damaged, their protective devices tripping, or loads such as battery chargers being below their minimum operating voltages. The team determined that the finding was of very low safety significance (Green) because it was a design deficiency that did not result in a loss of off-site power operability. The team determined that no cross cutting aspect was applicable because this finding was not indicative of current licensee performance. |
Site: | Oconee |
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Report | IR 05000269/2014007 Section 1R21 |
Date counted | Jun 30, 2014 (2014Q2) |
Type: | NCV: Green |
cornerstone | Mitigating Systems |
Identified by: | NRC identified |
Inspection Procedure: | IP 71111.21 |
Inspectors (proximate) | G Nicely J Eargle R Nease R Williams S Pindale S Sanchez T Fanelli T Tinkel W Monk |
Violation of: | 10 CFR 50 Appendix B Criterion III, Design Control |
INPO aspect | |
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Finding - Oconee - IR 05000269/2014007 | ||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||||
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Finding List (Oconee) @ 2014Q2
Self-Identified List (Oconee)
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