LER-2011-001, For Diablo Canyon Regarding Unit 2 Reactor Trip from Loss of Main Feedwater Pump 2-1 |
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| Reporting criterion: |
10 CFR 50.73(a)(2)(iv)(A), System Actuation
10 CFR 50.73(a)(2)(i)
10 CFR 50.73(a)(2)(vii), Common Cause Inoperability
10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded
10 CFR 50.73(a)(2)(viii)(A)
10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition
10 CFR 50.73(a)(2)(viii)(B)
10 CFR 50.73(a)(2)(iii)
10 CFR 50.73(a)(2)(ix)(A)
10 CFR 50.73(a)(2)(x)
10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor
10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat
10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown
10 CFR 50.73(a)(2)(v), Loss of Safety Function
10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications |
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| 3232011001R00 - NRC Website |
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I.b'"e Pacific Gas and Electric Company J
James R. Becker Site Vice President Diablo Canyon Power Plant Mail Code 104/5/601 P2 0. Box 56 Avila Beach, CA 93424 805.545.3462 Internal: 691.3462 Fax: 805.545.6445 May 25, 2011 PG&E Letter DCL-1 1-063 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555-0001 10 CFR 50.73 Docket No. 50-323, OL-DPR-82 Diablo Canyon Unit 2 Licensee Event Report 2-2011-001-00: Unit 2 Reactor Trip From Loss of Main Feedwater Pump 2-1
Dear Commissioners and Staff:
In accordance with 10 CFR 50.73(a)(2)(iv)(A), Pacific Gas and Electric Company is submitting the enclosed licensee event report regarding the Diablo Canyon Power Plant Unit 2 reactor trip from the loss of main feedwater pump 2-1.
There are no new or revised regulatory commitments in this report.
This event did not adversely affect the health and safety of the public.
swh2/50384994 Enclosure cc/enc:
Elmo E. Collins, NRC Region IV Michael S. Peck, NRC Senior Resident Inspector Alan B. Wang, NRR Project Manager James T. Polickoski, NRC Licensing Project Manager INPO Diablo Distribution J~2AC~
NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010)
, the NRC may digits/characters for each block) not conduct or sponsor, and a person is not required to respond to, the information collection.
- 3. PAGE Diablo Canyon Power Plant 05000 323 1 OF
- 4. TITLE Unit 2 Reactor Trip From Loss of Main Feedwater Pump 2-1
- 5. EVENT DATE
- 6. LER NUMBER
- 7. REPORT DATE
- 8. OTHER FACILITIES INVOLVED RV MNHDA YER FACILITY NAME DOCKET NUMBER MONTH DAY YEAR YEAR SEQUENTIAL REV MONTH DAY YEAR NUMBER NO.
105000 FACILITY NAME DOCKET NUMBER 03 26 2011 2011 1 1 0
05 25 2011 05000
- 9. OPERATING MODE
- 11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR §: (Check all that apply)
E] 20.2201(b)
[
20.2203(a)(3)(i)
E] 50.73(a)(2)(i)(C)
[
50.73(a)(2)(vii) 1
[]
20.2201(d)
[
20.2203(a)(3)(ii) 50.73(a)(2)(ii)(A)
[
50.73(a)(2)(viii)(A) fl 20.2203(a)(1)
[
20.2203(a)(4) 50.73(a)(2)(ii)(B) r] 50.73(a)(2)(viii)(B)
[
20.2203(a)(2)(i) fl 50.36(c)(1)(i)(A) 50.73(a)(2)(iii)
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50.73(a)(2)(ix)(A)
- 10. POWER LEVEL
[
20.2203(a)(2)(ii)
E 50.36(c)(1)(ii)(A)
I]
50.73(a)(2)(iv)(A)
[
50.73(a)(2)(x) 9f 20.2203(a)(2)(iii)
Q 50.36(c)(2) 50.73(a)(2)(v)(A)
[
73.71 (a)(4) 98 20.2203(a)(2)(iv)
[
50.46(a)(3)(ii)
[]
50.73(a)(2)(v)(B)
[
73.71 (a)(5) 5 20.2203(a)(2)(v) 5 50.73(a)(2)(i)(A) 5 50.73(a)(2)(v)(C) 5 OTHER E] 20.2203(a)(2)(vi)
[J 50.73(a)(2)(i)(B)
[J 50.73(a)(2)(v)(D)
Specify in Abstract below or in G. Safety System Responses An automatic actuation of the auxiliary feedwater system, steam generator blowdown isolation, and main feedwater isolation occurred during the plant shutdown. These actuations were expected and all components functioned as designed.
III. Cause of the Problem A. Immediate Cause The local MFW Pump 2-1 electronic components were subjected to hot feedwater spray from a leaking relief valve. As a result, when MFW Pump 2-1 was subjected to the hot feedwater spray from the XS-2-RV-95 failed inlet flange gasket, a grounded circuit for low-low lube oil reservoir level [SJ] caused the MFW Pump 2-1 automatic trip.
B. Root Cause The preliminary root cause identified that Maintenance Procedure MP M-54.1, "Bolt Fabrication and Tensioning," allowed the fasteners for bolted connections using sheet type gasket material to be tensioned to "snug tight" versus providing specific bolt torque requirements. As a result, flange gasket preload has not been consistently applied when sheet type gasket material is used. The failed gasket for the relief valve was installed using this maintenance procedure.
IV. Assessment of Safety Consequences
The DCPP Unit 2 shutdown was normal and as expected following the automatic feedwater pump trip and subsequent manual reactor trip. The Solid State Protection System functioned as designed upon receipt of the manual reactor trip signal. The reactor trip breakers opened and all control rods and shutdown rods inserted as designed. The automatic auxiliary feedwater system actuation was expected with all system components fuctioning as designed. This Condition I event was within the bounds of the Updated Final Safety Analysis Report and the post trip transient response was as expected. As such, this event is not considered risk significant and it did not adversely affect the health and safety of the public.
V. Corrective Actions
A. Immediate Corrective Actions Plant operators initiated a manual reactor trip in accordance with OP AP-15 following the automatic trip of MFW pump 2-1.
B. Corrective Actions to Prevent Recurrence (CAPR)
Using the change management process, Maintenance Procedure MP M-54.1, "Bolt Fabrication and Tensioning," was revised to specify torque requirements for tensioning fasteners that are greater than one half inch on bolted connections, regardless of classification and use, with the exception of soft gasket material (e.g. rubber, Teflon, and Neoprene).
VI. Additional Information
A. Failed Components XS-2-RV-95 inlet gasket
B. Previous Similar Events
The XS-2-RV-95 inlet gasket had previously failed during a plant shutdown for refueling on October 26, 2004. This previous gasket failure did not produce a MFW pump trip or unit shutdown.
C. Industry Reports INPO Operating Experience Report OE 33263, Main Feedwater Pump Amphenol Connection Water Intrusion Results in Manual Plant Trip (DCPP2).
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| 05000323/LER-2011-001, For Diablo Canyon Regarding Unit 2 Reactor Trip from Loss of Main Feedwater Pump 2-1 | For Diablo Canyon Regarding Unit 2 Reactor Trip from Loss of Main Feedwater Pump 2-1 | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-001, Regarding Mode Transition with Turbine-Driven Auxiliary Feedwater Pump 1-1 Inoperable | Regarding Mode Transition with Turbine-Driven Auxiliary Feedwater Pump 1-1 Inoperable | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-002, For Diablo Canyon, Unit 1, Regarding Single Failure Vulnerability of Unit 1 & 2 Auxiliary Building Ventilation System | For Diablo Canyon, Unit 1, Regarding Single Failure Vulnerability of Unit 1 & 2 Auxiliary Building Ventilation System | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-003, Regarding Deviation from License Condition for Physical Protection Due to Tsunami Events | Regarding Deviation from License Condition for Physical Protection Due to Tsunami Events | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-004-01, 1 for Diablo, Unit 1, Regarding Emergency Diesel Generator Actuated Upon 230 Kv Isolation Due to Maintenance Activities on Relay Panel | 1 for Diablo, Unit 1, Regarding Emergency Diesel Generator Actuated Upon 230 Kv Isolation Due to Maintenance Activities on Relay Panel | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-004, For Diablo Canyon Power Unit 1, Regarding Emergency Diesel Generators Actuated Upon 230-kV Isolation Due to Maintenance Activities on Relay Panel | For Diablo Canyon Power Unit 1, Regarding Emergency Diesel Generators Actuated Upon 230-kV Isolation Due to Maintenance Activities on Relay Panel | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-005-01, 1 for Diablo Canyon Unit 1, Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electrical Maintenance Testing Activities | 1 for Diablo Canyon Unit 1, Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electrical Maintenance Testing Activities | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-005, For Diablo Canyon Power Plant, Unit 1 - Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electric Maintenance Testing Activities | For Diablo Canyon Power Plant, Unit 1 - Emergency Diesel Generator Actuations Upon Loss of 230 Kv Startup Due to Electric Maintenance Testing Activities | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-006-01, Loss of Control Room Envelope Due to the Work Control Shift Foreman Incorrectly Authorizing Removal of a Blank Flange | Loss of Control Room Envelope Due to the Work Control Shift Foreman Incorrectly Authorizing Removal of a Blank Flange | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-006, For Diablo Canyon, Unit 1, Regarding Loss of Control Room Envelope Due to the Work Control Shift Foreman Incorrectly Authorizing Removal of a Blank Flange | For Diablo Canyon, Unit 1, Regarding Loss of Control Room Envelope Due to the Work Control Shift Foreman Incorrectly Authorizing Removal of a Blank Flange | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-007-02, Inadequate Control Room Envelope Testing Due to Inadequately-Documented In-leakage Test Data | Inadequate Control Room Envelope Testing Due to Inadequately-Documented In-leakage Test Data | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-007-01, Regarding Inadequate Control Room Envelope Testing Due to Inadequately - Documented In-leakage Test Data | Regarding Inadequate Control Room Envelope Testing Due to Inadequately - Documented In-leakage Test Data | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) | | 05000275/LER-2011-007, For Diablo Canyon, Unit 1, Inadequate Control Room Envelope Testing Due to Inadequately-Documented In-Leakage Test Data | For Diablo Canyon, Unit 1, Inadequate Control Room Envelope Testing Due to Inadequately-Documented In-Leakage Test Data | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) | | 05000275/LER-2011-008-01, Control Room Ventilation System Design Vulnerability | Control Room Ventilation System Design Vulnerability | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(viii)(B) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(ii)(8) | | 05000275/LER-2011-008, Regarding Control Room Ventilation System Design Vulnerability | Regarding Control Room Ventilation System Design Vulnerability | 10 CFR 50.73(a)(2)(iv)(A), System Actuation 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown 10 CFR 50.73(a)(2)(ix)(A), Prevented Safety Function in Multiple System 10 CFR 50.73(a)(2)(viii)(A) 10 CFR 50.73(a)(2)(i)(8) 10 CFR 50.73(a)(2)(v)(8) 10 CFR 50.73(a)(2)(ii)(8) 10 CFR 50.73(a)(2)(viii)(8) |
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