05000237/LER-1979-016, Forwards LER 79-016/01T-0

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Forwards LER 79-016/01T-0
ML17173A742
Person / Time
Site: Dresden Constellation icon.png
Issue date: 04/06/1979
From: Stephenson B
COMMONWEALTH EDISON CO.
To: James Keppler
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
Shared Package
ML17173A743 List:
References
79-311, NUDOCS 7904160170
Download: ML17173A742 (3)


LER-1979-016, Forwards LER 79-016/01T-0
Event date:
Report date:
2371979016R00 - NRC Website

text

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CommoAalth Edison Dresden Nuclear Power Station R.R. #1 Morris, Illinois 60'\\50 Telephone 815/942-2920 BBS Lt;r. /179-311 April 6,.1979 James G. Keppler, Regional Director Directdrate of Regulatory Operations - Region III U.S. Nuclear Regulatory Commission 799 Roosevelt Road Glen-Ellyn, IL 60137

  • Reportable Occurrence Report #79-16/0lT-0, Docket # 050-237 is hereby submitted to your office in accordance with Dresden Nuclear Power Station Technical Specification 6.6.B.1.(C),

abnormal degradation discovered in fuel cladding, reactor coolant pressure boundary, or.primary containment.

BBS/kmh Enclosure en Station Superintendent

_Dresden Nuclear Power Station CC:

Director of Inspection & Enforcement Director of Management Information & Program Control File/NRC REGUU\\10RY DOCl\\ET FIL£ COPY, 7904160 \\/O

ATTACHMENT TO LICENSEE EVENT REPORT 79-016/0lT-0.

COMMONWEALTH EDISON COHPANY (CWE)

DRESDEN UNIT 2 * (ILDRS-2)

DOCKET II 050-237 During the current refueling outage, workers discovered water dripping from an elbow on a drain line from the bottom of LPCI testable check valve 2-1501-25.

All leakage was contained inside the drywell and directed to the Drywell Floor Drain System.

Upon further investigation the leakage was determined to be coming from a crack in.the weld on the elbow.

The weld was cracked 360° around the pipe..

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Calculations showed that a complete severance of a l" line such as this*

would be well within the capabilities of ECCS systems.

The defective weld was ground out, repaired and dy.e. penetrant tested following approved procedures; The weld failure was apparently* due to an improper pipe fitup prior to welding* the. pipe originally i.e., pipe bottomed out in the socket..

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!During refueling, water was discovered to be dripp.ing from an elbow in the drain line 1 [2JI] ion a LPCI check valve.

This event was of minimal safety significance because all leak-J J j CQ:0 !age was contained in the Drywell Floor Drain System and the potential leakage, con-i []J:IJ 1sidering a complete severance of the l" line is well within the capabilities of the

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Previous occurrence reported as R.O. #50-237/1977-10

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ATTACHMENT.

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Defective weld was ground out, repaired IJ))] 1and dye-penetrant tested in accordance with approved procedures.

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