05000244/LER-1980-010-03, /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired

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/03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired
ML17309A114
Person / Time
Site: Ginna 
Issue date: 12/23/1980
From: Spector S
ROCHESTER GAS & ELECTRIC CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML17250A837 List:
References
LER-80-010-03L, LER-80-10-3L, NUDOCS 8012300525
Download: ML17309A114 (2)


LER-1980-010, /03L-0:on 801125,pinhole Leak Found in Weld on RHR Thermowell.Caused by Poor Quality Weld.Weld Repaired
Event date:
Report date:
2441980010R03 - NRC Website

text

4 U. S. NUCLEAR REGULATORYCOMMISSION 80-010/03L-0 LICENSEE EVENT REPORT (CAR 1275)

QI (PLEASE PRINT OR TYPE ALLREQUIRED INFORMATION) 6 Qs

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1 QE~QE LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 NRC FC 366 I7.77) system.

This constitutes a degradation of a system designed to contain radioactive

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a lternate discharge to RCS, and at lea st one steam generator wa s available CONTROL BLOCK:

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8 60 61 DOCKET NUMBER 68 69 EVENT DATE 74 75 REPORT DATE 80 EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO

~o2 During a unit'hutdown a pinhole leak tva s found in the weld of a thermowell on the RHR

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0 21 22 23 24 26 27 28 29 30 31 32 ACTION FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDQ PRIME COMP.

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The initial weld was of poor quality and is believed to be the reason for the leak.

The weld was repaired to current standards.

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80 80 80 45 80 80 80 NRC USE ONLY 68 69 80 Ts oN E 3 1 5 5 2 4 4 4 4 6, ext ~ 2 1 4 S. M. Spector NAME OF PREPARER 7

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FACILITY

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DISCOVERY DISCOVERY DESCRIPTION Q32

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10 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION Q39

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11 12 13 PERSONNEL INJURIES 7

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11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE

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