05000220/LER-1979-020-03, /03L-0:on 790901,during Steady State Operation, Drywell Cooler 14 Tripped & Leakage Increased to Above Five G/Minute.Caused by Cooler Tube Leak.Cooler Isolated & Returned to Acceptable Level.Shutdown Terminated

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/03L-0:on 790901,during Steady State Operation, Drywell Cooler 14 Tripped & Leakage Increased to Above Five G/Minute.Caused by Cooler Tube Leak.Cooler Isolated & Returned to Acceptable Level.Shutdown Terminated
ML18037A198
Person / Time
Site: Nine Mile Point 
Issue date: 09/10/1979
From: Duda E
NIAGARA MOHAWK POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML18037A196 List:
References
LER-79-020-03L, LER-79-20-3L, NUDOCS 7909170521
Download: ML18037A198 (2)


LER-1979-020, /03L-0:on 790901,during Steady State Operation, Drywell Cooler 14 Tripped & Leakage Increased to Above Five G/Minute.Caused by Cooler Tube Leak.Cooler Isolated & Returned to Acceptable Level.Shutdown Terminated
Event date:
Report date:
2201979020R03 - NRC Website

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60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO Durin stead state o eration No.

14 Dr well Cooler tri QB 74 75 REPORT DATE 80 d and dr 11 QB leaka e increased to above five m. Since dr well coolers are su lied b

Reactor Bui 1 din Cl osed Loo Cool in it was a

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an accpetable level, the shutdown 3

DISCOVERY DESCRIPTION Q32 Equi pment failure METHOD OF DISCOVERY

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