LER-1980-001, /01T-0:on 800107,in Mode 1,determinted That Plant Was Taken Into Operational Mode While in Action Statement of Limiting Condition for Operation.Caused by Personnel Error.Revision to Tech Specs Has Been Submitted |
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This is the second occurrence of this type reported.
Reference LER 79-72.
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8001290
SUPPLEMENTARY INFORMATION Report Number:
50-302/80-001/0lT-0 Facility:
Crystal River Unit #3 Report Date:
14 January 1980 Occurrence Date:
7 January 1980 Identification of Occurrence:
Ascension into an operational mode while in an action statement of a limiting condition for operation.
This event is contrary to Technical Specification 3.0.4.
Conditions Prior to Occurrence:
Mode 1 power operation (1007.)
Description of Occurrence:
At 1200 it was determined that the plant had entered into an operational mode while in an action statement of a limiting condition for operation.
The plant entered into Mode 2 at 2348 on 5 January 1980 and ascended into power operation while pres-surizer steam space sample isolation valve CAV-1 was declared inoperable.
Designation of Apparent Cause:
The cause of the event is attributed to personnel error.
The event resulted from an extension of a previous interpretation of the intent of Technical Specification 3.0.4 Analysis of Occurrence:
The penetration affected by the failure of CAV-1 was isolated as per the action statement requirements of Technical Speci-fication 3.6.3.1; therefore, the health and safety of the public were not endangered as a result of this event.
Corrective Action
A management meeting was held with the Plant Manager to review this event to prevent recurrence. A revision to Tech.ical Specification has been submitted to the NRC with a req.est for expeditious review that will delete the requirements of Section 3.0.4 for selected containment isolation valves.
Technical Specification change request #57 was submitted as follows:
A. "For ACTION statements b and c of Specification 3.6.3, add a footnote to read:
'These valves may be reopened on an intermit-tent basis under administrative control for up to four (4) hours in any 24-hour period as necessary for sampling or surveillance testing'."
B. Add ACTION statement e to read: "The provisions of Specification 3.0.4 are not applicable to those valves in Table 3.6-1 annotated 1821f287
SUPPLEMENTARY INFORMATION 14 Jan. 1980
Corrective Action
(Cont'd)
- 3. by double asterisks (**)."
Double asterisks have been added to appropriate valves in Table 3.6-1.
C. Add asterisk note to Table 3.6-1 to read: "May be opened on an intermittent basis under administrative control." Asterisks have been added to appropriate valves in Table 3.6-1.
REASON FOR THE PROPOSED CHANCE:
A. ACTION statements b and c of Specification 3.6.3.1 require penetrations with one or more inoperable isolation valves (s) to be isolated. However, other specifications renuire cycling of the valves used to complete the isolation for either sur-veillance testing or to draw samples to complete required analyses.
It is for this reason that the footnote has been proposed.
B. ACTION e has been proposed for Specification 3.6.3.1 for valves that, if they are inoperable and ACTION Statement b or c is in effect, aia in their post-containment isolation configuration.
Since these valves are already in their post-containment isolation configuration, they neither perform an emergency core cooling function, nor offer any hindrance to normal plant operations while shut or isolated.
There is no reason to restrain the entry into other OPERATIONAL MODES.
Therefore, the exception to the provisions of Specificction 3.0.4 is proposed.
C. The Table note is being proposed to Table 3.6-1 because there are times in MODES 1,2,3, and 4 that it is necessary to cycle these manual valves to perform surveillance, draw samples, or support entry into the containment. Additionally, this note is currently included in B&W Standard (NUREG-0103, Rev. 3).
Failure Data:
This is the second occurrence of this type reported.
Reference LER 79-72.
/rc 182(l 288
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| 05000302/LER-1980-001-01, /01T-0:on 800107,in Mode 1,determinted That Plant Was Taken Into Operational Mode While in Action Statement of Limiting Condition for Operation.Caused by Personnel Error.Revision to Tech Specs Has Been Submitted | /01T-0:on 800107,in Mode 1,determinted That Plant Was Taken Into Operational Mode While in Action Statement of Limiting Condition for Operation.Caused by Personnel Error.Revision to Tech Specs Has Been Submitted | | | 05000302/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000302/LER-1980-002-03, /03L-0:on 800105,following Normal Reactor Shutdown,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Leaking Fuel Pins & Anticipated Iodine Transient Following Shutdown | /03L-0:on 800105,following Normal Reactor Shutdown,Chem/Rod Sampling Revealed Reactor Coolant Dose Equivalent I-131 Exceeded Tech Spec Limit.Caused by Leaking Fuel Pins & Anticipated Iodine Transient Following Shutdown | | | 05000302/LER-1980-002, Forwards LER 80-002/03L-0 | Forwards LER 80-002/03L-0 | | | 05000302/LER-1980-003, Forwards LER 80-003/03L-0 | Forwards LER 80-003/03L-0 | | | 05000302/LER-1980-003-03, /03L-0:on 800104,following Pressurizer Degassification Operations,Pressurizer Steam Space Sample Isolation Valve CAV-1 Would Not Close.Cause Unknown.Threads on Valve Stem Assembly Found Stripped.Evaluation Scheduled | /03L-0:on 800104,following Pressurizer Degassification Operations,Pressurizer Steam Space Sample Isolation Valve CAV-1 Would Not Close.Cause Unknown.Threads on Valve Stem Assembly Found Stripped.Evaluation Scheduled | | | 05000302/LER-1980-004, Supplemental Info to LER 80-004/04L-0:during Jan 1980, Analyses of Seawater Samples Collected at Six Sample Stations Not Performed Correctly Due to Equipment Malfunctions.Samples Recollected & Analyzed | Supplemental Info to LER 80-004/04L-0:during Jan 1980, Analyses of Seawater Samples Collected at Six Sample Stations Not Performed Correctly Due to Equipment Malfunctions.Samples Recollected & Analyzed | | | 05000302/LER-1980-005-03, /03L-0:on 800116,during Surveillance Schedule Review,Discovered Incore Neutron Detector Sys Calibr Surveillance SP-140 Not Performed within Required Time Interval.Caused by Misinterpretation of Requirements | /03L-0:on 800116,during Surveillance Schedule Review,Discovered Incore Neutron Detector Sys Calibr Surveillance SP-140 Not Performed within Required Time Interval.Caused by Misinterpretation of Requirements | | | 05000302/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000302/LER-1980-006-03, /03L-0:on 800123,during Routine Surveillance, Reactor Bldg Charcoal Filter Bank Efficiency Was Less than 99%.Caused by Natural End of Life for Filter.Filters Replaced | /03L-0:on 800123,during Routine Surveillance, Reactor Bldg Charcoal Filter Bank Efficiency Was Less than 99%.Caused by Natural End of Life for Filter.Filters Replaced | | | 05000302/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000302/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000302/LER-1980-007-03, /03L-0:on 800130,during Daily Plant Operating Surveillance SP-300,discovered Average Reactor Bldg Temp of 130.5F.Caused by Temp Transmitter CI-563-TT Being Stuck,Due to Operation Outside Design Temp Range | /03L-0:on 800130,during Daily Plant Operating Surveillance SP-300,discovered Average Reactor Bldg Temp of 130.5F.Caused by Temp Transmitter CI-563-TT Being Stuck,Due to Operation Outside Design Temp Range | | | 05000302/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000302/LER-1980-008-03, /03L-0:on 800206,during ECCS Pump Operability Demonstration Surveillance SP-340,decay Heat Pump a Discharge Throttle Valve Would Not Control Flow Automatic Phase.Caused by Loose Wires on auto-manual Selector Switch | /03L-0:on 800206,during ECCS Pump Operability Demonstration Surveillance SP-340,decay Heat Pump a Discharge Throttle Valve Would Not Control Flow Automatic Phase.Caused by Loose Wires on auto-manual Selector Switch | | | 05000302/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000302/LER-1980-009-03, /03L-0:on 800209,following Power Reduction & on 800211,during Startup Operations,Rcs Sampling Revealed Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel Pins & Iodine Transient Following RCS Transient | /03L-0:on 800209,following Power Reduction & on 800211,during Startup Operations,Rcs Sampling Revealed Dose Equivalent I-131 Exceeded Tech Specs.Caused by Leaking Fuel Pins & Iodine Transient Following RCS Transient | | | 05000302/LER-1980-010-01, /01T-1:on 800226,during Routine Operation,Power Supply Failure Initiated Transient Condition,Resulting in Reactor Trip,Turbine Trip & Engineered Safeguards Actuation. Caused by Failure of Nni Voltage Buffer Card 4-7-10(4) | /01T-1:on 800226,during Routine Operation,Power Supply Failure Initiated Transient Condition,Resulting in Reactor Trip,Turbine Trip & Engineered Safeguards Actuation. Caused by Failure of Nni Voltage Buffer Card 4-7-10(4) | | | 05000302/LER-1980-010, Forwards LER 80-010/01T-1 | Forwards LER 80-010/01T-1 | | | 05000302/LER-1980-011-04, /04L-0:on 800222,discovered Representative Sample Not Obtained for Feb from Test Well 4,contrary to Tech Spec. Apparently Caused by Intake Canal Mod Const Activity.Tech Spec Change Request Will Be Submitted to Delete Require | /04L-0:on 800222,discovered Representative Sample Not Obtained for Feb from Test Well 4,contrary to Tech Spec. Apparently Caused by Intake Canal Mod Const Activity.Tech Spec Change Request Will Be Submitted to Delete Requirement | | | 05000302/LER-1980-011, Forwards LER 80-011/04L-0 | Forwards LER 80-011/04L-0 | | | 05000302/LER-1980-012, Forwards LER 80-012/04L-0 | Forwards LER 80-012/04L-0 | | | 05000302/LER-1980-012-04, /04L-0:on 800229,discovered That Environ Samples Were Not Taken from Locations at Required Frequencies.Caused by Personnel Error.Incident Occurrence Infrequent Therefore No Corrective Actions Necessary | /04L-0:on 800229,discovered That Environ Samples Were Not Taken from Locations at Required Frequencies.Caused by Personnel Error.Incident Occurrence Infrequent Therefore No Corrective Actions Necessary | | | 05000302/LER-1980-013, Forwards LER 80-013/04L-0 | Forwards LER 80-013/04L-0 | | | 05000302/LER-1980-013-04, /04L-0:on 800304,more than Two Std Deviations Were Discovered Between Preoperational Study & Operational Study in Metabolic Function of Discharge Salt Marshes.Possibly Caused by Natural or Seasonal Variations | /04L-0:on 800304,more than Two Std Deviations Were Discovered Between Preoperational Study & Operational Study in Metabolic Function of Discharge Salt Marshes.Possibly Caused by Natural or Seasonal Variations | | | 05000302/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000302/LER-1980-015-03, /03L-0:on 800306,while Performing Engineered Safeguards Functional Test,Decay Heat Suction Isolation Valve Began to Close Inadvertently.No Apparent Cause for Event.Investigation Underway | /03L-0:on 800306,while Performing Engineered Safeguards Functional Test,Decay Heat Suction Isolation Valve Began to Close Inadvertently.No Apparent Cause for Event.Investigation Underway | | | 05000302/LER-1980-016-01, /01T-0:on 800401,inadvertent Actuation of Fire Svc Deluge Sys Resulted in Damage to Auxiliary Bldg Ventilation Exhaust Filter AHFL-2A.Caused by Personnel Error During Reset of Fire Svc Panel alarm.AHFL-2A Media Replaced | /01T-0:on 800401,inadvertent Actuation of Fire Svc Deluge Sys Resulted in Damage to Auxiliary Bldg Ventilation Exhaust Filter AHFL-2A.Caused by Personnel Error During Reset of Fire Svc Panel alarm.AHFL-2A Media Replaced | | | 05000302/LER-1980-016, Forwards LER 80-016/01T-0 | Forwards LER 80-016/01T-0 | | | 05000302/LER-1980-017-03, /03L-0:on 800405,during Repair of B once-through Steam Generator Feedwater swing-disc Check Valve FWV-46, Discovered Valve Disc Retainer Pin Missing.Caused by Deficiency Occurring During Initial Manufacturer Assembly | /03L-0:on 800405,during Repair of B once-through Steam Generator Feedwater swing-disc Check Valve FWV-46, Discovered Valve Disc Retainer Pin Missing.Caused by Deficiency Occurring During Initial Manufacturer Assembly | | | 05000302/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000302/LER-1980-018-03, /03L-0:on 800413,during Chemistry Surveillance, Discovered That RCS Chloride & Fluoride Concentrations Were 0.24 Ppm & 0.274 Ppm.Caused by Chloride & Fluoride Contamination on Walls & Floors of Fuel Transfer Canal | /03L-0:on 800413,during Chemistry Surveillance, Discovered That RCS Chloride & Fluoride Concentrations Were 0.24 Ppm & 0.274 Ppm.Caused by Chloride & Fluoride Contamination on Walls & Floors of Fuel Transfer Canal | | | 05000302/LER-1980-018, Fowards LER 80-018/03L-0 | Fowards LER 80-018/03L-0 | | | 05000302/LER-1980-019-01, /01T-0:on 800517,crack Indication Discovered During Insp of Fuel Assembly NJ018E Upper End Fitting Holddown Spring.Investigation of Cause Underway.When Determined,Rept W/Corrective Actions Will Be Sent | /01T-0:on 800517,crack Indication Discovered During Insp of Fuel Assembly NJ018E Upper End Fitting Holddown Spring.Investigation of Cause Underway.When Determined,Rept W/Corrective Actions Will Be Sent | | | 05000302/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000302/LER-1980-020-03, /03L-0:on 800501,during Review of Surveillance Procedures,Discovered That Procedure for Weekly Battery Check SP-510 Was Not Performed for Wk of 800406.Caused by Damaged Hydrometer Used to Perform Surveillance | /03L-0:on 800501,during Review of Surveillance Procedures,Discovered That Procedure for Weekly Battery Check SP-510 Was Not Performed for Wk of 800406.Caused by Damaged Hydrometer Used to Perform Surveillance | | | 05000302/LER-1980-020, Forwards LER 80-020/03L-0 | Forwards LER 80-020/03L-0 | | | 05000302/LER-1980-021-03, /03L-0:on 800506,during Insp of Feedwater swing- Disc Check Valve FWV-45,valve Hinge Pin Was Discovered Missing.Caused by Deficiency During Initial Assembly of Valve by Manufacturer.Valve Is Being Repaired | /03L-0:on 800506,during Insp of Feedwater swing- Disc Check Valve FWV-45,valve Hinge Pin Was Discovered Missing.Caused by Deficiency During Initial Assembly of Valve by Manufacturer.Valve Is Being Repaired | | | 05000302/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000302/LER-1980-022, Forwards LER 80-022/04L-0 | Forwards LER 80-022/04L-0 | | | 05000302/LER-1980-022-04, /04L-0:on 800528,samples Not Obtained for Apr from Test Wells 1 & 4 & Ph Results Not Reported for Waste Water Ponds,Test Well 5 & Discharge Canal.Caused by Elimination of Test Well Sites Due to Canal Mod & Loss of Ph Data | /04L-0:on 800528,samples Not Obtained for Apr from Test Wells 1 & 4 & Ph Results Not Reported for Waste Water Ponds,Test Well 5 & Discharge Canal.Caused by Elimination of Test Well Sites Due to Canal Mod & Loss of Ph Data | | | 05000302/LER-1980-023-03, /03L-0:on 800517,radioactive Matl in Form of Bagged Contaminated Waste & Poly Wrapped Scrap Lumber Was Taken to Site Dump.Caused by Apparent Communication Problem Between Health Physics Personnel & Bldg Servicemen | /03L-0:on 800517,radioactive Matl in Form of Bagged Contaminated Waste & Poly Wrapped Scrap Lumber Was Taken to Site Dump.Caused by Apparent Communication Problem Between Health Physics Personnel & Bldg Servicemen | | | 05000302/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000302/LER-1980-024, Forwards LER 80-024/04L-0 | Forwards LER 80-024/04L-0 | | | 05000302/LER-1980-024-04, /04L-0:on 800523,discovered That I-131 Charcoal Cartridge for Wk Ending 800401 Was Inadvertently Discarded. Caused by Personnel Error.Responsible Personnel Were Instructed on Proper Procedures | /04L-0:on 800523,discovered That I-131 Charcoal Cartridge for Wk Ending 800401 Was Inadvertently Discarded. Caused by Personnel Error.Responsible Personnel Were Instructed on Proper Procedures | | | 05000302/LER-1980-025-03, /03L-0:on 800609,while Performing SP-112 Calibr of Reactor Protection Sys,Count Rate Amplifier for Channel a Source Range Neutron Flux Monitor Found out-of-tolerance Caused by Defective Pulse & Output Amplifier Cards | /03L-0:on 800609,while Performing SP-112 Calibr of Reactor Protection Sys,Count Rate Amplifier for Channel a Source Range Neutron Flux Monitor Found out-of-tolerance Caused by Defective Pulse & Output Amplifier Cards | | | 05000302/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000302/LER-1980-026-03, /03L-0:on 800714,while Performing SP-710 Rc Decay Heat Removal & Rc Makeup Sys Chemistry Surveillance Program, Chloride & Fluoride Concentrations Exceeded Limits.Caused by High Temp of Decay Heat Sys & Migration of Elements | /03L-0:on 800714,while Performing SP-710 Rc Decay Heat Removal & Rc Makeup Sys Chemistry Surveillance Program, Chloride & Fluoride Concentrations Exceeded Limits.Caused by High Temp of Decay Heat Sys & Migration of Elements | | | 05000302/LER-1980-026, Forwards LER 80-026/03L-0 | Forwards LER 80-026/03L-0 | | | 05000302/LER-1980-027-01, /01T-0:on 800728,in Mode 5,while Performing OP-401 Core Flooding Sys,Check Valve CFV-79 Failed Allowing About 500 Gallons of Liquid to Enter Nitrogen Sys Via NGV-4. Apparently Caused by CFV-79 Failure & Open NGV-4 | /01T-0:on 800728,in Mode 5,while Performing OP-401 Core Flooding Sys,Check Valve CFV-79 Failed Allowing About 500 Gallons of Liquid to Enter Nitrogen Sys Via NGV-4. Apparently Caused by CFV-79 Failure & Open NGV-4 | |
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