05000348/LER-1979-052-03, /03L-0:on 791106,refueling Water Storage Tank Declared Inoperable When Water Vol Fell Below Tech Specs. Caused by Drift Problems on Level Transmitters.Transmitters Undergoing Repairs

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/03L-0:on 791106,refueling Water Storage Tank Declared Inoperable When Water Vol Fell Below Tech Specs. Caused by Drift Problems on Level Transmitters.Transmitters Undergoing Repairs
ML19262A941
Person / Time
Site: Farley Southern Nuclear icon.png
Issue date: 12/03/1979
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19262A938 List:
References
LER-79-052-03L, LER-79-52-3L, NUDOCS 7912110338
Download: ML19262A941 (1)


LER-1979-052, /03L-0:on 791106,refueling Water Storage Tank Declared Inoperable When Water Vol Fell Below Tech Specs. Caused by Drift Problems on Level Transmitters.Transmitters Undergoing Repairs
Event date:
Report date:
3481979052R03 - NRC Website

text

NRC FORM 366 U. S. NUCLEAR REGULATORY COMMISSION (7-77)

LICENSEE EVENT REPO.1T NTROL 8 LOCK: l l

l l

l (PLEASE PRINT OR TYPE ALL REQUIRED INFORMATION) 1 6

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7 8 9 UCENSEE CODE 14 15 LICENSE NUMBER 26 26 LICENSE TYPE JO 51 C A T 58 CON'T RTil IL @l 01 51 01 Oi 01 3 l 4 l 8 Gil ll [ 0 l 6 l 7 l 9 }@l 1 l 2 l 0 l 3 l 7 l 9 l@

5O RC 7

8 60 68 COCK ET NUMBER m

63 EVENT DA7E I4 75 REPOHT DATE d0 EVENT DESCRIPTION AND PROB ABLE CONSEQUENCES h lo 121 l At 1325 on 11/6/79, the Refueling Water Storace Tank (RWST) was declared inoperable lo la l l when it was determined that the water volume (456,279 2allons) was below the Tech.

l Soec. 3.5.5 limit of 471,000 gallons.

Tech. Soec. 3.5.5 action statement r ecu ire-l o

4 o

5 l ments were met.

The RWST level was restored to >471,000 callons by 1700 on 11/6/79. l Q W l The lalth and safety of the general public were not affected.

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7 8 9 80 SYSTEM

CAUSE

CAUSE COMP VALVE CODE CCCE SLBCOOE COMPONENT COCE S t.,8 C 0 0 E SUCCCOE Ls l r @ i xl@ l Z i@ l_1 x l S i r i a i u i@ i Ti@ 12 i@

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to 11 12 13 18 19 20 SEQUEN TI AL CCCU R R ENCE REFORT R E VISIO N LER RC EVENT YEAR REPORT NO.

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J6 Je 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS i

o lAs a result of the initiation of a RWFT low level alarm (<471.000 ent!ansT d ich was I

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lat variance with the RWST level indicators (>471.000 Tallons)., troubleshoord--

I lcffort revealed that one level transmitter had drif ted low and the cther transmitter i

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. B l was exhibitine uncorrectable drif t problems.

One level transmit ter was returned to l

l service on 11/9/79 and the other transmitter will be renaired when narts are availablel -

4 8 3 80 STA S

% PCWER OTHER STATUS ISCO RY DISCOVERY DESCRIPTION l F l@ l 0 l 4 l 5 l@

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12 80 LOSS OF OH OAMAGE TO F ACILITY TYPE

DESCRIPTION

NA 7912110 4

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8 9 10 80 y ISSUE @[ ESCRIPTION NA l

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NAME OF PREPARER PHONE:

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