LER-1980-011, Following Two Plant Trips & Shutdown,Daddle Clamp Bolts for Two Hangars Were Found Broken.Both Hangers Are Hydraulic Snubbers.Failures Caused by Combination of Fatigue & High Impact Loading |
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| 3361980011R03 - NRC Website |
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EVEN1 oESCRIPTioN ANo PRoBABt.E CoNSEQUENCCs Following a full power plant trip 13/80), 2 broken saddle clamp bolts l
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Following a se.cond trip (3/22/80), an additional p-
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Following a plant shutdown g
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Both hangers j
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36 37 40 41 42 43 44 47 33 CAUSE oESCRIPTION ANo CORRECTIVE ACTIONS All failures were a combination of fat.igue and high impact loading.
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stop valves were replaced with high strength bolts for high temperature ' service i,
( ASME A-193i Grade B7). The improved fatigue characteristics of this low-alloy p;-) l steel should prevent a recurrence.
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ATTACHMENT LER 80-11/3L-2 Millstone Unit 0 4
1 Docket No.50-33c 1
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EVENT DESCRIPTION
1 During power ascension on 3/13/80 following a full power plant trip, two broken pipe saddle clamp bolts were found on hydraulic snubber hanger 490008. This hanger is located on a main steam lead prior to the HP turbine. The plant was at 30% power and the power ascension was halted until the broken bolts (1-1/2" UNF capscrews) were replaced. All other hangers on the HP turbine steam leads were inspected satisfactorily.
Following another full power trip, with the plant at 99% powe.r on 3/22/80, a broken saddle clamp bolt was found on hydraulic snubber hanger 490002.
The bolt (1-3/4" UNC machine bolt) was replaced and inspection revealed no other broken bolts on similar hangers. Both bolts were carbon steel.
Following a plant shutdown, including a turbine trip, on 5/08/80 the second saddle clamp bolt on hydraulic snubber hanger 490002 was found broken. At this time the carbon steel bolts on all similar saddle clamps were replaced with "1cw alloy steel bolting material for high temperature service" (ASME A-193, Grade 87).
These events resulted in declaring hangers 490008 and 490002 inoperable and the plant was operated in accordance with Technical Specification Action Statement 3.7.8.1 in each case.
CAUSE DESCRIPTION The bolt failures were caused by fatigue of the low carbon steel material.
In each case, the final failure was a result of the impact loading of the turbine stop and control valves tripping.
All saddle clamp bolts on similar hangers restraining the steam leads downstream of the turbine stop valves were replaced. The replacement bolting is low alloy steel bolting for high temperature service. (ASME A-193, Grade B7). The improved fatigue characteristics of this material should prevent recurrence.
There are no safety implications from these events in that these pipe supports are provided for a non-safety related purpose.
The or'iginal hydraulic snubber Technical Specification submittal included all snubbers in the plant. A change is pending to include only safety-related snubbers.
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| 05000245/LER-1980-001-03, /03L-0:on 800103,runback of Recirculation Pump a Resulted in Pump Speed Mismatch Greater than 10%.Resulted in Possible Error in LPCI Loop Selection Logic.Caused by Electronic Saturation.Sys Mods Being Considered | /03L-0:on 800103,runback of Recirculation Pump a Resulted in Pump Speed Mismatch Greater than 10%.Resulted in Possible Error in LPCI Loop Selection Logic.Caused by Electronic Saturation.Sys Mods Being Considered | | | 05000245/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000336/LER-1980-001, Forwards LER 80-001/03L-0 | Forwards LER 80-001/03L-0 | | | 05000336/LER-1980-001-03, /03L-0:on 800118,during Routine Insurance Insp Testing W/Plant at 100% Power,Turbine Driven Auxiliary Feedwater Pump Became Inoperable Due to Failure of Turbine Inboard,Outboard & Thrust Bearings.Caused by Excessive Wear | /03L-0:on 800118,during Routine Insurance Insp Testing W/Plant at 100% Power,Turbine Driven Auxiliary Feedwater Pump Became 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Tested.New Alignment Procedure Being Investigated | /03L-0:on 800121,during Routine Surveillance, Setpoint of One Main Steam Line High Flow Switch Higher than Allowed.Caused by Setpoint Drift.Switch Adjusted & Tested.New Alignment Procedure Being Investigated | | | 05000245/LER-1980-004, Forwards LER 80-004/03L-0 | Forwards LER 80-004/03L-0 | | | 05000336/LER-1980-005-01, /01T-0:on 800311,during Review of Safety Analysis, Discovered Incorrect Assumption Was Made in Analysis of Mode 5 Boron Dilution Event.Caused by Failure to Consider Operation W/Rcs Drained to Centerline of Hot Leg | /01T-0:on 800311,during Review of Safety Analysis, Discovered Incorrect Assumption Was Made in Analysis of Mode 5 Boron Dilution Event.Caused by Failure to Consider Operation W/Rcs Drained to Centerline of Hot Leg | | | 05000336/LER-1980-005, Forwards LER 80-005/01T-0 | Forwards LER 80-005/01T-0 | | | 05000245/LER-1980-005-03, /03L-0:on 800220,one Core Spray Subsystem Was Declared Inoperable,Resulting in Operation in Degraded Mode. Caused by Water Hammer Damage Due to Seat Leakage from Core Spray Injection & Check Valves.Pipe Supports Repaired | /03L-0:on 800220,one Core Spray Subsystem Was Declared Inoperable,Resulting in Operation in Degraded Mode. Caused by Water Hammer Damage Due to Seat Leakage from Core Spray Injection & Check Valves.Pipe Supports Repaired | | | 05000245/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000336/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000336/LER-1980-006-03, /03L-0:on 800310,w/charging Pump B Inoperable for Replacement,Charging Pump C Placed Out of Svc to Replace Failed Pump Packing.Caused by Natural end-of-life of Packing Due to Wear.Pump Packing Replaced | /03L-0:on 800310,w/charging Pump B Inoperable for Replacement,Charging Pump C Placed Out of Svc to Replace Failed Pump Packing.Caused by Natural end-of-life of Packing Due to Wear.Pump Packing Replaced | | | 05000245/LER-1980-006-03, /03L-0:on 800407,during Normal Operation,Pressure Indicating Switch That Senses Drywell Pressure for Automatic Pressure Relief Sys Logic Initiation,Found Isolated.Caused by Personnel Error.Switch Returned to Svc | /03L-0:on 800407,during Normal Operation,Pressure Indicating Switch That Senses Drywell Pressure for Automatic Pressure Relief Sys Logic Initiation,Found Isolated.Caused by Personnel Error.Switch Returned to Svc | | | 05000245/LER-1980-006, Forwards LER 80-006/03L-0 | Forwards LER 80-006/03L-0 | | | 05000336/LER-1980-007-03, /03L-0:on 800227,during Reactor Plant Startup, Condensate Storage Tank Level Fell Below Tech Spec Limit for Less than 30 Minutes.Caused by Excessive Water Demand from Blowdown & Regeneration Requirements | /03L-0:on 800227,during Reactor Plant Startup, Condensate Storage Tank Level Fell Below Tech Spec Limit for Less than 30 Minutes.Caused by Excessive Water Demand from Blowdown & Regeneration Requirements | | | 05000336/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000245/LER-1980-007-03, /03L-0:on 800516,discovered That Semiannual Functional Test of Cable Vault Smoke Detection Sys Had Been Overlooked.Caused by Test Not Being Listed on Unit Surveillance Schedule.Verification of Schedules Performed | /03L-0:on 800516,discovered That Semiannual Functional Test of Cable Vault Smoke Detection Sys Had Been Overlooked.Caused by Test Not Being Listed on Unit Surveillance Schedule.Verification of Schedules Performed | | | 05000245/LER-1980-007, Forwards LER 80-007/03L-0 | Forwards LER 80-007/03L-0 | | | 05000336/LER-1980-008-03, /03L-0:on 800303,during Routine Operations,Plant Computer Analog Input Values Became Erratic Rendering Pulse Counting Position Indication Sys Inoperable.Caused by Faulty Analog Input Driver Card.Sys Restored | /03L-0:on 800303,during Routine Operations,Plant Computer Analog Input Values Became Erratic Rendering Pulse Counting Position Indication Sys Inoperable.Caused by Faulty Analog Input Driver Card.Sys Restored | | | 05000336/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000245/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000245/LER-1980-008-03, /03L-0:on 800605,during Routine Surveillances, Found Pressures Switches 263-52C & 263-54A Tripped Outside Allowable Tech Spec.Caused by Setpoint Drift.Pressure Switches Reset to Required Setpoints | /03L-0:on 800605,during Routine Surveillances, Found Pressures Switches 263-52C & 263-54A Tripped Outside Allowable Tech Spec.Caused by Setpoint Drift.Pressure Switches Reset to Required Setpoints | | | 05000245/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000245/LER-1980-009-03, /03L-0:on 800605,during Routine Surveillance,Found Pressure Switch 263-55C Tripped Outside Allowable Setpoint. Caused by Setpoint Drift.Pressure Switch Reset to Required Setpoint | /03L-0:on 800605,during Routine Surveillance,Found Pressure Switch 263-55C Tripped Outside Allowable Setpoint. Caused by Setpoint Drift.Pressure Switch Reset to Required Setpoint | | | 05000336/LER-1980-009-03, /03L-0:on 800321,following Plant Trip from 100% Power,A Auxiliary Feed Pump Was Found Leaking Excessively from Gland Packing.Caused by Natural End of Life for Pump Packing.Pump Repacked | /03L-0:on 800321,following Plant Trip from 100% Power,A Auxiliary Feed Pump Was Found Leaking Excessively from Gland Packing.Caused by Natural End of Life for Pump Packing.Pump Repacked | | | 05000336/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000245/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000245/LER-1980-010-03, /03L-0:on 800613,during Testing of Penetration Anchor X-45 Base Plate Bolts,One Bolt Broke & Others Found Improperly Installed.Cause Not Stated.Bolts Removed & Replaced | /03L-0:on 800613,during Testing of Penetration Anchor X-45 Base Plate Bolts,One Bolt Broke & Others Found Improperly Installed.Cause Not Stated.Bolts Removed & Replaced | | | 05000336/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000336/LER-1980-010-03, /03L-0:on 800310,during Surveillance,Control Element Assembly Exhibited Erratic Position Indication & Was Declared Inoperable.Caused by Intermittent Open Conductor in Cable or Connector from Reed Switch | /03L-0:on 800310,during Surveillance,Control Element Assembly Exhibited Erratic Position Indication & Was Declared Inoperable.Caused by Intermittent Open Conductor in Cable or Connector from Reed Switch | | | 05000245/LER-1980-011-01, /01T-0:on 800803,both Air Ejector Offgas Sys Radiation Monitors Found Inoperable.Caused by Sample Line Manual Stop Valve Being Closed.Valve Did Not Appear on Sys Valve Lineup List.Valve Added to List | /01T-0:on 800803,both Air Ejector Offgas Sys Radiation Monitors Found Inoperable.Caused by Sample Line Manual Stop Valve Being Closed.Valve Did Not Appear on Sys Valve Lineup List.Valve Added to List | | | 05000245/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000336/LER-1980-011-03, /03L-0:on 800313,following Full Power Plant Trip, Two Broken Saddle Clamp Bolts Were Found on Hydraulic Snubber Hanger 490008 on Ms Lead to HP Turbine.Caused by Fatigue Cracking Due to High Vibration & Shear on Trips | /03L-0:on 800313,following Full Power Plant Trip, Two Broken Saddle Clamp Bolts Were Found on Hydraulic Snubber Hanger 490008 on Ms Lead to HP Turbine.Caused by Fatigue Cracking Due to High Vibration & Shear on Trips | | | 05000336/LER-1980-011, Forwards LER 80-011/03L-0 | Forwards LER 80-011/03L-0 | | | 05000336/LER-1980-012-03, During Power Operation, Hydraulic Snubber on Hangar 490001 Found W/No Visible Fluid Level.Caused by Seal Deterioration.Snubber Replaced | During Power Operation, Hydraulic Snubber on Hangar 490001 Found W/No Visible Fluid Level.Caused by Seal Deterioration.Snubber Replaced | | | 05000336/LER-1980-012, Forwards Updated LER 80-012/03X-1 | Forwards Updated LER 80-012/03X-1 | | | 05000245/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000245/LER-1980-012-03, /03L-0:on 800725,while Performing Routine Surveillance,Average Power Range Monitor (APRM) Channel 5 Was Reading 10% Below Tech Spec.Cause Unstated.Aprm Adjusted to Proper Value & Observed to Insure Stable Reading | /03L-0:on 800725,while Performing Routine Surveillance,Average Power Range Monitor (APRM) Channel 5 Was Reading 10% Below Tech Spec.Cause Unstated.Aprm Adjusted to Proper Value & Observed to Insure Stable Reading | | | 05000336/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000245/LER-1980-013-03, /03L-0:on 800905,during Drywell High Pressure Scram & Containment Isolation Functional & Calibr Test, Pressure Switch 2206-1621B Tripped Outside Allowable Band. Caused by Setpoint Drift.Switch Tested & Returned to Svc | /03L-0:on 800905,during Drywell High Pressure Scram & Containment Isolation Functional & Calibr Test, Pressure Switch 2206-1621B Tripped Outside Allowable Band. Caused by Setpoint Drift.Switch Tested & Returned to Svc | |
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