LER-1978-027, /01T-0:on 780511,B&W Found to Apply to CR-3 Incore Instruments Sys.Caused by Insufficienct Data from Prototype Studies.Corrective Actions Will Be Forwarded in Revision 1 to LER |
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| 3021978027R01 - NRC Website |
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lThis will confirm a report made to Mr. R. H.Wess=mn of your off4r.. s t-I o
r.u ni i 1515 on 11 May 1978.
At 1400. it was determined that a letter received I
from B&W on 8 May 1978 concerning uncertainties associated with incore g
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instruments does apply to CR-3.
Redundancy NA.
No hazard to the nealth j
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sitoil Cause of this event has been determined to be insufficient data from i
m I prototype incore instrument studies. Corrective Actions are presentiv i
gi being formulated and will be forwarded in a revision to this report.
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(SEE ATTACllED SUPPLEMENTAP.Y INFOPETION S11EET)
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SUPPLEMENTARY INFORMATION 4
1.~
'rt No.:
50-302/78-027/01T-0 Y
2.
viility:
Crystal River Unit #3 3.
Rep:rt Date:
12 May 1978 l4 Occurrence Date:
11 May 1978
, 5.
Id:ntification of Occurrence:
The values stated in Technical Speicifcation 3.2.1, Figure 3.2-1 & 3.2.4, Table 3.2-2 are believed to be non-conservative, as determined by B&W instituted program.
- 6.
Conditions Prior to Occurrence:
Mode 6 refueling.
7.
D:scription of occurrence:
b At 1400 it was determined that a letter received from B&W on 8 May 1978 does apply to CR-3 incore instruments systems.
The letter states in part:
S The initial error analysis for quadrant tilt and imbalance values derived from incore detector system signals was performed by B&W in 1974 based upon data obtained from
]
prototype detectors.
The results of the study were used to develop a tilt and imbalance error analysis for operating limits. As a result of concern expressed about these un-certainties based upon observed operational characteristics, B&W instituted a program early in 1978 to reevaluate the uncertainties using operating data.
Based upon incore detector performance at B&W operating plants, particularly in terms of quadrant power tilt measurement, it was proposed that the present uncertainty allowances for tilt and' imbalance might be insufficient.
Thus, the individual detector uncertainty value from currently available data was used in statistical analyses to determine the uncertainties which should be applied to the limiting quadrant tilt and imbalance values.
i The reinvestigation of the quadrant power tilt uncertainty found that the previous uncertainty values are too small and should be increased. The new uncertainty values are too small and should be increased.
The new uncertainty values are a function of both the individual incore detector signal uncertainty and the tilt limits. Table 1 gives the new tilt alarm limits corresponding to the existing actual Tech Spec limits for Crystal River #3.
The reinvestigation of uncertainties also led to increased uncertainties associated with imbalance. Tables 2 and 3 give the new imbalance alarm'setpoints for B&W operating plants corresponding to the approved technical specification limits for the current cycle of operation.
- 8.
Dasignation of Apparent Cause:
Cause of this event is due to insufficient data from prototype studies.
19.
ysis of occurrence:
d No hazard to the health and safety of plant or public as plant is defueled.
1
4 Supplementary Information
<tt No. 50-302/78-027/01T-0
~
1 2
10.
Corrective Action
Corrective actions are currently being formulated by CR-3 plant staff and B&W. Upon
- .w.letion, a revision to the report will be forwarded, 11.
Fa11urt Data:
First occurrence of an event of this' type, i
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TABLE 1 y
quadrant Tilt Lirrilts and Setpoints Alarm Setooints
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Tech Spec Full Symmetric Minimum Symrretric Ou t-o f-Co re Plant Limit (Actual Tilt)
System System System Crys tal River-3*
4.92 2.27 f.90 1.85 11.07 7.77 4.40 6.85 4
Changes required in Technical Speci fication. Table 3.2-2.
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f CRYSTAL RIVER-3 CYCLE 1 FR.0M 269 TO 40 3 EFP D
- ERROR ADJLSTED LOCA LIMITS POWER IMBALANCE LIMIT ALARM SETPOINTS
% OF 2452MW TECH SPECS FULL INCORE MINIMUM INCORE OUT-OF-CORE 0
- - 34.00
- - 25 00
- - 23.33
- - 22.75 68.
- - 34.00
- - 25 00
- - 23.33
- - 22.75 80.
- - 3 0.* 0C
~ -22 43
- - 19.55
- - 19.33 92.
- - 24.00
- - 18.00
- - 14.09
- - 14.27 i f, 2.
- - 2 4.00
- - 18.96
- - 13.74
- - 14.45 102.
6.00 1.20
- - 2. 4 0.
- - 3.12 92.
8.00 2'.20
.27
- - 1.34 84.
'17.00 9.59 7.65 6.75 70.
30.GG 20.77 19 20 13.45 0.'
3G.0:
20.77 19.23 13.45
- Assumes no changes necessary for Cycle 1-B ope ration.
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TABLE 3 s
CRYSTAL RIVER-3 CYCLE 1 FROM 400 EFPO TO EOC *
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ERROR ADJUSTED LOCA LIMITS POWER IMSALANCE LIMIT AL ARM SETp0INTS
% OF 2452MW TECH SPECS FULL'INCORE MINIMUM INC CR E OUT-OF-CORE
- - 3.4.03
- - 24.54
- - 23.13
- - 22.34 j
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68.
- - 3 4.00
- - 24.54
- - 23 13
- - 22.3'4 80.
- - 30.00
- - 22.12
- - 19.35
- - 19 01 92.
- - 1 5.02
- - 9.47
- - 6.33
- - 5.81 102.
- - 15.00
- - i c. 5 6
- - 5.9S
- - 6.06 iC2.
6.00 1.17
,2.60
- - 3.20 92.
5.00 2.04
.47
- - 1.49 54.
17.C]
9.63 7.45 6.63 7C.
30.07 20.34 19.00 1S.35 3.
30.00 2G.34 19.03 18.86
- Assumes no changes necessary for Cycle 1-B Operation.
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| 05000302/LER-1978-001, Forwards LER 78-001/03L-0 | Forwards LER 78-001/03L-0 | | | 05000302/LER-1978-001-03, /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | /03L-0:on 780103,3B Emergency Diesel Failed to Start During Maint on 3A Emergency Diesel Generator.Caused by Foreign Matter in Servo Booster Preventing Governor to Function Properly.Servo Booster Cleaned & Tested | | | 05000302/LER-1978-001-04, /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Coal Barges Entering & Maneuvering in Intake Canal During Sampling | /04X-0:on 780112-13,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Coal Barges Entering & Maneuvering in Intake Canal During Sampling | | | 05000302/LER-1978-002-03, /03L-0:on 780104,one Cable Tunnel Sump Pump Failed to Start During Operability Verification.Caused by Packaged Sump Pump Electric Motor Portion Failure.Pump Replaced | /03L-0:on 780104,one Cable Tunnel Sump Pump Failed to Start During Operability Verification.Caused by Packaged Sump Pump Electric Motor Portion Failure.Pump Replaced | | | 05000302/LER-1978-002, Forwards LER 78-002/03L-0 | Forwards LER 78-002/03L-0 | | | 05000302/LER-1978-002-04, /04X-0:on 780103-04,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Oil Barge Entering Intake Canal During Sampling | /04X-0:on 780103-04,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h ETS Levels. Partially Caused by Oil Barge Entering Intake Canal During Sampling | | | 05000302/LER-1978-003-03, /03L-O:on 780104,Unit 2 Battery Failed to Meet Quarterly Battery Test SP-511 Criteria.Caused by Electrolyte Stratification Due to Battery No Lead Condition.Request for Engineering Info Initiated to Evaluate & Recommend Solut | /03L-O:on 780104,Unit 2 Battery Failed to Meet Quarterly Battery Test SP-511 Criteria.Caused by Electrolyte Stratification Due to Battery No Lead Condition.Request for Engineering Info Initiated to Evaluate & Recommend Solution | | | 05000302/LER-1978-003, Forwards LER 78-003/03L-0 | Forwards LER 78-003/03L-0 | | | 05000302/LER-1978-003-04, /04X-0:on 780119-20,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding ETS Levels.Cause Undetermined | /04X-0:on 780119-20,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding ETS Levels.Cause Undetermined | | | 05000302/LER-1978-004-04, /04X-0:on 780201,unplanned Radioactive Gas Release Occurred During Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | /04X-0:on 780201,unplanned Radioactive Gas Release Occurred During Maint on Nitrogen Sys Header.Caused by Leaking MUV-141F & MUV-140 Makeup Tank Valves.Revisions Initiated to Consider Interconnecting Sys Impact | | | 05000302/LER-1978-004, Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | Forwards Supplemental Info to LER 78-004/04X-0 Re Unplanned Radioactive Gas Release During Maint.Personnel Associated W/Incident & Gaseous Pipe Contents List Encl.List Withheld Per Privacy Act | | | 05000302/LER-1978-004-03, /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | /03L-0:on 780108,reactor Coolant Dose Equivalent I-131 Found Contrary to Tech Spec Limitations.Caused by Transient Spikes Following Reactor Trip & Known Leaking Fuel Pins.Corrective Action Unnecessary | | | 05000302/LER-1978-005-04, /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | /04X-0:on 780127-28,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 51 kg/24-h Tech Spec Level.Partially Caused by Coal Barges Exciting Intake Canal During Sampling Period | | | 05000302/LER-1978-005-03, /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | /03L-0:on 780109,one Sump Pump Failed to Start During Cable Tunnel Sump Pump Operability Test SP-322 Performance.Caused by Failure of Start Control Bulb Switch Due to Inadequate Current Capacity | | | 05000302/LER-1978-005, Forwards LER 78-005/03L-0 | Forwards LER 78-005/03L-0 | | | 05000302/LER-1978-006, Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | Responds to NRC Re Violation Noted in IE Insp Rept 50-302/78-02.Corrective Actions:Problems Re Clearances Not Being Issued,Placed on Equipment or Released Per CP-115 Corrected.One Case Reported in LER 78-006/03L-0 | | | 05000302/LER-1978-006-03, /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | /03L-0:on 780111,HPI Isolation Valve MUV-25 Breaker Inadvertantly Opened & Red Tagged Out of Svc During Normal Mode 1 Operations.Clearance Procedure Reviewed W/Personnel | | | 05000302/LER-1978-006-04, /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | /04X-0:on 780206-07,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Unknown | | | 05000302/LER-1978-007-01, /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | /01T-2:on 780204,valve Operator FWV-15 Not Changed as Required by Upgrading of Steam Line Rupture Matrix.Caused by Lack of Appropriate Engineering Change Notice.Mod Package Completed.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-007, Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | Forwards Revision 2 to LER 78-007/01T-0,consisting of Supplementary Info | | | 05000302/LER-1978-007-04, /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | /04X-0:on 780216 & 17,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Coal Barge Exiting Intake Canal During Sampling May Have Been Partial Cause | | | 05000302/LER-1978-008, Forwards LER 78-008/03L-0 | Forwards LER 78-008/03L-0 | | | 05000302/LER-1978-008-04, /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | /04T-0:on 780305,waste Gas Header Overpressurized & Blew Auxiliary Bldg Loop Seals During RCS Degassing. Caused by Personnel Error.Personnel & Supervisors Instructed | | | 05000302/LER-1978-008-03, /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780122 During Sampling,Reactor Coolant Dose Equivalent I-131 Found to Be 1.42 Uci Per Gram.Caused by Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-009-03, /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | /03L-0:on 780122 Control Rod Driveline Breaker a Failed to Trip During Reactor Protection Sys Functional Test SP-110.Caused by Undercurrent Relay Failure.Breaker Replaced | | | 05000302/LER-1978-009-04, /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | /04X-0:on 780223-24,biomass of Fish & Shellfish Impinged on Intake Screens Exceeding 50 kg/24-h Reporting Level of Ets.Caused by Two Coal Barges Exiting & Coal Barge Entering Intake Canal During Sampling | | | 05000302/LER-1978-009, Forwards LER 78-009/04x-0 | Forwards LER 78-009/04x-0 | | | 05000302/LER-1978-010-03, /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | /03L-0:on 780123,security Alarm Sounded an Unauthorized Entry Into Vital Area Through Unlocked Door. Locking Devices on Vital Area Doors Altered.Key Now Needed for Outside Opening.Doors Cannot Be Left Unlocked | | | 05000302/LER-1978-010-04, /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | /04X-0:on 780307-08,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2 & 3 Exceeded 50 Kg Per 24-h Reporting Level.Oil Barge Entering Intake Canal During Sampling Period May Have Been Cause | | | 05000302/LER-1978-010, Forwards LER 78-010/03L-0 | Forwards LER 78-010/03L-0 | | | 05000302/LER-1978-011-04, /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | /04X:on 780303-04,biomass of Fish & Shellfish Impinged on Intake Screens of Units 1,2, & 3 Exceeded 50 Kg Per 24-h Reporting Level.Cause Undetermined | | | 05000302/LER-1978-011, Forwards LER 78-011/03L-0 | Forwards LER 78-011/03L-0 | | | 05000302/LER-1978-011-03, /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | /03L-0:on 780201,during Mode 3 Operation,Primary Containment Integrity Not Maintained When Nitrogen Valve NGV-81 Open for 3-h 42 Minutes.Caused by Oversight of Tech Spec 3.6.1 1 Requirements.Personnel Instructed | | | 05000302/LER-1978-012, Forwards LER 78-012/03L-0 | Forwards LER 78-012/03L-0 | | | 05000302/LER-1978-012-03, /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | /03L-0:on 780203,steamline Rupture Matrix Actuated During Heatup & Before Entry Into Operational Mode 2.Caused by Dead Band Shift of 600 Psig Pressure Switches MS-94,95- PS2.Switches Recalibr & Manual Bypass to Be Installed | | | 05000302/LER-1978-012-04, /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0331,improper Procedures Used in Environ Sample Analyses.Procedures Revised & More Efficient Counting Configurations & Overnight Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013-03, /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | /03L-0:on 780208,A & B Boric Acid Storage Tanks Found Inoperable While Performing Operability Check of Boron Injection Sources.Caused by Failure to Follow Procedures. Operators Instructed | | | 05000302/LER-1978-013-04, /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | /04X-0:June 1977-Mar 1978 Contractor Environ Sample Analyses Used Incorrect Procedures.Possibly Caused by Insufficient Sample Size & Count Times.Count Times Being Tested.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-013, Forwards LER 78-013/03L-0 | Forwards LER 78-013/03L-0 | | | 05000302/LER-1978-014-04, /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | /04X-0:on 780101-0502,environ Samples Not Analyzed W/Procedures Providing LLDs Equal to or Less than ETS Requirements.Caused by Inadequate Techniques &/Or Equipment. Normal Samples Taken.(Supplementary Info Sheet Only.) | | | 05000302/LER-1978-014-03, /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pend | /03L-0:on 780210,chemical Addition Valves CAV 1 & 2 Failed to Close on Completion of Pressurizer Steam Space Sampling.Caused by Incorrect Torque Switch Setting of Valve CAV-1.Operability restored.CAV-2 Corrective Action Pending | | | 05000302/LER-1978-014, Forwards LER 78-014/03L-0 | Forwards LER 78-014/03L-0 | | | 05000302/LER-1978-015-04, /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | /04T-0:on 780511,20 Uci Radioactive Liquid Released During Spent Resin Transfer to Vendor Vehicle. Caused by Line Rupture.Transfer Terminated & Radioactive Protection Measures Implemented.Corrective Action Pending | | | 05000302/LER-1978-015-03, /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | /03L-0:on 780215,during Reactor Trip Chemical/ Radiation Sampling Revealed Reactor Coolant Dose Equivalent Exceeded Limits.Caused by Expected Transient Spikes Following Trip & Leaking Fuel Pins.No Action Needed | | | 05000302/LER-1978-015, Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | Forwards LER 78-015/04T-1.LER 78-015/04T-0 Encl | | | 05000302/LER-1978-016, Forwards LER 78-016/01T-0 | Forwards LER 78-016/01T-0 | | | 05000302/LER-1978-016-01, /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | /01T-0:on 780310,in Mode 5 Operation,Unplanned Reactivity Insertion of 4.3% of Delta K/K.Caused by Dilution of RCS Upon Draining.Rcs Boron Sampling Surveillance Increased | | | 05000302/LER-1978-016-04, /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | /04L-0 (Supplementary Info Sheet):On 780404, Sample Not Obtained from Test Well 5 for Months of Apr & May.Caused by Well Being Inadvertently Covered by Const Debris.Well to Be Available for June Sampling | | | 05000302/LER-1978-017-01, /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | /01T-0:on 780306,17 Loose Parts Identified as Coupling & Spider Assembly of BPR- B-47,discovered in B once-through Steam Generator.Caused by Assembly Failure. Corrective Action to Be Determined | | | 05000302/LER-1978-017, Forwards LER 78-017/01T-0 | Forwards LER 78-017/01T-0 | |
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