05000327/LER-1980-066-03, /03L-0:on 800516,containment Isolation Valves FCV1-7,-14,-25 & -32 Determined Not Protected Against Steam Jet Resulting from Crack in Loop 1 Main Steam Riser.Caused by Design Error.Action Initiated to Install Proper Supports

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/03L-0:on 800516,containment Isolation Valves FCV1-7,-14,-25 & -32 Determined Not Protected Against Steam Jet Resulting from Crack in Loop 1 Main Steam Riser.Caused by Design Error.Action Initiated to Install Proper Supports
ML19324A086
Person / Time
Site: Sequoyah 
Issue date: 06/13/1980
From: Swearingen J
TENNESSEE VALLEY AUTHORITY
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19324A082 List:
References
LER-80-066-03L, LER-80-66-3L, NUDOCS 8006200457
Download: ML19324A086 (2)


LER-1980-066, /03L-0:on 800516,containment Isolation Valves FCV1-7,-14,-25 & -32 Determined Not Protected Against Steam Jet Resulting from Crack in Loop 1 Main Steam Riser.Caused by Design Error.Action Initiated to Install Proper Supports
Event date:
Report date:
3271980066R03 - NRC Website

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EVCNT DESCh11PTION AND PROS A8LE CONSEOutNCES Qlo g i Containment isolation valves FCVl-7. -ll4 -25 and -32 are not pro-i tected against a ' steam jet resulting from a crack in loop 1 main steam i ITm I EI riser. These valves could be d= = ed by this steam jet.

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CAUSE DESCRIPTtON AND CORRECnVE ACTIONS 27 i

EI Design error. Division of Engineering Design misinterpreted informa-l i tion sunn11ed by Westinahouse.

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  • ' Tenne'ssee Valley Authority Sequoyah t*uclear Planc LER SUPPLEMENTAL INFORMATION SQRO-50-327/ 8066 Technical Specification Involved:

6.9.1.13.b Reported Under Technical Specification 6.9.1.13.b Date of Occurrence: 5/16/80 Time of Occurrence: 0800 EDT Unit 1 Identification and Description of Occurrence Containment isolation valves FCV 1-7, -14, -25, and -32 are not protected against a steam jet resulting from a c ack in loop 1 main steam riser.

These valves could be damaged by this steam jet.

Conditions Prior to Occurrence Reactor in mode 5.

Action Specified in the Technical. Specifi' cation Surveillance Requirements Met Due to Inoperable Equipment None required in mode 5.

j Apparent Cause of Occurrence Division of Engineering Design misinterpreted information provided by i,

Westinghouse and deleted the supports and protective devices.

Analysis of Occurrence If a crack were to occur in main steam riser, the steam jet impinging on the blowdown lines could cause all four valves to be damaged.

Corrective Action

The deleted supports and protective devices will be added by ECN 5285.

Failure Data N/A.