05000278/LER-1980-016-01, /01T-0:on 800717,reanalysis by Bechtel of as-built Piping Determined That Stresses on Snubber 3-10-GB-S-44 Exceeded Operability Criteria.Caused by Inadequate Design Due to as-built Condition & Seismic Analysis Info Variance

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/01T-0:on 800717,reanalysis by Bechtel of as-built Piping Determined That Stresses on Snubber 3-10-GB-S-44 Exceeded Operability Criteria.Caused by Inadequate Design Due to as-built Condition & Seismic Analysis Info Variance
ML19331B639
Person / Time
Site: Peach Bottom 
Issue date: 07/31/1980
From: Cooney M
PECO ENERGY CO., (FORMERLY PHILADELPHIA ELECTRIC
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML19331B633 List:
References
LER-80-016-01T, LER-80-16-1T, NUDOCS 8008120524
Download: ML19331B639 (1)


LER-1980-016, /01T-0:on 800717,reanalysis by Bechtel of as-built Piping Determined That Stresses on Snubber 3-10-GB-S-44 Exceeded Operability Criteria.Caused by Inadequate Design Due to as-built Condition & Seismic Analysis Info Variance
Event date:
Report date:
2781980016R01 - NRC Website

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