05000302/LER-1980-041-03, /03L-0:on 801002,during Normal Operation,Reactor Coolant Tank Isolation Valve WDV-94 Would Not Close Due to Inadequate Torque Switch Setting.Setting Adjusted to Higher Value

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/03L-0:on 801002,during Normal Operation,Reactor Coolant Tank Isolation Valve WDV-94 Would Not Close Due to Inadequate Torque Switch Setting.Setting Adjusted to Higher Value
ML19339A671
Person / Time
Site: Crystal River 
Issue date: 10/27/1980
From:
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19339A659 List:
References
LER-80-041-03L, LER-80-41-3L, NUDOCS 8011040499
Download: ML19339A671 (2)


LER-1980-041, /03L-0:on 801002,during Normal Operation,Reactor Coolant Tank Isolation Valve WDV-94 Would Not Close Due to Inadequate Torque Switch Setting.Setting Adjusted to Higher Value
Event date:
Report date:
3021980041R03 - NRC Website

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- SUPPLEMENTARY INFORMATION Report No.:

50-302/80-041/03L-0

'Ficility:

Crystal River Unit No. 3 R2 port Date:

27 October 1980 Occurrence Date:

2 October 1980 Identification of Occurrence:

Failure to have containment isolation valves operable contrary to Technical Specification 3.6.3.1.

Conditions Prior to Occurrence:

Mode 1 power operation (100%)

Description of Occurrence:

At 2323 after pumping down the Reactor Coolant Drain Tank, WDV-94, RC Drain Tank Isolation Valve failed to close from the Control Room.

Manual valves WDV-808 and 840 were used to isolate the tank, and maintenance was initiated. Operability was restored at 1120 on 3 October 1980.

Designation of Apparent Cause:

The cause of this event is attributed to an inadequate setting on the. torque switch.

Analysis of Occurrence:

There was no effect upon the general public health or safety.

Corrective Action

The torque switch setting was adjusted and a functional test was performed. A reinspection of the torque switch setting will be performed in three (3) months.

Failure Data.

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.This is the second occurrence for WDV-94 and the twenty-sixth event reported under this specification.

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