LER-1980-184, /01T-0:on 801120,in Mode 1,at 94% Power,Auxiliary Bldg Gas Treatment Sys Was Declared Inoperable.Caused by Nitrogen Supply Line Being Run Under Railroad Door to Cask Loading Area,Preventing Door from Completely Closing |
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| 3271980184R01 - NRC Website |
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l i l 2 I l secondarv containment enclosure was subseauentiv inspected and no additional I i 13 J l tinauthorized nenetrations were found.
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Tennessee Valley Authority Sequovah Nuclear Plant i
LER SUPPLEMENTAL INFORMATION SORO-50-327/80184 Technical Specification Involved:
3.7.8.1 Reported r:nder Technical Specification:
6.9.1.12.b Date of Occurrence: 11/20/80 Time of Occurrence: 0930 CST Identification and Description of Occurrence:
The auxiliary building gas treatment system (ALGTS) was declared inoperable due to a nitrogen supply line being run under the railroad door to the cask loading area preventing the door from completely closing.
It was unknown whether or not the ABGTS would maintain the required k" H 0 vacuum under this 3
condition.
~
During subsequent testing of the ABGTS at 2315 CST, vacuum relief damper, 0-FCo-30-149, failed in the open position. The ABGTS was again delcared inoperable sic.ce the k" H 0 vacuum could not be maintained.
3 Conditions Prior to Occurrence:
Mode 1 with reactor power at 49%.
Apparent Cause of Occurrence:
The nitrogen line having to be run under the railroad door was a recoenized con-dition.
Investigation discovered that this condition had not been tested during either preoperational or surveillance testing to verify the ABGTS would maintain the required k" H 0 vacuum with the line running under the railroad door.
3 The vacuum relief damper failed due to a faulty flow control operator.
Corrective Action
The nitrogen line was removed from under the railroad door at 0952 CST and the door closed completely. The ABGTS was later tested with the pipe reinstalled under the railroad door to establish if the required k" H,0 vacuum could be naintained under this condition. During the test the vacuum relief damper failed apen and was repaired within Technical Specification tine limits.
Af ter the damper was repaired the ABGTS was tested with the pipe run under the railroad door and the k
H O vacuum could not be maintained at the required 2
system flow rates specified in the surveillance requirements. The pipe was removed and the door closed. The A3GTS was retested and the k" H;0 vacuum was maintained.
_ Failure Da a:
N/A
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| 05000327/LER-1980-001, Forwards LER 80-001/01T-0 | Forwards LER 80-001/01T-0 | | | 05000327/LER-1980-001-01, /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | /01T-0:on 800301-03,during Initial Fuel Loading, Licensee Failed to Estimate Flowrate from Svc Bldg Exhaust at 4-h Intervals.Caused by Misunderstanding of Tech Spec Requirements.Plant Instructions Revised | | | 05000327/LER-1980-002, Forwards LER 80-002/01T-0 | Forwards LER 80-002/01T-0 | | | 05000327/LER-1980-002-01, /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | /01T-0:on 800306,contents of Task Decontamination Collector Tank Discharged Via Liquid Radwaste Effluent Line to Cooling Tower Blowdown W/O Flow Estimates Being Performed.Caused by Misunderstanding of Tech Specs | | | 05000327/LER-1980-003-01, /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | /01T-0:on 800310,following Initial Fuel Loading, Flow Through Auxiliary Bldg Exhaust Sampler Not Maintained for 3.25-h.Caused by Misunderstanding of Tech Specs. Personnel Reinstructed in Applicable Requirements | | | 05000327/LER-1980-003, Forwards LER 80-003/01T-0 | Forwards LER 80-003/01T-0 | | | 05000327/LER-1980-004, Forwards LER 80-004/01T-0 | Forwards LER 80-004/01T-0 | | | 05000327/LER-1980-004-01, /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | /01T-0:on 800311,following Initial Fuel Loading, Flow Estimates for Auxiliary Bldg Vent Monitor Not Performed for 10-h.Caused by Misunderstanding of Tech Specs.Personnel Reinstructed Re Applicable Requirements | | | 05000327/LER-1980-005-03, /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | /03L-0:on 800311,while Performing SI-247.605, Reactor Solid State Protection Sys Was Placed in Input Inhibit Mode,Removing High Voltage from Source Range Channel N31.Caused by Removal of Fuses from Voltage Cut Out Relay | | | 05000327/LER-1980-005, Forwards LER 80-005/03L-0 | Forwards LER 80-005/03L-0 | | | 05000327/LER-1980-006-01, /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | /01T-0:on 800314,w/essential Raw Cooling Water Radiation Monitors on Train a Inoperable,Personnel Determined That Limiting Condition of Operation Requires Sampling.Caused by Misinterpretation of Tech Specs | | | 05000327/LER-1980-006, Forwards LER 80-006/01T-0 | Forwards LER 80-006/01T-0 | | | 05000327/LER-1980-007-01, /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | /01T-0:on 800315,following Initial Core Loading, Found Incorrect (Nonconservative) Valve Operator Weights Used in Seismic Analysis for Component Cooling Water Valves FCV-70-133,134 & 183.Caused by Incorrect Vendor Data | | | 05000327/LER-1980-007, Forwards LER 80-007/01T-0 | Forwards LER 80-007/01T-0 | | | 05000327/LER-1980-008, Forwards LER 80-008/03L-0 | Forwards LER 80-008/03L-0 | | | 05000327/LER-1980-008-03, /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Instal | /03L-0:on 800303,cooling Tower Blowdown Effluent Line Flow Monitor O-FR-27-175 Was Declared Inoperable.Flow Monitor Consistently Indicated Higher Flowrate than Actually Existed.Cause Unknown.Different Instrument to Be Installed | | | 05000327/LER-1980-009, Forwards LER 80-009/03L-0 | Forwards LER 80-009/03L-0 | | | 05000327/LER-1980-009-03, /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | /03L-0:on 800303,liquid Radwaste Effluent Line Flow Monitor 0-FT-77-42 Consistently Indicated Higher Discharge Flow Rate than Actually Observed.Cause Not Stated.Flow Monitor Modified & Returned to Svc | | | 05000327/LER-1980-010-03, /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | /03L-0:on 800304,gaseous Vent Flow Rate Monitors for Units 1 & 2 Shield Bldgs & Auxiliary Bldg Were Declared Inoperable.Cause Not Stated.Gaseous Flow Rate Monitors to Be Redesigned | | | 05000327/LER-1980-010, Forwards LER 80-010/03L-0 | Forwards LER 80-010/03L-0 | | | 05000327/LER-1980-011, Forwards LER 80-011/01T-0 | Forwards LER 80-011/01T-0 | | | 05000327/LER-1980-011-01, /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | /01T-0:on 800314,support Pin Insp at Foreign Plant Revealed Stress Corrosion Cracking in Westinghouse Supplied Pins.Insp Supported Westinghouse Ltr Informing Utils of Potential Hazard.Pins Will Be Replaced | | | 05000327/LER-1980-012-03, /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | /03L-0:on 800301,during Initial Core Loading,Rhr Flow Secured or Throttled Above Tech Specs.Caused by Intentional Increase to Allow Placement of Fuel Assemblies Near Loop 4 Hot Leg | | | 05000327/LER-1980-012, Forwards LER 80-012/03L-0 | Forwards LER 80-012/03L-0 | | | 05000327/LER-1980-013-03, /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | /03L-0:on 800302,failed to Analyze Samples from Unit 2 Shield Bldg Exhaust.Caused by Misunderstanding of Surveillance Requirements.Lab Personnel Instructed on Sampling & Analysis Requirements | | | 05000327/LER-1980-013, Forwards LER 80-013/03L-0 | Forwards LER 80-013/03L-0 | | | 05000327/LER-1980-014, Forwards LER 80-014/03L-0 | Forwards LER 80-014/03L-0 | | | 05000327/LER-1980-014-03, /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | /03L-0:on 800328,while Performing Check Source Test,Auxiliary Bldg Vent Noble Gas Monitor Had Module Power Problem & Failed in Svc.Caused by Zener Diode IN4740 & Transistor Fmps A13 Shorting Out | | | 05000327/LER-1980-015-03, /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | /03L-0:on 800305,while in Mode 6 W/Fuel Loading Complete,Pressure Was Only Being Monitored in One Steam Generator & Reactor Pressure Vessel.Caused by Misunderstanding of Surveillance Instruction | | | 05000327/LER-1980-015, Forwards LER 80-015/03L-0 | Forwards LER 80-015/03L-0 | | | 05000327/LER-1980-016, Forwards LER 80-016/03L-0 | Forwards LER 80-016/03L-0 | | | 05000327/LER-1980-016-03, /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | /03L-0:on 800307,at Completion of Fuel Loading & W/Core Alterations Still underway,SI-65 Was Not Performed. Caused by Misinterpretation of Tech Specs by Personnel.No Corrective Actions Necessary | | | 05000327/LER-1980-017-03, /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | /03L-0:on 800310,while in Mode 6,turbine Bldg Sump Monitor O-RM-90-212 Alarm Kept Coming In.Monitor Was Declared Inoperable.Caused by Malfunctioning Flow Switch Not Allowing Sufficient Flow Through Monitor | | | 05000327/LER-1980-017, Forwards LER 80-017/03L-0 | Forwards LER 80-017/03L-0 | | | 05000327/LER-1980-018-01, /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | /01T-0:on 800326,while in Mode 6 W/All Fuel Loaded,Exposed Cables Inside Containment Between Conduit & Penetrations Not Qualified to re-evaluated post-LOCA Max Dose Levels.Cables Shielded from Exposure to New Dose Level | | | 05000327/LER-1980-018, Forwards LER 80-018/01T-0 | Forwards LER 80-018/01T-0 | | | 05000327/LER-1980-019, Forwards LER 80-019/01T-0 | Forwards LER 80-019/01T-0 | | | 05000327/LER-1980-019-01, /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | /01T-0:on 800326,found Possibility of Not Maintaining Control Room Habitability Due to Leakage of Unfiltered Air.Possibly Caused by Isolation Dampers. Corrective Mods Planned | | | 05000327/LER-1980-020, Forwards LER 80-020/01T-0 | Forwards LER 80-020/01T-0 | | | 05000327/LER-1980-020-01, /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | /01T-0:on 800404,investigation Revealed That Several vendor-designed Pipe Supports Were Designed Utilizing Manufacturer Std 0.25-inch U-bolt Which Overstressed During Seismic Event.Caused by Design Error | | | 05000327/LER-1980-021-03, /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | /03L-0:on 800308,while in Mode 6,flow Rates from Auxiliary Bldg Ventilation Sys Flow Rate Monitor Were Not Recorded for Three Shifts.Caused by Misreading of Notation Used in Surveillance Instruction.Temporary Change Issued | | | 05000327/LER-1980-021, Forwards LER 80-021/03L-0 | Forwards LER 80-021/03L-0 | | | 05000327/LER-1980-022-03, /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | /03X-2:on 800318,sample Isolation Valves 1-FCV-90-108,109,110,114,115 & 116 Closed,Isolating Radiation Monitors.Caused by Isolation of Nonessential Control Air to Sample Valves.Valves Reopened | | | 05000327/LER-1980-022, Forwards LER 80-022/03L-0 | Forwards LER 80-022/03L-0 | | | 05000327/LER-1980-023, Forwards LER 80-023/03L-0 | Forwards LER 80-023/03L-0 | | | 05000327/LER-1980-023-03, /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | /03L-0:on 800402,during Surveillance Testing, Diesel Generator 2A-A Feedbreaker Failed to Close.Caused by Power Contacts Being Dirty.Power Contacts Cleaned | | | 05000327/LER-1980-024, Forwards LER 80-024/03L-0 | Forwards LER 80-024/03L-0 | | | 05000327/LER-1980-024-03, /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | /03L-0:on 800331,flow Switches on Radiation Monitors ORM-90-212 & 122 Found Inoperable.Caused by Small Particulate Matter in Monitored Liquid.Design Change Request Initiated.Weekly Preventive Maint Program Established | | | 05000327/LER-1980-025, Forwards LER 80-025/03L-0 | Forwards LER 80-025/03L-0 | | | 05000327/LER-1980-025-03, /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | /03L-0:on 800313 W/Unit 1 in Mode 6,O-RM-90-225 Condensate Demineralizer Effluent Line Was Taken Out of Svc for Maint.Caused by Weak Transistor.Transistor Replaced & Monitor Returned to Svc | |
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