05000302/LER-1980-048-03, /03L-0:on 801116 & 18,containment Isolation Valve CAV-3 Did Not Close While Sampling Pressurizer Water Space. Caused by Inadequate Closing Torque.Valve Closed,Deactivated & Maint Performed

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/03L-0:on 801116 & 18,containment Isolation Valve CAV-3 Did Not Close While Sampling Pressurizer Water Space. Caused by Inadequate Closing Torque.Valve Closed,Deactivated & Maint Performed
ML19345D983
Person / Time
Site: Crystal River 
Issue date: 12/16/1980
From: Hernandez V
FLORIDA POWER CORP.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML19345D981 List:
References
LER-80-048-03L, LER-80-48-3L, NUDOCS 8012220312
Download: ML19345D983 (2)


LER-1980-048, /03L-0:on 801116 & 18,containment Isolation Valve CAV-3 Did Not Close While Sampling Pressurizer Water Space. Caused by Inadequate Closing Torque.Valve Closed,Deactivated & Maint Performed
Event date:
Report date:
3021980048R03 - NRC Website

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EVENT OE50as#tCN ANO *eCO A31.3 00NSIOUENCIS bC r o,:, gat 1837 on November 16, 1980 and agaTn at 0950 on Nov.18,1980, containment isola

. to.21 (tion valve CAV-3 would'not close while sampling the pressurizer water space.

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r o I levents were contrary to T.S. 3.6.3.1.

Ineachcase,CAV-2wasclosedanddeactivatep

and maintenance was initiated. There was no effect upon the health or safety of

,the general public. These are the second and third occurrences for CAV-3, and this,

,,,; [is the twenty-eighth report under this Specification.

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g,,,, ; was functionally checked; operability was restored at 1620 Nov.19,1980. No further corrective action.

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'Name of Preparer:

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(SEE ATO.CZD SU??? Wr'rD.2I I't?CF3J.. IC'i 5 --- A) 8012 2 20 %

No SUPPLEMENTARY INFORMATION Report No.:

50-302/80-048/03L-0 j

Facility:

Crystal River Unit #3 Report Date:

16 December 1980 Occurrence Date:

16 November 1980 Identification of Occurrence:

Failure to have containment. isolation valves operable contrary to Technical Specification 3.6.3.1.

Conditions Prior to Occurrence:

l Mode 1 power operation (100%).

I Description of Occurrence:

At 1837 on November 16, 1980 after sampling the pressurizer water space, it was discovered that containment isolation valve CAV-3 would not close. CAV-2 was closed and deactivated j

and maintenance was initiated. Operability was restored at 0115 November 17, 1980. At 0950 November 18,1980 CAV-3 again failed to Close. CAV-2 was again closed and deactivated and additional maintenance was initiated. Operability was i

restored at 1620 November 19, 1980.

Designation of Apparent Cause:

The cause of these events is attributed to inadequate closing

torque, i

Analysis of Occurrence:

There was no effect upon the health or safety of the general public.

Corrective Action

The valve stem for CAV-3 was lubricated after the first event and the functional test was-satisfactory. After the second event, the torque switch setting was increased. No further I

corrective action required.

Failure Data:

These are the second and third occurrences for CAV-3,and this is the twenty-eighth event reported under this Specification.

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