05000364/LER-1981-012-03, /03L-0:on 810427,turbine Driven Auxiliary Feedwater Pump Was Declared Inoperable When Speed Could Not Be Automatically Controlled.Caused by Installation Wiring Error in Manual Potentiometer Circuit.Error Corrected

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/03L-0:on 810427,turbine Driven Auxiliary Feedwater Pump Was Declared Inoperable When Speed Could Not Be Automatically Controlled.Caused by Installation Wiring Error in Manual Potentiometer Circuit.Error Corrected
ML20004C358
Person / Time
Site: Farley 
Issue date: 05/29/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20004C357 List:
References
LER-81-012-03L-01, LER-81-12-3L-1, NUDOCS 8106030247
Download: ML20004C358 (1)


LER-1981-012, /03L-0:on 810427,turbine Driven Auxiliary Feedwater Pump Was Declared Inoperable When Speed Could Not Be Automatically Controlled.Caused by Installation Wiring Error in Manual Potentiometer Circuit.Error Corrected
Event date:
Report date:
3641981012R03 - NRC Website

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4 60 61 OOCxET NUMetR 64 49 EVENT DATg 14 7s REPORT DATE 83 EVENT DECCRIPTioN AND pro 8ABLE CONSEQUENCES h o 121 l At 0830 on 4-27-81. durino initial cerformance of survaillanca ta<t FND 7 RTD_?? e I

l.o 121 l (Turbine Driven Aux {liary Feedwater Pump Operability Testl the TDAFW oumo was declared irt -

1,o p,i g operable when the speed could not be automatically controlled (manual soeed control l

functioned properly).

Tech.* Spec. 3.7.1.2,in part, requir.es the TDAFW oump to be oper-l

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l-able. Tech. Spec. 3.7.1.2 action statement requirements were met.

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,,,,,approximately 0830 on 4-28-81.

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