05000364/LER-1981-043-03, /03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring

From kanterella
Revision as of 04:58, 21 December 2024 by StriderTol (talk | contribs) (StriderTol Bot insert)
(diff) ← Older revision | Latest revision (diff) | Newer revision → (diff)
Jump to navigation Jump to search
/03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring
ML20011A743
Person / Time
Site: Farley 
Issue date: 10/16/1981
From: Hairston W
ALABAMA POWER CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML20011A734 List:
References
LER-81-043-03L-01, LER-81-43-3L-1, NUDOCS 8110290374
Download: ML20011A743 (1)


LER-1981-043, /03L-0:on 810918,following Performance of Operability Test,Diesel Generator 1C Found Inoperable When Tripped Under Load.Caused by High Crankcase Pressure Resulting from Cylinder Lining Scoring
Event date:
Report date:
3641981043R03 - NRC Website

text

LICENSEE EVENT REPORT--

1 CONTROL BLCCX: l l

l l

l l lh (PLEASE PRINT OR TYC'E ALL REQUIRED INFORMATIONI 1

0 o I i l l A l L l J l M l F l 2 l@l 0 l 0 l - l 0 l OI O l 0 l 0.l-l0 l 0 l@l 4 l 1 l 1l Il 1l@l l

l@

F 3 9 UCENSEE CCDE 14 15 LICENSE NUM8ER a5

5 LICENSE TYPE JO 57 CA T 54

[ 9.

3c[3"c l L l@l0 l 5 l 0 l 0. l 0 l 31 6l 4 @l 0 l 9 ll' l8 l 8 l 1 l@l 1 l 0 l 1 l 6 ! 8 I 1 l@

"E 7

i

'O 60 61 COCKET NUMBER 63 63 EVENT CATE 74 75 REPCRT QATE 40 EVENT DESCRIPTICN AND PROBABLE CONSECUENCES h 10 62) l At 0252 on 9/18/81,followino oprfnrmanco nf FNP 1 ATPJA_1 (091C Onnrahilitu Toe + } Diocal I

oi3( l Gener.
Lor 1C was declared inoperable when.it tripped under load. Tech. Spec. 3.8.1.1 in ;
o ;e j lpart, requires DG 1C to be operable. Tech. Spec. 3.8.1.1.b.2 action statement requir.e-l 9oa3l l ments were met.

Health / safety of the public was not affected.

j io 86 I I I

l O 171 l l

l013l l 7

'l 3

60 SYSTEM

CAUSE

CAUSE CCMP.

VALVE CCCE CCCE SUSCCOE COMPCNENT CCCE SUSCCOE SUSCCCE

{019l l E! E l @ lE lh lB l@ lE lN lG lI l N l E l@ lZ l@ lZl@

7 a

9 to 11 12 t3 18 19

C SEQU ENTI AL OCCURRENCE REPCRT REVISION LEBtRO EVENT YEA R REPORT NO.

CCCE TYPE N O.

@ yu l 811l l-l l 01413 l l/l l013l lLl l-l

.l 0 l aE T

7.

22 23 24 26 27 28

3 30 31 32 T

N A C.

CN PL ? T M T HOURS 22 SS FC 1 S.

S PP E M NUFA RER g

.. IA @lZl@

lZ l@

l Z l@

[0 l 010 l 0 l [Njg l N [g l Alg l p l 0 l1 lo

.3 45 a6 37 40 4:

42 43 u-47 CAUSE CEECRIPTION AND CCRRECTIVE ACTIONS 27 l i i o l l The DG 1C trip was due to high crankcase pressure. An investigation revealed that the l3 ;il l number 1 and 11 cylinder liners were scored. The scoring of the liners caused localized ;

ii,,l l heating and exhaust leakage into the oil sump. This, in turn, caused the high crankcase ;_

li63l l pressure. Following the completion of repairs and successful testing, DG IC was returned y

,,,4 l l to service at 1603 on 10/02/81.

7

- 8 9

80

$A agpCWER OTH ER STATUS Cf C h

CISCCVERY OESCRIPTICN -

ii i5 l l El@ l ll 0l Ol@l NA l

lB (@lSurveillanceTest l

a $nviTY cClTENT 7

A AMOuNTCF ACTIVITY @ l aELEASEc or RELEASE LCCAT!CN OF RELEASE l1 66llZl@_lZl@l l

NA l_

NA 7

3 3 to 11 4.*

45 80 PERSONNEL EXPOSURES NUM8ER TYPE DESCRIPT1CN j i I 7 l l 0l 01 O l@l Z l@l NA l

PERSCNNEt'iN2u' dies NUMSER CESCRIPTION [t t a l l 0l' 010 l@l iA l

7 53

.it u

ao

.[

  • ! LCSS OF CA CAMAGE TO FACILITY 43 TYPE CE!CAIPTtON ft,9 lZl@l NA l

7 8 9. PusuC Tv 10 30 8110290374 G11015 NRC USE ONLY 43 i a 101 l Nlh[OESCRIPTtCN iSSuEo PDR ADOCK 05000364

=

i a s to I. IlI!IIIIllIllI NA S

PDR 6s as

. ao 3 -

NAME OF PREPARER: W. G. Hairston, III PHONE: (205)899-5156 o;