05000336/LER-1981-032-03, /03L-0:on 810925,one Reactor Bldg Closed Cooling Water Header Declared Inoperable.Caused by Piping Hanger Repairs.Piping Sys Restored to Svc Upon Completion of Repairs

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/03L-0:on 810925,one Reactor Bldg Closed Cooling Water Header Declared Inoperable.Caused by Piping Hanger Repairs.Piping Sys Restored to Svc Upon Completion of Repairs
ML20011A914
Person / Time
Site: Millstone 
Issue date: 10/23/1981
From: Bates R
NORTHEAST NUCLEAR ENERGY CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
Shared Package
ML20011A911 List:
References
LER-81-032-03L-01, LER-81-32-3L-1, NUDOCS 8111030350
Download: ML20011A914 (1)


LER-1981-032, /03L-0:on 810925,one Reactor Bldg Closed Cooling Water Header Declared Inoperable.Caused by Piping Hanger Repairs.Piping Sys Restored to Svc Upon Completion of Repairs
Event date:
Report date:
3361981032R03 - NRC Website

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[o]h]l On _9/25/8.1,_one_.of_two_Reacj;orlutidingflosed Cooling flateL(_RBCCW)_J1eadersn ___j was declared inoperable due to piping hanger re. pairs. _0peration continued j

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in accordance with Technical Specifications section 3.7.3.1.

On 9/28/81, one

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hanger repairs. Operation continued in accordance with Technical Specifications _

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The RBCCW header was restored to service within 26 hours3.009259e-4 days <br />0.00722 hours <br />4.298942e-5 weeks <br />9.893e-6 months <br /> and j

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the safety injection header was restored to service within 8 hou,s.

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