text
i Rope Ferry Rd. (Route 156), Titerford, CT 06385 rg N:rtheast wustone Nuclea Per Stadon Nuclear Energy Northeast Nuclear Energy Company P.O. Box 128 Taterford, CT 06385-0128 (860) 444-4300 Fax (860) 444-4277 The Northeast Utilities System JN 2 71996 Docket No. 50-336 B15737 Re: 10 CFR 50.73 U.S. Nuclear Regulatory Commission Document Control Desk Washington, DC 20555 This letter forwards Licensee Event Report (LER) 96-001-01 documenting an event that j
occurred at Millstone Nuclear Power Station, Unit No. 2 on January 4,1996. This LER is being submitted pursuant to 10 CFR 50.73(a)(2)(i).
i 1
Very truly yours, NORTHEAST NUCLEAR ENERGY COMPANY V
l
- M P. N. Richardson Director-Millstone Unit No. 2 Attachment: LER 96-001-01 cc:
T. T. Martin, Region i Administrator P. D. Swetland, Senior Resident inspector, Millstone Unit No. 2 D. G. Mcdonald, Jr., NRC Project Manager, Millstone Unit No. 2 l
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l 9607010392 960625 PDR ADOCK 05000336 [hhr/)4 c
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U.S. NUCLEAR REGULATORY COMMISSION APPROYED BY OMB NO. 3160-0104 NRC FORM 366 EXP1REs 04/30/98
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LICENSEE EVENT REPORT (LER) l'at"U ? Voc5f""NoTt#Rv"'c?#Je^r'#.'reot" sc sR*Mht&osEin'tef!"I&"1" "#MleaT?8tMat *
(See reverse for required number of i
digits / Characters for each block)
FACluTY NAME (1)
DOCKET NUMBER L2)
PAGE (3)
Millstone Nuclear Power Station Unit 2 05000336 1 of 5 TITLE 14)
Reactor Coolant System Heatup Rate Exceeded Technical Specification Limit EVENT DATE (5)
LER NUMBER (6)
REPORT DATE (7)
OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR YEAR SEQUENTIAL REVISION MONTH DAY YEAR FAclVTY NAME DOCKET NUMBER NUMBER 01 04 96 96 001 01 6
25 96 OPERATING THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR 5: (Check one or more) (11)
MODE W 1
20.2201(b) 20.2203(a)(2Hv>
X so.73(=>(2Hi) 50.73(a>(2)(viii>
POWER 20.2203(aH1) 20.2203(a)(3)(i) 50.73(a)(2)(ii) 50.73(aH2Hx)
LEVEL (10) 100 20.2203(aH2Hi) 20.2203(a)(3Hii) 50.73(a)(2Hiii) 73.71 20.2203(a)(2)(ii) 20.2203(a)(4) 50.73(aH2)(iv)
OTHER
"'""';"""'"""""""l" 20.2203(a)(2)(iii) 50.36(c)(1) 50.73(a)(2)(v) specify in Abstract below i
or in NRC Forrn 366A
20.2203(a)(2)(iv) 50.36(cH2) 50.73(a)(2)(vii)
LICENSEE CONTACT FOR THIS LER (12)
NAME TELEPHONE NUMBER (include Area Code)
M. D. Ehredt, Nuclear Licensing Supervisor (860)440-2142 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT (13)
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE
CAUSE
SYSTEM COMPONENT MANUFACTURER REPORTABLE TO NPRDS TO NPRDS SUPPLEMENTAL REPORT EXPECTED (14)
EXPECTED MONTH DAY YEAR SUBMISSION
[
YES NO (if yes, complete EXPECTED SUBMISSION OATE).
ABSTRACT (Limit to 1400 spaces, i.e., approximately 15 single-spaced typewritten lines) (16)
On January 4,1996 at 1815 houit with the plant in Mode 1 at 100% power, an enginaering review identified that the Reactor Coolant System (RCS) heatup rate requirements of Technical Specifications (TS) section 3.4.9.1 were not satisfied during an RCS heatup on December 17,1995. The RCS heatup rate was determined to be 72 F in a one hour period, which was iri excess of the Technical Specification's limit of 50*F per hour. The action statement requirement to perform an engineering evaluation of the structural integrity of the RCS and its acceptability for continued operation was not performed until January 4,1996. This event is being reported pursuant to the rsquirements of 10 CFR 50.73(a)(2)(i)(B), " reporting of any operation or condition prohibited by the plant's Technical Specifications."
Supplement 1 to this LER is being submitted since the Event Review Team (ERT) has completed their investigation of this event. The ERT determined the root causes to include design and procedura^ weaknesses for controlling the plant heate rate, and ineffective corrective actions implemented subsequent to the August 1995 RCS heetup event.
Planned corrective actions include changes to the plant operating procedures, changes to the plant heatup/cooldown monitoring computer program, and operator training to address this event and the August 1995 RCS heatup event.
e Thtre were no automatic or manually initiated safety responses resulting from this event.
NRC FORM 366 M 95)
aU.S. NUCLEAR REGULATORY CnMMISSION (4 95; UCENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVislON Millstone Nuclear Power Station Unit 2 05000336 NUMBER NUMBER 2 of 5 96 001 01 TEXT (If more span is required. use additional copies of NRC Form 366A) fil) 1.
Description of Event
On January 4,1996 at 1600 hours0.0185 days <br />0.444 hours <br />0.00265 weeks <br />6.088e-4 months <br />, with the plant in Mode 1 at 100% power, an engineering review concluded that the Reactor Coolant System (RCS) heatup rate requirements of the TS Limiting Condition for Operation (LCO) 3.4.9.1 (a) were not satisfied during the RCS heatup on Deaember 17,1995. Engineering determined that the RCS heatup rate was 72'F in a one hour period, which exceeded the LCO limit of 50"F per hour. During the RCS heatup on December 17,1995, the operating shift was unable to detect that the heatup rate limit in LCO 3.4.9.1(a) had been exceeded.
Utilizing the existing procedures based on the computer program data, the operating shift noted that the RCS heatup rate was 49.5 F in the one hour period following the start of the Reactor Coolant Pumps (RCP). Operators initiated an Adverse Condition Report (ACR) to document the unusual heatup rate.
However, in accordance with the procedures and computer program data, it was believed, at that time, that the heatup rate had not exceeded the LCO limit.
As a result of the ACR, an engineering review of the RCS heatup data was performed on December 18,1995, which concluded that the RCS heatup rate limit was not exceeded. However, this initial review did not consider the affect of shutdown cooling (SDC) injection temperature at the time that the SDC system was secured. An additional engineering review of the RCS heatup data was performed in January 1996 after additional questions were raised concerning the RCS heatup rate ACR. The January 1996 engineering review noted the following evonts of the RCS heatup on December 17,1995:
The SDC system was secured at 0425 hours0.00492 days <br />0.118 hours <br />7.027116e-4 weeks <br />1.617125e-4 months <br /> in preparation to start RCPs At the time that SDC was secured, the SDC injection temperature was 155 F e
Shortly after securing SDC, the RCS loop 2 cold leg temperature was observed to increase from 155*F e
to 185 F The "B" RCP was started at 0448 hours0.00519 days <br />0.124 hours <br />7.407407e-4 weeks <br />1.70464e-4 months <br /> and the "D" RCP was started at 0451 hours0.00522 days <br />0.125 hours <br />7.457011e-4 weeks <br />1.716055e-4 months <br /> e
At 0525 hours0.00608 days <br />0.146 hours <br />8.680556e-4 weeks <br />1.997625e-4 months <br />, the RCS loop 2 cold leg temperature was 227 F (one hour after securing SDC) e Based on the above, it was concluded that the heatup rate was 72 F in a one-hour period, which exceeded the LCO limit.
11.
Cause of Event
An Event Review Team's (ERT) review of this event identified the following root causes that resulted in the plant heatup rate exceeding TS limits:
a.
Computer software specifications and bases documents to procedures do not provide sufficient det*
concerning what constitutes a heatup/cooldown or which instruments should be utilized for calculating '
the heatup/cooldown rates in the reactor coolant or pressurizer. The lack of design document detail led to less than adequate operating procedures and monitoring capabilities to control heatup, and the computer heatup/cooldown program was not capabic of accurately detecting and conveying to the operators the RCS heatup and cooldown rates. As a result, the operators were unaware of the event.
The plant surveillance procedure used to monitor RCS heatup and cooldown rates requires that the RCS heatup rate be assessed at least once every 30 minutes during a plant heatup. This assessment GeRC FORM 366A (4-951
NRC FORM 326A U.S. NUCLEAR REGULATORY CoMMISSloN
(&95)
LICENSEE EVENT REPORT (LER)
TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR ScQUENTIAL REVISION Millstone Nuclear Power Station Unit 2 05000336 NUMBER NUMBER 3 of 5 96 001 01 TEXT (if more space is required, use addotional copies of NFtC Form 366A) 1111 uses the average of the RCS loop 1 and loop 2 cold leg temperature values. The plant computer heatup/cooldown monitoring software program was developed to reflect the above procedure requirements. During the December 17,1995 RCS heatup, the average of the RCS loop 1 and loop 2 temperatures was 170'F. The combination of using the average of the loop cold leg temperatures and the averaging methodology used by the plant computer concealed the magnitude of the reactor vessel downcomer heatup rate.
The plant heatup procedures also did not provide adequate instructions for establishing system conditions prior to the termination of SDC and starting the RCPs, such as the evaluation of the RCS heat balance, increasing the SDC injection temperature to minimize the reactor vessel downcomer heatup rate when SDC is secured, and controlling the heatup rate end sources of heat input at low temperatures. During the December 17,1995 RCS heatup there still remained significant core decay heat, since the reactor had been shutdown for approximately 3 days follcwing 120 days of operation at full power. This decay heat, combined with the heat input from twa operating RCPs, created a heatup rate condition which approached 50 F per hour. Additienally, since the heatup started near 185 F, the steam generators were ineffective in controlling the heatup rate until after they had begun to steam (i.e., at about 230 F).
b.
The evaluation of the heatup event in the summer of 1995 identified inadequate training and lack of detail in the heatup procedure as the primary causes. However, the corrective actions identified as a result of the heatup event were ineffective and not correctly prioritized, d
c.
Weaknesses and limitations in the plant design and procedures placed additional demands on the operators and did not provide them with adequate means of monitoring and controlling heatups.
Current operating procedures require the operator to secure SDC and raise reactor pressure, prior to starting the first RCP, due to minimum RCP seal pressure and SDC design pressure limite. TS LCO 3.4.1.3 allows operation under certain plant conditions, with the RCPs and SDC pumps out of service for up to 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, and requires the operator to enter into a 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> TS Action. This causes significant thermal-hydraulic changes in the region of the reactor vessel downcomer.
The root causes summarized above were submitted in a Northeast Utilities' letter B15653 dated April 19,1996, in response to an NRC request to provide the results of a detailed assessment of the causal factors underlying the weaknesses found in the procedures that are utilized to maintain RCS temperature within required limits.
Ill. Analysis of Event this event is being reported pursuant to the requirements of 10 CFR 50.73(a)(2)(i)(B), reporting of any operation or condition prohibited by the plant's Technical Specifications. The requirements for TS LCO 3.4.9.1(a) were not met when the RCS heatup rate exceeded the TS limit and the corresponding actions were not completed. Additionally, the requirements for TS LCO 3.0.4 were not met when the plant continued to change modes to full power operation, while not having met the actions of TS LCO 3.4.9.1(a).
L'RC FORM 366A q&95)
f e
1 aU.S. NUCLEAR REGULATORY COMMISslON (4 95)
UCENSEE EVENT REPORT (LER) l TEXT CONTINUATION FACILITY NAME (1)
DOCKET NUMBER (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 2 05000336 NUMBER NUMBER 4 of 5 96 001 01 TEXT (11more space is required, use additional copics of NRC Form 366A) (17}
The LCO for TS section 3.4.9.1(a) requires that the RCS heatup rate be limited to "50 F in any one hour l
period with T,yg above 140 F." This limit was exceeded at 0525 hours0.00608 days <br />0.146 hours <br />8.680556e-4 weeks <br />1.997625e-4 months <br /> on December 17,1995 when the RCS heatup rate was 72 F in a one hour period.
The action ror this TS LCO requires that "with any of the above limits exceeded, restore the temperature I
and/or pressure to within the limit within 30 minutes; perform an engineering evaluation to determine the effe;:ts of the out-of-limit condition on the structural integrity of the Reactor Coolant System; determine that the Reactor Coolant System remains acceptable for continued operations or be in at least HOT STANDBY within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and reduce the RCS T., and pressure to less than 200 F and 500 psia, respectively, within the fc,llowing 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />."
Since the exceeded RCS heatup rate was not identified by the operating shift on December 17,1995, the TS LCO was not entered. The action for this LCO is to perform an engineering evaluation of the structural integrity of the RCS and its acceptability for continued operation, which was not performed until January 4,1996.
Subsequent to the discovery of this event, an engineering evaluation was performed and concluded that the structuralintegrity of the RCS was not affected and remained acceptable for continued operation.
During the RCS heatup on December 17,1995, the pressurizer heatup rate limit of 100 F/hr contained in j
TS LCO 3.4.9.2(a) was also exceeded. The required actions for TS LCO 3.4.9.2(a) are to restore the
]
heatup rate within 30 minutes and to perform an engineering evaluation to determine the affects of the out-of-limit condition. This action was met.
However, as part of the detailed assessment of the weaknesses in the procedures for controlling plant heatups the ERT also evaluated the events related to exceeding the pressurizer heatup rate. The ERT concluded that the primary cause was that neither personnel nor procedures recognized the need to manage non-condensable gases in the pressurizer, that exist during short shutdowns when the primary system boundary has not been breached. Accumulation of non-condensable gases blanketing the steam space temperature detector and subsequent utilization of pressurizer spray, which mixed the steam space volume, was a primary cause of the temperature transient at the top of the pressurizer Plant procedures did not provide guidance for evaluation of, or the actions to be taken, when differences between the pressurizer steam space and water space temperature were observed.
IV. Corrective Action
Changes to the plant operating and surveillance procedures, the plant heatup/cooldown monitoring computer program, and the operator training program will be implemented to allow operators to properly monitor and control the RCS and pressurizer heatup rate.
Detailed corrective actions planned to be completed were submitted on April 19,1996 in response to the request to provide the results of a detailed assesim,nt of the causal factors underlying the event. In summary, the corrective actions include:
Revising procedures to incorporate consistent definitions, monitoring details based on computer software improvements, and equipment manipulation strategies for both heatups and cooldowns.
Developing new procedures in the area of reactor coolant system heat balance.
~
,U.S. NUCLEAR REGULATORY COMMISSION (4-95) *
- f UCENSEE EVENT REPORT (LER)
TEXT CONTINUATICN FACILITY NAME (1)
DOCKET NUMBE.1 (2)
LER NUMBER (6)
PAGE (3)
YEAR SEQUENTIAL REVISION Millstone Nuclear Power Station Unit 2 05000336 NUMBER NUMBER 5 of 5 96 001 01 TEXT (if more space is required, use additional copies of NRC Form 366A) (17)
Completing an investigation into single RCP operation and operation of RCPs in parallel with SDC.
Developing a new program for the management of non-condensable gases in the RCS.
Providing additional training for the detection and mitigation of non-condensable gases, and plant heatup and cooldown evolution's.
Developing strengthened administrative controls for tracking and completing ERT commitments.
Corrective actions will be completed prior to entry into Mode 4.
As committed in the April 19,1996 letter, the detailed schedule for completion of the corrective actions will be forwarded to the resident NRC inspector when finalized.
V.
Additional Information
Similar Events LER 95-030 reported an event that resulted in a RCS heatup rate that exceeded the TS limit.
LER 96-007 reoorted an event that resulted in a RCS cooldown rate that exceeded the TS limit.
Manufacturer Data None j
NRC FoMM 366A (4-95)
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| 05000336/LER-1996-001, :on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program |
- on 960625,discovered Reactor Coolant Sys Heatup Rate Exceeded Tech Spec.Caused by Design & Procedural Weaknesses Re Plant Heatup Controls.Revised Plant Operating Procedures & Heatup/Cooldown Computer Program
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-001-02, :on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power |
- on 960120,supplementary Leak Collection & Release Sys Declared Inoperable Due to Equipment Failure of Door Latch.Door Repaired & Plant Returned to 100% Power
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-002, :on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash |
- on 960108,determined That Ice Plug in Common Line Resulted in Inability to Backwash Svc Water Strainers. Caused by Mod to Backwash Line Piping.Ice Plug Removed, Restoring Ability to Backwash
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000423/LER-1996-002-02, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Identified. Caused by Inadequate Procedure.Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) | | 05000423/LER-1996-002, :on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual |
- on 960310,inadequate Surveillance for Determining Shutdown Margin When Unisolating Rcl Occurred Due to Procedure Inadequacy.Changes Will Be Made to Technical Requirements Manual
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000245/LER-1996-003, :on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements |
- on 960111,discovered Existing Anchorage of EDG Day Tank Not Seismically Adequate.Caused by Original Design Deficiency.Anchorage of EDG Tank Will Be Graded to Meet Design Basis of Seismic Load Requirements
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2)(i) 10 CFR 50.73(e)(2)(viii) | | 05000336/LER-1996-003-01, :on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys |
- on 960205,failed to Recognize Requirement to Enter TS LCO 3.0.3 Following Discovery of Ice Blockage. Caused by Inadequate Problem Identification Methods.Design Basis Summary Documents Have Been Prepared Re TS Safety Sys
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000245/LER-1996-003-02, Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | Forwards LER 96-003-02 Which Documents an Event That Occurred at Mnps,Unit 1 on 960111,per 10CFR50.73(a)(2)(i) & 10CFR50.73(a)(2)(ii).Commitments Made in Ltr,Submitted | 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-003-01, :on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised |
- on 960312,temporary I-Beams Located Overhead of Recirculation Spray Sys HXs Discovered.Caused by Inadequate Work Control.Work Control Procedures Revised
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-004-01, :on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment |
- on 960319,determined That Auxiliary Feedwater Isolation Valves Were in Noncompliance W/Ts.Caused by Misinterpretation of Ts.Revised Operating Procedure to Preclude cross-connected Sys Alignment
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2) | | 05000336/LER-1996-004, :on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented |
- on 960131,svc Water Strainer Backwash Sys Susceptibility to Freezing Following Loss of Intake Structure non-vital Heating Occurred.Caused by Inadequate Original Design.Design Change Implemented
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000423/LER-1996-004-02, :on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements |
- on 960316,auxiliary Feedwater Isolation Valves Noncompliance W/Ts Occurred.Caused by Misinterpretation of Ts.Event Reviewed W/Station Personnel to Caution Others on TS Surveillance Requirements
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-005-01, :on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability |
- on 960212,discovered PEO Improperly Utilized to Replace Automatic Backwash Function of Svc Water Strainer Backwash Sys.Caused by Failure to Enter TS Action Statement. Revise Procedures for IST SWS Pump Operability
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-005-02, :on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated |
- on 960321,service Water Booster Pump Auto Start Discovered Disable.Caused by Inadequate Review.C/A: Bypass Jumper Removed & Mod Initiated
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) 10 CFR 50.73(a)(2)(1) 10 CFR 50.73(s)(2) | | 05000423/LER-1996-005-03, :on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised |
- on 960321,design Noncompliance Noted for High Temp Automatic Start Feature of SWS Booster Pumps.Caused by Weakness in Design Control Process.Operating Procedures Revised
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-006-01, :on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established |
- on 960207,service Water Pump Motor Flood Protection Not Provided.Caused by Inadequate Administrative Controls.Administrative Controls Established
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-006-02, :on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner |
- on 960330,plant Shutdown Required by TS for AFW Containment Isolation Valves Declared Inoperable.Caused by Opened Valves Outside Containment.Unit Was Shutdown in Orderly Manner
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown | | 05000423/LER-1996-007, :on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed |
- on 960403,containment Recirculation Spray, Quench Spray & Safety Injection Sys Were Outside Design Basis Due to Design Errors.Design Reviews of Rss,Qss,Si & Other Sys Will Be Performed
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(viii) | | 05000336/LER-1996-007, :on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised |
- on 960220,discovered RCS C/D Rate Exceeded TS Limit.Caused by Use of Wrong Temp Sensor.Plant Operating Procedures,Heatup/C/D Monitoring Computer Program & Operator Training Involving These Events Revised
| | | 05000423/LER-1996-007-01, :on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable |
- on 960403,CRS & Qs Sys Found Outside Design Basis Due to Design Errors.Restored Sys to Appropriate Design Basis Requirements Prior to Declaring Sys Inoperable
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-007-02, Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | Forwards LER 96-007-02 Which Supplements Rept Submitted on 960502,per 10CFR50.73(a)(2)(ii)(B),10CFR50.73(a)(2)(v)(B&D), 10CFR50.73(a)(2)(vii)(B&D).Commitments in Response to Event, Encl | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000336/LER-1996-008, :on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced |
- on 960222,concluded That Condition of Wire Mesh Screen Encl Over Two Containment Recirculation Suction Pipes Outside Design Basis.Caused by Const/Installation Error.Screen Encl Being Replaced
| | | 05000423/LER-1996-008-01, :on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism |
- on 960412,reactor Protection Sys Lead/Lag Time Constants Found non-conservative.Caused by Failure of Vendor to Identify Conservative Calibr Requirements.Tss Changed to Correctly Identify Direction of Conservatism
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000423/LER-1996-009, :on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint |
- on 960423,inoperable Shutdown Margin Monitors from Low Count Rate Occurred Due to Inadequate Design Control.Reduced SMM Setpoint
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000245/LER-1996-009-01, :on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed |
- on 960109,isolation Condenser Makeup Water Temperature Below Design Basis Limit,Determined.Caused by Inadequate Design Specification.Preliminary Assessment of non-ductile Failure of Isolation Condenser Sys Performed
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000336/LER-1996-009-01, :on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change |
- on 960216,post LOCA Contianment Pressure Prevented Timely Extraction of PASS Air Sample & H Sample. Caused by Inadequate Assessment of Revised Post LOCA Response Analysis.Implemented Design Change
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2) | | 05000423/LER-1996-009-02, Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | Submits Table of Commitments Re LER 96-009-02 Per 10CFR50.73(a)(2)(ii) | 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-010, :on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised |
- on 960222,identified That Containment Hydrogen Monitor Flow Could Not Be Established W/Containment at Atmospheric Pressure Due to Improper Setting of Sys Pressure Regulators.Sys Calib Procedure Will Be Revised
| | | 05000423/LER-1996-010-02, :on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted |
- on 960425,determined That Potential Failure Mode of Rod Control Sys Acopian Power Supplies Could Create Unanalyzed Condition.Caused by Inadequate Design Review. Reset Feature Will Be Deleted
| 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000336/LER-1996-011-01, :on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised |
- on 960222,required Time to Enter Mode 5 Exceeded.Caused by Effective Action Not Being Initiated to Revise SDC & Cooldown Rate Monitoring Procedures.Operating & Surveillance Procedures Will Be Revised
| | | 05000423/LER-1996-011-02, :on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/ |
- on 960512,determined That Both Trains of CR Envelope Pressurization Sys Inoperable Due to Imbalance in air-conditioning Sys.Cr air-conditioning Sys Rebalanced.W/
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-012, :on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/ |
- on 960515,containment Leakage in Excess of TS Limits Noted,Due to Valve Leakage.Containment Spray Line Penetration 100 Flushed to Remove Any Boron Deposits.W/
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(i) | | 05000336/LER-1996-012-01, :on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected |
- on 960228,SIS Drain Stop Valves Failed to Meet Functional Requirements of Ts.Caused by Personnel Error & Inadequate Retest Requirements.C/A:Valve 2-SI-618 Modified & Safety Related Solenoid Valves Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(x) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000423/LER-1996-012-02, :on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits |
- on 960515,containment Leakage Exceeded Tech Spec Limit.Caused by Boric Acid Residue.Performed Flush of Line to Remove Boron Deposits
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded | | 05000423/LER-1996-013, :on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified |
- on 960612,design Deficiency in Rhrs.Caused by Inconsideration That Failure Mode of RHS Flow Control Valves Could Create High RHS Heat Exchanger CCP Discharge Temps. Actuators for Heat Exchanger Valves,Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition | | 05000336/LER-1996-013-01, :on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply |
- on 960314,assessed Wide Range Logarithmic Neutron Flux Monitors Nuclear Instrumentation Channels A,B,C & D as Inoperable Due to Potential Susceptability to Common Mode Failure.Replaced Failed Power Supply
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-013-02, :on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement |
- on 960515,determined Design Deficiency in Residual Heat Removal System (Rhs).Caused by Original Plant Design.Corrective Actions Will Be Described in Supplement
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000336/LER-1996-014-01, :on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3 |
- on 960311,weekly TS Surveillances Missed. Caused by Personnel Error W/Respect to Scheduling.C/A: Implemented Requirements of Surveillance Procedure Sp 2614A-3
| 10 CFR 50.73(a)(2)(i) | | 05000423/LER-1996-014-02, :on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown |
- on 960516,surveillances for Emergency Diesel Generator Performed During Operation,Versus Shutdown.Caused by Misinterpretation of Shutdown Stipulation.Surveillances Performed During Shutdown
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(iii) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-015-05, Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | Forwards LER 96-015-05,documenting Event That Occurred at Plant,Unit 3 on 960610,per 10CFR50.73(a)(2)(ii)(B). Commitments Made within Ltr Submitted | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2) | | 05000423/LER-1996-015-04, Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | Forwards LER 96-015-04,documenting Condition Determined at Unit 3 on 960610.Util Commitments in Response to Event Contained within Attachment 1 to Ltr | 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000336/LER-1996-015-01, :on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures |
- on 960312,failed to Perform Action Requirement for TS LCO 3.3.1.1.Caused by Failure to Recognize Applicability of TS During Abnormal Equipment Configuration. Revised Procedures
| 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition | | 05000423/LER-1996-015-02, Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | Forwards LER 96-015-02 Re Inadequate Electrical Separation Between Redundant Protection Trains Associated W/Reactor Trip Switches & Reactor Trip Breaker Indicating Lights | 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability | | 05000423/LER-1996-016-02, :on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches |
- on 960619,switchgear Cabinet in Noncompliance W/Seismic Design Basis & Subsequently Inadvertent Esfa Signal Occurred.Personnel Did Not Latch Known Seismic Latches as Required.Engaged Latches
| | | 05000336/LER-1996-016-01, :on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested |
- on 960312,common Power Supply Cable to 4 Condenser Pit Level Switches Found Improperly Connected. Caused by Inadequate Work Control.Cable Properly Connected & Trip Circuits Tested
| 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) | | 05000336/LER-1996-017, :on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified |
- on 960320,discovered That Hydrogen Monitoring Sys Does Not Meet Single Failure Criterion by Reg Guide 1.97.Caused by Failure to Adequately Consider Sys Design Basis Requirements.Design Change Modified
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-017-02, :on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised |
- on 960621,determined Design Deficiency Existed in Tornado Protection Ventilation Dampers,Could Have Affected EDGs Following Tornado.Caused by Inadequate Original Plant Const Design.Procedure Revised
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat | | 05000336/LER-1996-018-01, Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | Forwards LER 96-018-01,documenting Condition That Was Discovered at Unit 2 on 960319.LER Suppl Provides Update on Analyses & Investigation of Condition.Attachment 1 Is Clarification of Original Commitment Associated W/Ler | 10 CFR 50.73(a)(2)(v), Loss of Safety Function | | 05000336/LER-1996-018, :on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced |
- on 960316,gaps Discovered in Encls Door Seals for Motor Control Ctrs B51 & B61.Caused by Weakness in Existing Program to Inspect & Verify Integrity of Environ Protective Barriers.Doors for MCC B51 & MCC B61 Replaced
| 10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(x) 10 CFR 50.73(a)(2)(viii) | | 05000423/LER-1996-019-02, :on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept |
- on 960627,RCS PORV Block Valves Were Determined to Be Unable to Perform Intended Safety Functions.Caused by Structural Design Deficiency.C/A Will Be Provided in Supplement to Rept
| 10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition 10 CFR 50.73(a)(2)(v), Loss of Safety Function 10 CFR 50.73(a)(2)(vii), Common Cause Inoperability 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(a)(2)(i) 10 CFR 50.73(a)(2)(iii) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(a)(2)(viii) 10 CFR 50.73(a)(2) |
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