ENS 43353
ENS Event | |
---|---|
21:23 May 9, 2007 | |
Title | Unanalyzed Condition Due to Identified Non Compliant Fire Protection Manual Operator Actions |
Event Description | {{#Wiki_filter:During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined there were 11 non-compliant manual operator actions that were being performed to achieve and maintain hot safe shutdown in Fire Area A06 (1B32 area). These manual actions were being performed in an Appendix R Section III.G.1/G.2 fire area, however, they do not meet the criteria for allowable manual actions specified in RIS 2006-10, 'Regulatory Expectations with Appendix R Paragraph III.G.2 Operator Manual Actions.'
The discovery of these non-compliant manual actions is being reported as an unanalyzed condition as defined by 10 CFR 50.72(b)(3)(ii). Appropriate compensatory measures have been established for Fire Area A06 via initiation of hourly fire rounds. An extent of condition review has been initiated that will encompass the remainder of the safe shutdown areas in both Point Beach Nuclear Plant (PBNP) units. The results of the extent of condition will be documented in the site's corrective action program with compensatory measures being established as appropriate. The 60-day licensee event report, submitted to the Commission in accordance with 10 CFR 50.73(a)(2)ii), will provide the results of the manual action compliance review and follow-up corrective actions. The PBNP Resident Inspector has been notified of this event.
This is an update to EN 43353 submitted at 19:33 EDT on 05/09/07: During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined that non-compliant manual operator actions are credited to achieve and maintain hot safe shutdown for a fire. The following actions were identified during the extent of condition reviews conducted subsequent to EN 43353 report.
1 - Fire Area A03, 1P-2C CVCS Charging Pump Cubicle 1 - Fire Area A04, 1P-2B CVCS Charging Pump Cubicle 1 - Fire Area A05, 1P-2A CVCS Charging Pump Cubicle 6 - Fire Area A07, Chemical Drain, Laundry Tank and Reactor Coolant Pump Seal Filter Room 5 - Fire Area A08, HVAC Equipment Room & Pipeway No. 1 Valve Gallery Area These manual actions are credited for safe shutdown in an Appendix R Section III.G.1/G.2 fire area, however, they do not meet the criteria for allowable manual actions specified in RIS 2006-10, 'Regulatory Expectations with Appendix R Paragraph III.G.2 Operator Manual Actions.' The discovery of these non-compliant manual actions is being reported as an unanalyzed condition as defined by 10 CFR 50.72(b)(3)(ii). Appropriate compensatory measures have been established for Fire Areas A03, A04, A05, A07 and A08 via initiation of hourly fire rounds. An extent of condition review is continuing that will encompass the remainder of the safe shutdown areas in both Point Beach Nuclear Plant (PBNP) units. The PBNP Resident Inspector has been notified of this event." Notified R3DO (Mark Ring).
This is an update to EN 43353 submitted at 19:33 EDT on 05/09/07: During performance of NFPA-805 Transition Project Task SUP-I, 'Manual Action Compliance,' it was determined that the following non-compliant manual operator actions are credited to achieve and maintain not safe shutdown for a fire. These actions were identified during the extent of condition reviews for the above referenced report [The following non-compliant actions were identified:] 5 [actions for] Fire Area A01, Primary Auxiliary Building El. 44'& 66' (Except FX237) 5 [actions for] Fire Area A01-G, Unit 1 Fa�ade 5 [actions for] Fire Area A01-H, Unit 2 Fa�ade 3 [actions for] Fire Area A10, Radioactive Gas Treatment Area 3 [actions for] Fire Area A11, Pipeway No. 4 Valve Gallery 1 [actions for] Fire Area Al 2, 2P2C CVCS Charging Pump Room 1 [actions for] Fire Area A13, 2P2B CVCS Charging Pump Room 1 [actions for] Fire Area A14, 2P2A CVCS Charging Pump Room 12 [actions for] Fire Area A15, 2B32 Motor Control Center Area 21 [actions for] Fire Area A23N, North Side of Auxiliary Feedwater Pump Room 19 (actions for] Fire Area A23S, South Side of Auxiliary Feedwater Pump Room 8 [actions for] Fire Area A25, D06 Battery Room 9 [actions for] Fire Area A26, D05 Battery Room 7 [actions for] Fire Area A27, G01, Diesel Generator Room 7 [actions for] Fire Area A28, G02 Diesel Generator Room 1 [actions for] Fire Area A29, Air Compressor Room 1 [actions for] Fire Area A61, P206A & P207A Fuel Oil Pump Room 7 [actions for] Fire Area A71, Diesel Generator Building, Train B Areas The licensee notified the NRC Resident Inspector. Notified R3DO (Ring).
During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined that the following non-compliant manual operator actions are credited to achieve and maintain hot safe shutdown for a fire. These actions were identified during the extent of condition reviews for the above referenced report. [The following non-compliant actions were identified:] 28 Fire Area A01- A, Primary Auxiliary Building, EL. 8' & Below 18 Fire Area A02, Containment Spray / Safety Injection Pump Room 11 Fire Area A01-CN, Primary Auxiliary Building, EL 26' South Wing 10 Fire Area A01-CS, Primary Auxiliary Building, EL 26' South Wing 9 Fire Area A16, D106 Battery Room 9 Fire Area A17, D04 Electrical Equipment Room 9 Fire Area A18, DO3 Electrical Equipment Room 8 Fire Area A19, D105 Battery Room 16 Fire Area A01-E,Turbine Building & South Service Building 1 Fire Area A01-F, Yard Area 1 Fire Area A54, D305 Swing Battery & D301 Charger Rooms 5 Fire Area A36, Unit 1 Containment Area 5 Fire Area A46, Unit 2 Containment Area 7 Fire Area A68, Train B East Duct Bank & Manholes 2 Fire Area A70, Train A West Duct Bank & Manholes The licensee notified the NRC Resident Inspector. Notified R3DO (Ring) }}[[Event description::Description::{{#Regex_clear:During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined there were 11 non-compliant manual operator actions that were being performed to achieve and maintain hot safe shutdown in Fire Area A06 (1B32 area). These manual actions were being performed in an Appendix R Section III.G.1/G.2 fire area, however, they do not meet the criteria for allowable manual actions specified in RIS 2006-10, 'Regulatory Expectations with Appendix R Paragraph III.G.2 Operator Manual Actions.' The discovery of these non-compliant manual actions is being reported as an unanalyzed condition as defined by 10 CFR 50.72(b)(3)(ii). Appropriate compensatory measures have been established for Fire Area A06 via initiation of hourly fire rounds. An extent of condition review has been initiated that will encompass the remainder of the safe shutdown areas in both Point Beach Nuclear Plant (PBNP) units. The results of the extent of condition will be documented in the site's corrective action program with compensatory measures being established as appropriate. The 60-day licensee event report, submitted to the Commission in accordance with 10 CFR 50.73(a)(2)ii), will provide the results of the manual action compliance review and follow-up corrective actions. The PBNP Resident Inspector has been notified of this event.
This is an update to EN 43353 submitted at 19:33 EDT on 05/09/07: During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined that non-compliant manual operator actions are credited to achieve and maintain hot safe shutdown for a fire. The following actions were identified during the extent of condition reviews conducted subsequent to EN 43353 report.
1 - Fire Area A03, 1P-2C CVCS Charging Pump Cubicle 1 - Fire Area A04, 1P-2B CVCS Charging Pump Cubicle 1 - Fire Area A05, 1P-2A CVCS Charging Pump Cubicle 6 - Fire Area A07, Chemical Drain, Laundry Tank and Reactor Coolant Pump Seal Filter Room 5 - Fire Area A08, HVAC Equipment Room & Pipeway No. 1 Valve Gallery Area These manual actions are credited for safe shutdown in an Appendix R Section III.G.1/G.2 fire area, however, they do not meet the criteria for allowable manual actions specified in RIS 2006-10, 'Regulatory Expectations with Appendix R Paragraph III.G.2 Operator Manual Actions.' The discovery of these non-compliant manual actions is being reported as an unanalyzed condition as defined by 10 CFR 50.72(b)(3)(ii). Appropriate compensatory measures have been established for Fire Areas A03, A04, A05, A07 and A08 via initiation of hourly fire rounds. An extent of condition review is continuing that will encompass the remainder of the safe shutdown areas in both Point Beach Nuclear Plant (PBNP) units. The PBNP Resident Inspector has been notified of this event." Notified R3DO (Mark Ring).
This is an update to EN 43353 submitted at 19:33 EDT on 05/09/07: During performance of NFPA-805 Transition Project Task SUP-I, 'Manual Action Compliance,' it was determined that the following non-compliant manual operator actions are credited to achieve and maintain not safe shutdown for a fire. These actions were identified during the extent of condition reviews for the above referenced report [The following non-compliant actions were identified:] 5 [actions for] Fire Area A01, Primary Auxiliary Building El. 44'& 66' (Except FX237) 5 [actions for] Fire Area A01-G, Unit 1 Fa�ade 5 [actions for] Fire Area A01-H, Unit 2 Fa�ade 3 [actions for] Fire Area A10, Radioactive Gas Treatment Area 3 [actions for] Fire Area A11, Pipeway No. 4 Valve Gallery 1 [actions for] Fire Area Al 2, 2P2C CVCS Charging Pump Room 1 [actions for] Fire Area A13, 2P2B CVCS Charging Pump Room 1 [actions for] Fire Area A14, 2P2A CVCS Charging Pump Room 12 [actions for] Fire Area A15, 2B32 Motor Control Center Area 21 [actions for] Fire Area A23N, North Side of Auxiliary Feedwater Pump Room 19 (actions for] Fire Area A23S, South Side of Auxiliary Feedwater Pump Room 8 [actions for] Fire Area A25, D06 Battery Room 9 [actions for] Fire Area A26, D05 Battery Room 7 [actions for] Fire Area A27, G01, Diesel Generator Room 7 [actions for] Fire Area A28, G02 Diesel Generator Room 1 [actions for] Fire Area A29, Air Compressor Room 1 [actions for] Fire Area A61, P206A & P207A Fuel Oil Pump Room 7 [actions for] Fire Area A71, Diesel Generator Building, Train B Areas The licensee notified the NRC Resident Inspector. Notified R3DO (Ring).
During performance of NFPA-805 Transition Project Task SUP-1, 'Manual Action Compliance,' it was determined that the following non-compliant manual operator actions are credited to achieve and maintain hot safe shutdown for a fire. These actions were identified during the extent of condition reviews for the above referenced report. [The following non-compliant actions were identified:] 28 Fire Area A01- A, Primary Auxiliary Building, EL. 8' & Below 18 Fire Area A02, Containment Spray / Safety Injection Pump Room 11 Fire Area A01-CN, Primary Auxiliary Building, EL 26' South Wing 10 Fire Area A01-CS, Primary Auxiliary Building, EL 26' South Wing 9 Fire Area A16, D106 Battery Room 9 Fire Area A17, D04 Electrical Equipment Room 9 Fire Area A18, DO3 Electrical Equipment Room 8 Fire Area A19, D105 Battery Room 16 Fire Area A01-E,Turbine Building & South Service Building 1 Fire Area A01-F, Yard Area 1 Fire Area A54, D305 Swing Battery & D301 Charger Rooms 5 Fire Area A36, Unit 1 Containment Area 5 Fire Area A46, Unit 2 Containment Area 7 Fire Area A68, Train B East Duct Bank & Manholes 2 Fire Area A70, Train A West Duct Bank & Manholes The licensee notified the NRC Resident Inspector. Notified R3DO (Ring) }}| ]] |
Where | |
---|---|
Point Beach ![]() Wisconsin (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition | |
LER: | 05000266/LER-2007-002 |
Time - Person (Reporting Time:+-1.83 h-0.0763 days <br />-0.0109 weeks <br />-0.00251 months <br />) | |
Opened: | Ryan Rode 19:33 May 9, 2007 |
NRC Officer: | Jeff Rotton |
Last Updated: | May 17, 2007 |
43353 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 43353\u003C/a\u003E - \u003Ca href=\"/Point_Beach\" title=\"Point Beach\"\u003EPoint Beach\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EUnanalyzed Condition Due to Identified Non Compliant Fire Protection Manual Operator Actions\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 43353 - Point Beach\n","link":"","lat":44.280972222222225,"lon":-87.53674444444445,"icon":"/w/images/9/9b/NextEra_Energy_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
Unit 2 | |
---|---|
Reactor critical | Critical |
Scram | No |
Before | Power Operation (100 %) |
After | Power Operation (100 %) |
WEEKMONTHYEARENS 532392018-03-01T22:43:0001 March 2018 22:43:00
[Table view]10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Tornado Missile Vulnerabilities ENS 529762017-09-18T22:24:00018 September 2017 22:24:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Control Room Envelope Not Maintained ENS 507402015-01-15T23:04:00015 January 2015 23:04:00 10 CFR 50.72(b)(3)(v)(B), Loss of Safety Function - Remove Residual Heat, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Inadequately Sealed Piping Penetrations and Postulated Flooding Event ENS 484022012-10-12T09:20:00012 October 2012 09:20:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Reactor Power Exceeded Fsar Analyzed Value ENS 443512008-07-16T20:16:00016 July 2008 20:16:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Potential Fire Propagation Between Rooms Could Affect Appendix R Safe Shutdown ENS 434872007-07-12T15:15:00012 July 2007 15:15:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Fire Inspection Analysis of Pressurizer Porvs and Block Valves ENS 433532007-05-09T21:23:0009 May 2007 21:23:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition Due to Identified Non Compliant Fire Protection Manual Operator Actions ENS 421292005-11-08T14:44:0008 November 2005 14:44:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Design Basis for Long Term Cooling Not Correctly Modeled ENS 421092005-11-02T05:00:0002 November 2005 05:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Tech Spec Required Shutdown Due to Degradation of Containment Coatings ENS 420202005-09-27T15:00:00027 September 2005 15:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Postulated Faults Have Electrical Current in Excess of the Maximum Listed Interrupting Ratings. ENS 418562005-07-20T09:51:00020 July 2005 09:51:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Minimum Recirculation Valves Will Not Automatically Open in Local Operating Mode ENS 417582005-06-08T22:24:0008 June 2005 22:24:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Unanalyzed Condition - Fire Organizational Plan No Longer Aligned with Safe Shutdown Analysis ENS 417542005-06-07T23:00:0007 June 2005 23:00:00 10 CFR 50.72(b)(3)(ii)(B), Unanalyzed Condition Appendix R Safe Shutdown Strategy Deficiency 2018-03-01T22:43:00 | |