ENS 44629
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ENS Event | |
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05:57 Nov 5, 2008 | |
Title | Emergency Diesel Generator Start Due to Unexpected Esf Signal |
Event Description | This is an 8-hour notification to report a valid ESF signal to start the 1A Emergency Diesel Generator that occurred on 11/5/08 at 0057. Salem Unit 1 is in Mode 5, with core cooling being provided by 12 RHR pump. The Reactor Coolant System is being maintained at 173 F and 315 PSIG with a pressurizer level of 35 percent. The operating crew was performing a load shed surveillance test for a single component IAW test plan. The test plan used the Safeguards Equipment Cabinet (SEC) test pushbuttons to verify the equipment's response to a load shed signal. When the 1A SEC test pushbutton was actuated in addition to testing the single component it opened the in-feed breaker to the 1A 4KV vital bus and the bus was de-energized and loaded in blackout conditions. All equipment functioned as designed and core cooling was unaffected and remained in-service from 12 RHR pump powered from 1B 4KV bus. Investigation revealed the test plan did not take into account all components operated by the test pushbutton and the test pushbutton operated as designed. The 1A 4KV vital bus was restored to off-site power and the 1A EDG was restored to a standby condition. There were no personnel injured during the event.
The NRC Resident Inspector has been notified. LAC Township was notified by the licensee. Notified R1DO (Caruso). |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+-0.22 h-0.00917 days <br />-0.00131 weeks <br />-3.01356e-4 months <br />) | |
Opened: | Tom Byykkonen 05:44 Nov 5, 2008 |
NRC Officer: | Donald Norwood |
Last Updated: | Nov 5, 2008 |
44629 - NRC Website
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Unit 1 | |
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Reactor critical | Not Critical |
Scram | No |
Before | Cold Shutdown (0 %) |
After | Cold Shutdown (0 %) |
WEEKMONTHYEARENS 562862022-12-24T07:22:00024 December 2022 07:22:00
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Loss of an Operating Steam Generator Feed Pump (Sgfp) ENS 486172012-12-21T10:28:00021 December 2012 10:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Trip on Turbine Trip ENS 485342012-11-25T16:30:00025 November 2012 16:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Steam Generator Feedwater Regulator Valve Not Responding to Demand Signal ENS 484572012-10-30T05:09:00030 October 2012 05:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip from 100% Power ENS 477662012-03-23T18:28:00023 March 2012 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Followed by Automatic Reactor Trip ENS 469922011-06-26T04:00:00026 June 2011 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pump ENS 467742011-04-21T20:01:00021 April 2011 20:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Circulating Water Pumps Out of Service ENS 463372010-10-17T09:12:00017 October 2010 09:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to 4 Kv Group Bus Undervoltage Condition ENS 463362010-10-16T03:21:00016 October 2010 03:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Turbine Trip ENS 460752010-07-07T15:17:0007 July 2010 15:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Caused by Main Generator and Turbine Trip ENS 458482010-04-16T20:41:00016 April 2010 20:41:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Emergency Diesel Generator Start Due to Loss of a 4160 V Bus ENS 456472010-01-21T23:20:00021 January 2010 23:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 456042010-01-03T13:04:0003 January 2010 13:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Circulators After Uptake of River Ice ENS 446292008-11-05T05:57:0005 November 2008 05:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Start Due to Unexpected Esf Signal ENS 438732007-12-28T22:54:00028 December 2007 22:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip on Failure of Station Power Transformer ENS 435502007-08-06T17:10:0006 August 2007 17:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Spurious Interlock Signal to Feedwater Regulating Valves ENS 432592007-03-28T00:50:00028 March 2007 00:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Low Steam Generator Water Level Initiated Auxiliary Feedwater Signal and a Reactor Trip Signal ENS 429462006-10-30T01:11:00030 October 2006 01:11:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of Auxiliary Feedwater During Msiv Testing ENS 423952006-03-08T16:09:0008 March 2006 16:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip as a Result of a Turbine Generator Trip ENS 408752004-07-15T23:44:00015 July 2004 23:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Trip from 8% Power Due to Lowering Water Level on 23 Steam Generator ENS 408652004-07-13T17:05:00013 July 2004 17:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Low Steam Generator Water Level. ENS 406652004-04-11T04:23:00011 April 2004 04:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Plant Had a Valid Esf Signal to Start 1C Emergency Diesel Generator ENS 406392004-04-03T15:50:0003 April 2004 15:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Auxiliary Feedwater System During Maintenance 2022-12-24T07:22:00 | |
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