ENS 43259
ENS Event | |
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00:50 Mar 28, 2007 | |
Title | |
Event Description | This 8-hour notification is being made to report that an Auxiliary Feedwater (AFW) system actuation signal was generated and a Reactor Protective Signal (RPS) generated with the reactor subcritical.
On March 27, 2007 at approximately 2050, Salem Unit 1 was in Mode 3 following a planned manual reactor trip to begin a scheduled refueling outage. Operators had established initial Reactor Coolant System cooldown using the steam dumps for heat removal and the 11, 12, and 13 AFW pumps for steam generator make-up. All three pumps had been previously placed in-service in accordance with plant procedures. As plant cooldown proceeded, narrow range levels in 11, 12, and 13 Steam Generators reached the low steam generator setpoint trip, resulting in a valid ESF actuation (i.e., start signal to the AFW pumps); however all AFW pumps were already in-service. The actuation signal also generated a reactor trip signal to be initiated by the reactor protection system; however, the plant was already in a shutdown condition with the reactor trip breakers open. The lowest level during this transient occurred in 13 Steam Generator and was 11.3% narrow range level. Steam generator water level was restored to a normal value and the RCS cooldown recommenced. There were no equipment failures that contributed to this event. The NRC Resident has been informed. |
Where | |
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Salem New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
Time - Person (Reporting Time:+1.02 h0.0425 days <br />0.00607 weeks <br />0.0014 months <br />) | |
Opened: | Jason Hancock 01:51 Mar 28, 2007 |
NRC Officer: | Jason Kozal |
Last Updated: | Mar 28, 2007 |
43259 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Not Critical |
Scram | No |
Before | Hot Standby (0 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 562862022-12-24T07:22:00024 December 2022 07:22:00
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System Actuation Automatic Reactor Trip Due to Main Turbine Trip ENS 512902015-08-05T19:38:0005 August 2015 19:38:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Reactor Coolant Flow ENS 505502014-10-20T00:51:00020 October 2014 00:51:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Resulting in Aux Feedwater Actuation ENS 500922014-05-07T08:56:0007 May 2014 08:56:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip Due to Generator Protection Relay ENS 500322014-04-14T01:13:00014 April 2014 01:13:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Actuation of Main Generator Protection Relay ENS 500122014-04-09T01:14:0009 April 2014 01:14:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Manually Tripped Following the Loss of an Operating Steam Generator Feed Pump (Sgfp) ENS 486172012-12-21T10:28:00021 December 2012 10:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Trip on Turbine Trip ENS 485342012-11-25T16:30:00025 November 2012 16:30:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Steam Generator Feedwater Regulator Valve Not Responding to Demand Signal ENS 484572012-10-30T05:09:00030 October 2012 05:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip from 100% Power ENS 477662012-03-23T18:28:00023 March 2012 18:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Turbine Trip Followed by Automatic Reactor Trip ENS 469922011-06-26T04:00:00026 June 2011 04:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Reactor Coolant Pump ENS 467742011-04-21T20:01:00021 April 2011 20:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Circulating Water Pumps Out of Service ENS 463372010-10-17T09:12:00017 October 2010 09:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to 4 Kv Group Bus Undervoltage Condition ENS 463362010-10-16T03:21:00016 October 2010 03:21:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Turbine Trip ENS 460752010-07-07T15:17:0007 July 2010 15:17:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Caused by Main Generator and Turbine Trip ENS 458482010-04-16T20:41:00016 April 2010 20:41:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unplanned Emergency Diesel Generator Start Due to Loss of a 4160 V Bus ENS 456472010-01-21T23:20:00021 January 2010 23:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Low Steam Generator Water Level ENS 456042010-01-03T13:04:0003 January 2010 13:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Circulators After Uptake of River Ice ENS 446292008-11-05T05:57:0005 November 2008 05:57:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Emergency Diesel Generator Start Due to Unexpected Esf Signal ENS 438732007-12-28T22:54:00028 December 2007 22:54:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Trip on Failure of Station Power Transformer ENS 435502007-08-06T17:10:0006 August 2007 17:10:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Trip Due to Spurious Interlock Signal to Feedwater Regulating Valves ENS 432592007-03-28T00:50:00028 March 2007 00:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Low Steam Generator Water Level Initiated Auxiliary Feedwater Signal and a Reactor Trip Signal ENS 429462006-10-30T01:11:00030 October 2006 01:11:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Start of Auxiliary Feedwater During Msiv Testing ENS 423952006-03-08T16:09:0008 March 2006 16:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip as a Result of a Turbine Generator Trip ENS 408752004-07-15T23:44:00015 July 2004 23:44:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Trip from 8% Power Due to Lowering Water Level on 23 Steam Generator ENS 408652004-07-13T17:05:00013 July 2004 17:05:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on Low Low Steam Generator Water Level. ENS 406652004-04-11T04:23:00011 April 2004 04:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Plant Had a Valid Esf Signal to Start 1C Emergency Diesel Generator ENS 406392004-04-03T15:50:0003 April 2004 15:50:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Actuation of Auxiliary Feedwater System During Maintenance 2022-12-24T07:22:00 | |